The company was facing higher machine downtime on the manufacturing line. After carrying out the root cause analysis using various lean tools such as 5W 1H, Ishikawa Diagram, and Pareto Chart conclusion has been made that die changeover is the root cause of the machine downtime. SMED implementation kick-off started with observing the current changeover activities. After that various kind of wastes identified. External and Internal activities separated and internal activities are streamlined using Precedence diagram and Gantt chart. That has resulted in standard work operations and increased parallel activities. The previous changeover time was 252 minutes and after SMED implementation it is estimated that changeover will be completed in 72 minutes.