The document discusses redesigning the cold forging process and tooling for producing a valve tappet part. The original single-stage process resulted in inconsistent and excessive head offsetting. Analyzing the process found the D2/d2 and l/d ratios exceeded standards. Recalculations determined a two-stage process with an intermediate stepped blank was needed. Trials with new tooling produced satisfactory results with low, consistent head offsetting. Implementation of the redesigned two-stage process and tooling solved the issues, improved dimensions consistency, reduced setup time and waste.