The variable frequency drive controlling the CO2 compressor motor at an IFFCO fertilizer plant was causing problems by shutting off during faults and not allowing individual control of motor speed. Modifications were made to allow faults to be diagnosed, run the motor individually without other equipment, and reduce motor speed to match compressor needs. This eliminated issues like backups and saved over Rs. 10 lacs annually in energy costs while improving plant output. The implemented suggestions received awards and recognition for the employee.