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Circulating Water Pump-A Overhauling Report
 
November 27, 2011-December 01, 2011
Prepared by
Md. Maruf Akhtar
Maintenance Planner
Haripur Power Limited
Co-Author
Ashik Ahmed
Maintenance Engineer
Haripur Power Limited
Checked by
A.B. Siddique
MMT Supervisor
Haripur Power Limited
Approved by
Kazi Samsul Alam
Plant Manager
Haripur Power Limited
2222
November 27, 2011-December 01, 2011
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22//1199
Equipment No: CW-M-PP-03A
Equipment Name: Circulating Water Pump-A
History
Haripur have two cooling water pump (CWP-A/B) each 50% capacity. According to
schedule maintenance plan each pump is overhauled after 16,000 running hours.
The overhauling work of cooling water pump is carried out in advance of schedule
outage for minimize the outage task and foreign vendor support. CWP-A was scheduled
for overhauling in Feb-2012 and it was decided to complete in Dec-2011.
The pump suction is from river water to discharge to water boxes of steam condenser.
It’s a vertical shaft, 1350 discharge bore mixed flow pump. It’s driven by an 1100 KW
vertically mounted motor with a rated full load rpm of 494. Rated flow rate of the
pump is 18, 600 m3/hr.
Before the overhauling CWP-A, NDE side vibration of motor as being monitored was too
high for its sound performance. Vertical vibration data at NDE was measured as high as
6.3 mm/sec which was way alarming.
Suspected regions were out-clearances of bearings and wear-rings. O & M came to a
decision for complete overhauling of the pump which started on November 27, 2011
and was completed on December 01, 2011.
Specification of the Equipment and History of CWP-A
overhauling works
Circulating Water Pump-A (Vertical Mixed Flow Pump)
Installed in year: 2000
PPPuuummmppp DDDeeetttaaaiiilllsss
Shop Order No KA0366
Serial No: KA0366-CWP-001 (or 002) For Pump A & B.
Tag No: CW-M-PP-03-1
Capacity 18,600 m3/hr
Total Head 16M
Speed 493 RPM
Power 1100KW
3333
November 27, 2011-December 01, 2011
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MMMoootttooorrr DDDaaatttaaa
Manufactured By
Electric Motor Manufacture Dept.
Industrial & Power System Division
Hyundai Heavy Industries Co, Ltd.
1,CHEONHA-DONG,DONG-KU,ULSAN,KOREA
Tel: 82-52-230-6671,72
Motor Application C.W.Pump
Rated HP/KW 1474.5 HP/1100KW
Motor Type SQUIRREL, CAGE
Frame No HLA7 902-36Y
Rated Voltage 6600 V
Phase 3 phase Induction/50HZ
Full Load Current 134.7 A
Speed Synchronous 500/494
MMMaaaiiinnnttteeennnaaannnccceee HHHiiissstttooorrryyy CCCWWWPPP---AAA
CWP-A was overhauled in Feb-2006, Feb-2008 and Mar-2010 as a part of scheduled
maintenance. Next overhauling was scheduled in Feb-2012 but we started the work
two months earlier to reduce coming outage (scheduled in Feb-2012) activities and to
concentrate more on outage-2012.
Dismantling Procedure
The motor-pump assembly was disassembled with the following steps:
The stop gate
was inserted
into the intake
basin with the
help of gantry
crane.
4444
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Note: before inserting the gate, it’s important to grease the slots of the gate; the
slots will guide thru the railing inside the basin.
3 submergible pumps (ф4” & ф3”) were being placed inside the intake basin to
continuously pump out water.
Note: submerge pumps were drawn to the intake when inside water level was reduced
to 310 cm and this was done by running the main pump for few seconds after placing
the stop gate.
The pump was then stopped and motor was isolated.
Pump was decoupled from the motor and lift of the pump was noted as 11.1
mm
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November 27, 2011-December 01, 2011
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Note: there are 6 stud bolts and 6 reamer bolts in the coupling. Space nut is screwed
to the pump shaft and pump end hub is keyed to the shaft which drops down after
loosening the coupling bolts.
Cooling water lines had been removed.
The motor and motor pedestal was sequentially removed by gantry crane.
3 gland packing were removed by screw driver.
Gland and upper bearing housing (brg housing o-ring, P#1492 to be reused)
were removed afterward; all these were lifted using eyebolt-shackle-belt
assembly of appropriate sizes.
Elbow cover was lifted (after removing tow center pins) by the crane up to
when the top spider hoisted over the column pipe as it was to be supported by
H-beam underneath.
Elbow cover and upper shaft tube were unfastened sequentially.
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November 27, 2011-December 01, 2011
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Note: There is a distance ring which rests between elbow cover and upper shaft tube
which must be handled and kept safely.
Note: There is a tapering part in every leg of the spider and this side would face the
downside while assembling.
7777
November 27, 2011-December 01, 2011
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Upper spider along with the intermediate shaft tube was then dismantled after
lifting the resting assembly as long as the lower spider was supported similarly.
The upper shaft was then separated from the lower shaft by dismantling the
line shaft coupling & thrust ring using special tool as seen in the figure.
Lower spider, lower enclosure tube,
discharge bowl and impeller were then
taken out altogether and spider-tube
was dismantled in similar fashion.
Discharge bowl was separated from the
impeller-shaft assembly by removing
the stopper ring.
8888
November 27, 2011-December 01, 2011
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Note: Match marking is provided in every part disassembled.
Shaft was disassembled separated from the impeller using an extractor.
Note: Impeller washer must be removed first before extracting impeller from the
shaft using special tool (mechanical jacking).
Casing wear ring was pulled using hydraulic jack & a fabricated special jack
with nearly 100 bar of pressure. Impeller wear ring was extracted by tapping &
unscrewing it.
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November 27, 2011-December 01, 2011
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Dummy Inspection
Dummy inspection refers to
checking whether discharge bowl
seats in its slots after assembling
it with only shaft tubes, spiders
and elbow cover.
After assembling all these and
tightening the elbow cover on its
bolts; a gap of 3 mm found
beneath the discharge bowl on its
seating slots. It had to be
compensated. A shim of 3 mm
was ordered instantly with same
shape of distance ring from
nearby workshop of stainless
steel.
Findings
Followings were the findings on disassembly:
 Stop ring set-screw (one out of two) was found loose when dismantling.
 Casing wear ring and impeller wear ring were found heavily eroded.
 Impeller blade edges were found rubbed (perhaps with the impeller liner).
10101010
November 27, 2011-December 01, 2011
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 Discharge bowl anti-rotation pins were found partially sheared and were
repaired by build-up & grinding before assembly.
Note: Keys are marked as in the table:
Mark Position
1-1 Impeller-lower shaft
1-2 Lower shaft-line coupling
1-3 Upper shaft-line coupling
1-4 Pump end hub-upper shaft
Assembly
Before assembling, feroform bearings and sleeves were forcibly taken out. New
fabricated casing wear ring & impeller wear rings (from local workshop) were dressed
with set-screws being punched and countered on respective housings. Impeller liner &
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November 27, 2011-December 01, 2011
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1111//1199
basin surroundings were checked and declared fine to go in. Shaft run-out and sleeve-
bearing clearances were measured and found within the operative range. Discharge
bowl was painted by Barger Marine Black on its non-mating portions with inside
column. Elbow O-ring and bowl O-ring were fabricated locally from cord.
Clearances
Lower Sleeve Intern Sleeve 1 Intern Sleeve 2 Upper Sleeve
Brg Dia 180.40 mm 180.50 mm 180.30 mm 180.46 mm
Sleeve Dia 179.79 mm 179.90 mm 179.90 mm 179.86 mm
Clearance 0.61 mm 0.60 mm 0.40 mm 0.60 mm
Design 0.481-0.679 0.453-0.650 0.453-0.650 0.453-0.650
Shaft Run-out
Both shafts were properly cleaned; run-outs as measured are:
1 2 3 4 5 6 7
Upper ShaftMotor Side
1 2 3 4 5 6 7
Lower Shaft
Impeller Side
12121212
November 27, 2011-December 01, 2011
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Dial gauge readings corresponding to the points on upper shaft
-0.01
0
-0.030.04
Point 1
-0.02
0
-0.01-0.02
Point 2
-0.11
0
-0.08-0.04
Point 3
-0.12
0
-0.11-0.02
Point 4
-0.11
0
-0.09-0.03
Point 5
-0.06
0
-0.050.02
Point 6
0.03
0
0.06-0.01
Point 7
13131313
November 27, 2011-December 01, 2011
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1133//1199
Dial gauge readings corresponding to the points on lower shaft
0.13
0
0.070.08
Point 1
-0.09
0
-0.03-0.05
Point 2
-0.11
0
-0.05-0.10
Point 3
-0.12
0
-0.01-0.11
Point 4
-0.14
0
-0.01-0.11
Point 5
-0.08
0
0.01-0.04
Point 6
0.12
0
0.020.12
Point 7
14141414
November 27, 2011-December 01, 2011
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1144//1199
 Maximum run-out noticed 0.14 mm and it was same as of previous overhauling.
 Feroform bearings were put in deep-fridge in the Canteen for long 14 hours.
Now they could easily dig-into the respective places.
 There was an obvious gap between the split pieces of the stop ring when they
were placed to screw over the shaft.
 Whole assembly was just the reverse of disassembly.
Motor Inspection
 Motor NDE side fan cover removed and cleaned.
 Motor DE side cleaned.
 Motor cooler’s all cooling holes cleaned.
 NDE side Bearing oil replaced with new oil (DTE 15M, approx-200 ltr.)
 Motor Insulation resistance checked & found IR-10 Gohm, WR-0.79 ohm.
 Motor space heater checked & found WR-29 ohm
 DE side bearing greased and grease chamber opened for checking the grease
condition of the bearing and found satisfactory.
Checks on assembly
To confirm whether the discharge bowl seats
on its slots with no unwanted gap after
inserting extra 3 mm shim (with existing
distance ring) underneath the elbow cover. It
was checked and found ok.
15151515
November 27, 2011-December 01, 2011
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1155//1199
Greasing to all spider leg sides, O-ring grooves.
Plating Molykote to the bolts, studs, sleeves, thrust rings, impeller washer,
shaft coupling & all other mating surfaces etc.
Tightening the bolts in a crisscross pattern like the following:
Alignment
After reinstalling motor pedestal and motor, gap between motor coupling and pump
coupling was kept 10.5 mm by turning the space nut toward the motor hub ensuring
the required gap.
A steel scale was kept stood
vertically in the hub surfaces
and motor jacks were adjusted
to bring the required alignment.
When the centerline of the
pump & motor was confirmed,
the hubs were coupled with
reamer bolts. Now the tip
Steel Scale
16161616
November 27, 2011-December 01, 2011
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1166//1199
clearances (radial clearances of the impeller and impeller liner in the suction bell)
were recorded. The values are:
POS E W N S
1 2.8 1.60 2.95 1.65
2 3.2 1.80 1.90 3.40
3 1.80 2.70 2.05 3.00
4 1.95 2.45 2.90 1.85
Tip clearances were judged good. Now relative position of the shaft assembly against
static elbow cover-brg housing-gland was adjusted by adjusting motor. After
adjustment, alignment readings are as follows:
For example in the East side of the shaft; distance of the shaft from the gland is
109.84 mm as measured by inside micrometer. These readings show good centering of
the pump
W E
N
S
109.92 109.84
109.82
109.94
17171717
November 27, 2011-December 01, 2011
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1177//1199
Modifications
 Ladder arrangement (between band screen &
gantry crane entry hole) inside the basin has
been modified to facilitate larger size (ф6”)
submerge pumps to travel in.
 2 angle bars have been welded to the column
pipe outer body to ease climbing to the gland
packing area inspection while the pump is
running.
Start-up
Here is a comparison of data of vibration parameters of the M/C taken both before and
after maintenance:
Before Maintenance (9:00 hrs on 20-Nov-11)
Vibration in mm/sec
Temp (0C)
Motor Current
(amp)
Inside Water
Level (mm)Position H V A
Pump DE 1.5 2.3 0.9
117 5331
Pump NDE 1.0 1.4 0.6
Motor DE 2.6 4.4 1.0 48
Motor NDE 3.8 6.3 0.7 42
After Maintenance (After start-up at 20:15 hrs on 01-Dec-11)
Vibration in mm/sec
Temp (0C)
Motor Current
(amp)
Inside Water
Level (mm)Position H V A
Pump DE 1.1 1.4 0.6
114 4900Pump NDE 0.5 1.1 0.3
Motor DE 2.1 2.4 1.0 40
18181818
November 27, 2011-December 01, 2011
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1188//1199
Motor NDE 3.2 2.8 1.0 38
Spares List
Following spares have been consumed:
SL Code No Description Qty
1 CW-M-PP-03--BRNG-01 Submerge Brg, Intermediate 02 EA
2 CW-M-PP-03--BRNG-02 Submerge Brg, lower 01 EA
3 CW-M-PP-03--BRNG-03 Submerge Brg, upper 01 EA
4 CW-M-PP-03--PACK-01 Gland Packing, P#1391 01 EA (03 pcs)
5 CW-M-PP-03--SLVE-01 Packing Sleeve, P#1227 01 EA
6 CW-M-PP-03--SLVE-02 Shaft Sleeve, upper P#1224 01 EA
7 CW-M-PP-03--SLVE-03 Shaft Sleeve, inter P#1225 02 EA
8 CW-M-PP-03--SLVE-04 Shaft Sleeve, lower P#1226 01 EA
9 CW-M-PP-03--RING-01 Casing Wear Ring, P#1261 01 EA
10 CW-M-PP-03--RING-02 Impeller Wear Ring, P#1262 01 EA
Workforce
Overall Supervision A.B. Siddique, MMT Supervisor
Craft Person: Md. Saiful Islam, MMT Engineer
HPL Working Person MMT Engineers-Hanif, Enamul, Ashik, Maruf
Maintenance Assistance
Amzad (Rigging), Islam (Crane Operation), Muktar
(Welding/heating)
Local Labor Tapas, Mahtab (High Skilled Technicians)
19191919
November 27, 2011-December 01, 2011
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1199//1199
Achievements
Spares (SL. 9 & 10) had been fabricated from local workshop. These are precision
items made from SS and this was a challenge for us. We have overcome the challenge
successfully and it saves significant amount of money worth USD 9,000.00. Previously
these two items were foreign purchased with USD 10,015.00 and this time cost was
around USD 1100.00 as made by local fabrication.
Conclusion
Pump overhauling is done earlier than scheduled time and it was put into service at
the 5th day from shutdown. Moreover an additional inspection (discharge bowl gap
checking by dummy assembly) is done this time. We also learn that a significant cost
can be reduced by exploring local manufacturing of such spares. Pump vibration and
other parameters became smoother after the overhauling.

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Maintenance report on Circulating Water Pump (CWP) Overhauling

  • 1.   Circulating Water Pump-A Overhauling Report   November 27, 2011-December 01, 2011 Prepared by Md. Maruf Akhtar Maintenance Planner Haripur Power Limited Co-Author Ashik Ahmed Maintenance Engineer Haripur Power Limited Checked by A.B. Siddique MMT Supervisor Haripur Power Limited Approved by Kazi Samsul Alam Plant Manager Haripur Power Limited
  • 2. 2222 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    22//1199 Equipment No: CW-M-PP-03A Equipment Name: Circulating Water Pump-A History Haripur have two cooling water pump (CWP-A/B) each 50% capacity. According to schedule maintenance plan each pump is overhauled after 16,000 running hours. The overhauling work of cooling water pump is carried out in advance of schedule outage for minimize the outage task and foreign vendor support. CWP-A was scheduled for overhauling in Feb-2012 and it was decided to complete in Dec-2011. The pump suction is from river water to discharge to water boxes of steam condenser. It’s a vertical shaft, 1350 discharge bore mixed flow pump. It’s driven by an 1100 KW vertically mounted motor with a rated full load rpm of 494. Rated flow rate of the pump is 18, 600 m3/hr. Before the overhauling CWP-A, NDE side vibration of motor as being monitored was too high for its sound performance. Vertical vibration data at NDE was measured as high as 6.3 mm/sec which was way alarming. Suspected regions were out-clearances of bearings and wear-rings. O & M came to a decision for complete overhauling of the pump which started on November 27, 2011 and was completed on December 01, 2011. Specification of the Equipment and History of CWP-A overhauling works Circulating Water Pump-A (Vertical Mixed Flow Pump) Installed in year: 2000 PPPuuummmppp DDDeeetttaaaiiilllsss Shop Order No KA0366 Serial No: KA0366-CWP-001 (or 002) For Pump A & B. Tag No: CW-M-PP-03-1 Capacity 18,600 m3/hr Total Head 16M Speed 493 RPM Power 1100KW
  • 3. 3333 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    33//1199 MMMoootttooorrr DDDaaatttaaa Manufactured By Electric Motor Manufacture Dept. Industrial & Power System Division Hyundai Heavy Industries Co, Ltd. 1,CHEONHA-DONG,DONG-KU,ULSAN,KOREA Tel: 82-52-230-6671,72 Motor Application C.W.Pump Rated HP/KW 1474.5 HP/1100KW Motor Type SQUIRREL, CAGE Frame No HLA7 902-36Y Rated Voltage 6600 V Phase 3 phase Induction/50HZ Full Load Current 134.7 A Speed Synchronous 500/494 MMMaaaiiinnnttteeennnaaannnccceee HHHiiissstttooorrryyy CCCWWWPPP---AAA CWP-A was overhauled in Feb-2006, Feb-2008 and Mar-2010 as a part of scheduled maintenance. Next overhauling was scheduled in Feb-2012 but we started the work two months earlier to reduce coming outage (scheduled in Feb-2012) activities and to concentrate more on outage-2012. Dismantling Procedure The motor-pump assembly was disassembled with the following steps: The stop gate was inserted into the intake basin with the help of gantry crane.
  • 4. 4444 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    44//1199 Note: before inserting the gate, it’s important to grease the slots of the gate; the slots will guide thru the railing inside the basin. 3 submergible pumps (ф4” & ф3”) were being placed inside the intake basin to continuously pump out water. Note: submerge pumps were drawn to the intake when inside water level was reduced to 310 cm and this was done by running the main pump for few seconds after placing the stop gate. The pump was then stopped and motor was isolated. Pump was decoupled from the motor and lift of the pump was noted as 11.1 mm
  • 5. 5555 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    55//1199 Note: there are 6 stud bolts and 6 reamer bolts in the coupling. Space nut is screwed to the pump shaft and pump end hub is keyed to the shaft which drops down after loosening the coupling bolts. Cooling water lines had been removed. The motor and motor pedestal was sequentially removed by gantry crane. 3 gland packing were removed by screw driver. Gland and upper bearing housing (brg housing o-ring, P#1492 to be reused) were removed afterward; all these were lifted using eyebolt-shackle-belt assembly of appropriate sizes. Elbow cover was lifted (after removing tow center pins) by the crane up to when the top spider hoisted over the column pipe as it was to be supported by H-beam underneath. Elbow cover and upper shaft tube were unfastened sequentially.
  • 6. 6666 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    66//1199 Note: There is a distance ring which rests between elbow cover and upper shaft tube which must be handled and kept safely. Note: There is a tapering part in every leg of the spider and this side would face the downside while assembling.
  • 7. 7777 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    77//1199 Upper spider along with the intermediate shaft tube was then dismantled after lifting the resting assembly as long as the lower spider was supported similarly. The upper shaft was then separated from the lower shaft by dismantling the line shaft coupling & thrust ring using special tool as seen in the figure. Lower spider, lower enclosure tube, discharge bowl and impeller were then taken out altogether and spider-tube was dismantled in similar fashion. Discharge bowl was separated from the impeller-shaft assembly by removing the stopper ring.
  • 8. 8888 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    88//1199 Note: Match marking is provided in every part disassembled. Shaft was disassembled separated from the impeller using an extractor. Note: Impeller washer must be removed first before extracting impeller from the shaft using special tool (mechanical jacking). Casing wear ring was pulled using hydraulic jack & a fabricated special jack with nearly 100 bar of pressure. Impeller wear ring was extracted by tapping & unscrewing it.
  • 9. 9999 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    99//1199 Dummy Inspection Dummy inspection refers to checking whether discharge bowl seats in its slots after assembling it with only shaft tubes, spiders and elbow cover. After assembling all these and tightening the elbow cover on its bolts; a gap of 3 mm found beneath the discharge bowl on its seating slots. It had to be compensated. A shim of 3 mm was ordered instantly with same shape of distance ring from nearby workshop of stainless steel. Findings Followings were the findings on disassembly:  Stop ring set-screw (one out of two) was found loose when dismantling.  Casing wear ring and impeller wear ring were found heavily eroded.  Impeller blade edges were found rubbed (perhaps with the impeller liner).
  • 10. 10101010 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1100//1199  Discharge bowl anti-rotation pins were found partially sheared and were repaired by build-up & grinding before assembly. Note: Keys are marked as in the table: Mark Position 1-1 Impeller-lower shaft 1-2 Lower shaft-line coupling 1-3 Upper shaft-line coupling 1-4 Pump end hub-upper shaft Assembly Before assembling, feroform bearings and sleeves were forcibly taken out. New fabricated casing wear ring & impeller wear rings (from local workshop) were dressed with set-screws being punched and countered on respective housings. Impeller liner &
  • 11. 11111111 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1111//1199 basin surroundings were checked and declared fine to go in. Shaft run-out and sleeve- bearing clearances were measured and found within the operative range. Discharge bowl was painted by Barger Marine Black on its non-mating portions with inside column. Elbow O-ring and bowl O-ring were fabricated locally from cord. Clearances Lower Sleeve Intern Sleeve 1 Intern Sleeve 2 Upper Sleeve Brg Dia 180.40 mm 180.50 mm 180.30 mm 180.46 mm Sleeve Dia 179.79 mm 179.90 mm 179.90 mm 179.86 mm Clearance 0.61 mm 0.60 mm 0.40 mm 0.60 mm Design 0.481-0.679 0.453-0.650 0.453-0.650 0.453-0.650 Shaft Run-out Both shafts were properly cleaned; run-outs as measured are: 1 2 3 4 5 6 7 Upper ShaftMotor Side 1 2 3 4 5 6 7 Lower Shaft Impeller Side
  • 12. 12121212 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1122//1199 Dial gauge readings corresponding to the points on upper shaft -0.01 0 -0.030.04 Point 1 -0.02 0 -0.01-0.02 Point 2 -0.11 0 -0.08-0.04 Point 3 -0.12 0 -0.11-0.02 Point 4 -0.11 0 -0.09-0.03 Point 5 -0.06 0 -0.050.02 Point 6 0.03 0 0.06-0.01 Point 7
  • 13. 13131313 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1133//1199 Dial gauge readings corresponding to the points on lower shaft 0.13 0 0.070.08 Point 1 -0.09 0 -0.03-0.05 Point 2 -0.11 0 -0.05-0.10 Point 3 -0.12 0 -0.01-0.11 Point 4 -0.14 0 -0.01-0.11 Point 5 -0.08 0 0.01-0.04 Point 6 0.12 0 0.020.12 Point 7
  • 14. 14141414 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1144//1199  Maximum run-out noticed 0.14 mm and it was same as of previous overhauling.  Feroform bearings were put in deep-fridge in the Canteen for long 14 hours. Now they could easily dig-into the respective places.  There was an obvious gap between the split pieces of the stop ring when they were placed to screw over the shaft.  Whole assembly was just the reverse of disassembly. Motor Inspection  Motor NDE side fan cover removed and cleaned.  Motor DE side cleaned.  Motor cooler’s all cooling holes cleaned.  NDE side Bearing oil replaced with new oil (DTE 15M, approx-200 ltr.)  Motor Insulation resistance checked & found IR-10 Gohm, WR-0.79 ohm.  Motor space heater checked & found WR-29 ohm  DE side bearing greased and grease chamber opened for checking the grease condition of the bearing and found satisfactory. Checks on assembly To confirm whether the discharge bowl seats on its slots with no unwanted gap after inserting extra 3 mm shim (with existing distance ring) underneath the elbow cover. It was checked and found ok.
  • 15. 15151515 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1155//1199 Greasing to all spider leg sides, O-ring grooves. Plating Molykote to the bolts, studs, sleeves, thrust rings, impeller washer, shaft coupling & all other mating surfaces etc. Tightening the bolts in a crisscross pattern like the following: Alignment After reinstalling motor pedestal and motor, gap between motor coupling and pump coupling was kept 10.5 mm by turning the space nut toward the motor hub ensuring the required gap. A steel scale was kept stood vertically in the hub surfaces and motor jacks were adjusted to bring the required alignment. When the centerline of the pump & motor was confirmed, the hubs were coupled with reamer bolts. Now the tip Steel Scale
  • 16. 16161616 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1166//1199 clearances (radial clearances of the impeller and impeller liner in the suction bell) were recorded. The values are: POS E W N S 1 2.8 1.60 2.95 1.65 2 3.2 1.80 1.90 3.40 3 1.80 2.70 2.05 3.00 4 1.95 2.45 2.90 1.85 Tip clearances were judged good. Now relative position of the shaft assembly against static elbow cover-brg housing-gland was adjusted by adjusting motor. After adjustment, alignment readings are as follows: For example in the East side of the shaft; distance of the shaft from the gland is 109.84 mm as measured by inside micrometer. These readings show good centering of the pump W E N S 109.92 109.84 109.82 109.94
  • 17. 17171717 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1177//1199 Modifications  Ladder arrangement (between band screen & gantry crane entry hole) inside the basin has been modified to facilitate larger size (ф6”) submerge pumps to travel in.  2 angle bars have been welded to the column pipe outer body to ease climbing to the gland packing area inspection while the pump is running. Start-up Here is a comparison of data of vibration parameters of the M/C taken both before and after maintenance: Before Maintenance (9:00 hrs on 20-Nov-11) Vibration in mm/sec Temp (0C) Motor Current (amp) Inside Water Level (mm)Position H V A Pump DE 1.5 2.3 0.9 117 5331 Pump NDE 1.0 1.4 0.6 Motor DE 2.6 4.4 1.0 48 Motor NDE 3.8 6.3 0.7 42 After Maintenance (After start-up at 20:15 hrs on 01-Dec-11) Vibration in mm/sec Temp (0C) Motor Current (amp) Inside Water Level (mm)Position H V A Pump DE 1.1 1.4 0.6 114 4900Pump NDE 0.5 1.1 0.3 Motor DE 2.1 2.4 1.0 40
  • 18. 18181818 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1188//1199 Motor NDE 3.2 2.8 1.0 38 Spares List Following spares have been consumed: SL Code No Description Qty 1 CW-M-PP-03--BRNG-01 Submerge Brg, Intermediate 02 EA 2 CW-M-PP-03--BRNG-02 Submerge Brg, lower 01 EA 3 CW-M-PP-03--BRNG-03 Submerge Brg, upper 01 EA 4 CW-M-PP-03--PACK-01 Gland Packing, P#1391 01 EA (03 pcs) 5 CW-M-PP-03--SLVE-01 Packing Sleeve, P#1227 01 EA 6 CW-M-PP-03--SLVE-02 Shaft Sleeve, upper P#1224 01 EA 7 CW-M-PP-03--SLVE-03 Shaft Sleeve, inter P#1225 02 EA 8 CW-M-PP-03--SLVE-04 Shaft Sleeve, lower P#1226 01 EA 9 CW-M-PP-03--RING-01 Casing Wear Ring, P#1261 01 EA 10 CW-M-PP-03--RING-02 Impeller Wear Ring, P#1262 01 EA Workforce Overall Supervision A.B. Siddique, MMT Supervisor Craft Person: Md. Saiful Islam, MMT Engineer HPL Working Person MMT Engineers-Hanif, Enamul, Ashik, Maruf Maintenance Assistance Amzad (Rigging), Islam (Crane Operation), Muktar (Welding/heating) Local Labor Tapas, Mahtab (High Skilled Technicians)
  • 19. 19191919 November 27, 2011-December 01, 2011 CCCIIIRRRCCCUUULLLAAATTTIIINNNGGG   WWWAAATTTEEERRR   PPPUUUMMMPPP‐‐‐AAA   OOOVVVEEERRRHHHAAAUUULLLIIINNNGGG   222000111111    1199//1199 Achievements Spares (SL. 9 & 10) had been fabricated from local workshop. These are precision items made from SS and this was a challenge for us. We have overcome the challenge successfully and it saves significant amount of money worth USD 9,000.00. Previously these two items were foreign purchased with USD 10,015.00 and this time cost was around USD 1100.00 as made by local fabrication. Conclusion Pump overhauling is done earlier than scheduled time and it was put into service at the 5th day from shutdown. Moreover an additional inspection (discharge bowl gap checking by dummy assembly) is done this time. We also learn that a significant cost can be reduced by exploring local manufacturing of such spares. Pump vibration and other parameters became smoother after the overhauling.