This document summarizes a study on improving productivity at an assembly station through work study techniques. The study involved observing the existing assembly process, identifying non-value added activities like transportation and delays, and proposing a new layout and process flow. Data was collected through manual time studies and video work studies. Analysis using Work Pro software showed the proposed method reduced cycle time from 45.49 to 30.94 minutes, improving productivity from 20 to 30 units per day. Ergonomic evaluation tools RULA and REBA also showed reduced risk of injury with the proposed method. The changes resulted in increased productivity while improving workplace ergonomics and safety.