Trident Group.

                 1
Trident – Geographies
                   Punjab, India – Dhaula Campus
                   600 Acres
                   Home Textiles, Energy and Paper Units
                   Takshashila (Center of Excellence)


                   Punjab, India – Sanghera Campus
                   350 Acres
                   Yarn Units, Ananda (Leadership Workshop
                   Center)

                   Madhya Pradesh, India – Budhni Campus
                   800 Acres
                   Yarn and Proposed Home Textiles Units



                   Corporate Office – Ludhiana, Punjab (India)
                   Sales Offices in NY (US), Delhi and Mumbai
                   (India)




2
Diversification through Integration

                                                                Power & Steam

                           Power



                                 Power                      Steam &
                                                            Sulphuric Acid
 TRIDENT YARN                            ENERGY                                 TRIDENT PAPER
  3.94 Lakhs Spindles/                   50 MW per day                            475 MTs per day
    275 MTs per day
                                                Power & Steam
                                 Yarn

                                                                                        Sulphuric
                                                                  Power
                                                                                        Acid

                         Terry Fabric                       Sulphuric Acid




 BATHROBES                                TOWEL                                 TRIDENT CHEM
                                                                                  275 MTs per day




  3
ENERGY CONSUMPTION DETAILS

                         CONSUMPTION       UNIT OF
S.NO.        ENERGY         AMOUNT      MEASUREMENT
  1        ELECTRICITY    125,297,782       KWH
  2           STEAM           6500         MT/DAY
  3      GROUND WATER       3650000       M3/YEAR
  4     RECYCLED WATER      1095000       M3/YEAR
  5       CO2 EMISSION       199429      TON CO2 EQ
Projects for FY 2013-2014


       S.No.                            Project Name                                UOM    Baseline   Target
         1         Reduction in specific power consumption in pulp area           KWH/MT     317       264
         2         Reduction in specific steam consumption in pulp area            MT/MT     2.68      2.41
         3        To improve the condensate return from towel and paper              %        66        74
         4       Reduction in specific power consumption in Paper machine         KWH/MT     344       335
         5       Reduction in specific steam consumption in Paper machine          MT/MT     2.11      2.07
         6     Reduction in specific power consumption in towel manufactring      KWH/MT     2.69      2.41
         7     Reduction in specific Steam consumption in towel manufactring       MT/MT     7.08       6.2

                To increase the usage of Hot water consumtion( from 850 Kl/day
               to 1000 Kl/day) and reduction in soft water consumption(102lt/kg
        8                  to 95 lt/kg) in Dye House by 31st July,2013            KL/day     850      1000
                To reduce the power consumption in WFL from 293 Kw-h/MT to
        9                       264 Kw-h/MT by Septermber-13                      KWH/MT     293       264
                To reduce the soft water consumption(From 102lt/kg to 95 lt/kg)
        10                       in Dye House by 31st July,2013                   LTR/kg     102       95
Initiatives Linked to energy conservation projects
                                              ENERGY CONSERVATION PLANNER 2013-2014
                                                                                               Approx.Investment         Estimated Savings*
S no                            Project Title                            Implementation Area       ( in Lacs)        UOM          Saving Value
       Reduction in Power consumption of Pm-1 drives by changing
                                                                                PM I                 225           KW / year         336384
 1     the present open gear system with Silent drive system

       Steam savings from Blow heat Recovery System, converting
                                                                                PULP                 320           MT / year           100
       vent system from batch digesters to heat water.
 2
       Reduction in steam Consumption by commissioning of closed
                                                                                PM I                 100           MT / year          8760
 3     hood with heat recovery system
       Reduction in steam Consumption by modification of PM-1
                                                                                PM I                 125           MT / year          9000
 4     steam & condensate system
                                                                                                                   KW / year         566940
       Rope less tail treading system to reduce tail treading time
 5                                                                              PM-2                  395          MT / year          2244

 6     Replacement of poor MC pumps (3) with efficient MC pumps                 WFL                   180          KW / year         378432

 7     Blow Heat Recovery project                                               WFL                   334          MT / year          23800

 8     MC PUMPS 9nos (VFD to be provide )                                       SFL                   40           KW / year         578160
       Installation of the additional finisher effect in Evap-2 for
                                                                                                                   MT / year          3432
       increasing the production
9                                                                              Rec-2                  500          KW / year         262500
10     Modification & up gradation of the RB-2                                 Rec-2                  100          MT / year          1890
       Improving the firing liquor concentration ( mix feed from evap-
       1&2) , furnace stability & improving the asset condition ( Like
11     ESP internal & casing, Air & FG ducting, SBs)                           Rec-1                  70           MT / year          23800


12     Installation of VFD on FD Fan of Boiler 2/3                           Energy 2/3               40           KW/year           326400
Initiatives Linked to energy conservation projects
                    Energy Conservation planner (2013-2014)
                                                        Investment              Estimated Savings*
 S no                 Project Title
                                                     (Tentative in Lacs)    UOM          Saving Value
           Replacement of Electrical heater by
  1                                                          3             KW / year        350000
                      Steam Radiator
         Installation of main header of size 6" in
  2     place of 4" to improve the water flow in             6             KW / year         72000
        process house with lower pump running
           Installation of new ss line of 10" for
  3      Effluent transfer from shortest route to            14            KW / year         70000
               reduce power consumption
        Replacement/Modification of Sot water
  4       line for Dye house for reduction in               1.5            KW / year         73000
          energy of Pumping at pump house.

        Installation of VFD 2 nos. for Blowers on
  5                                                         1.5            KW / year         87600
                  Stenter machine no 2.


  6     Atomization of soft water transfer system            2             KW / year         36500


           Introduction of LED technology for
                        lighting
  7                                                         1.53           KW / year         18250



                          Total                              30             49.5145         707350
Summary of initiatives


No. of initiatives – 60
Total investment involved- 3.53 crores
Estimated savings- 7.32 crores
Payback Period- 6months
Management's perspective
ENERGY MANAGEMENT POLICY
Improvement
             In
    Grey Folding Process
             by
    Value Stream Mapping
           through
    Low Cost Automation
            under
TPM pillar KK Kobetsu Kaizen




                               11

Case Study_Trident Group

  • 1.
  • 2.
    Trident – Geographies Punjab, India – Dhaula Campus 600 Acres Home Textiles, Energy and Paper Units Takshashila (Center of Excellence) Punjab, India – Sanghera Campus 350 Acres Yarn Units, Ananda (Leadership Workshop Center) Madhya Pradesh, India – Budhni Campus 800 Acres Yarn and Proposed Home Textiles Units Corporate Office – Ludhiana, Punjab (India) Sales Offices in NY (US), Delhi and Mumbai (India) 2
  • 3.
    Diversification through Integration Power & Steam Power Power Steam & Sulphuric Acid TRIDENT YARN ENERGY TRIDENT PAPER 3.94 Lakhs Spindles/ 50 MW per day 475 MTs per day 275 MTs per day Power & Steam Yarn Sulphuric Power Acid Terry Fabric Sulphuric Acid BATHROBES TOWEL TRIDENT CHEM 275 MTs per day 3
  • 4.
    ENERGY CONSUMPTION DETAILS CONSUMPTION UNIT OF S.NO. ENERGY AMOUNT MEASUREMENT 1 ELECTRICITY 125,297,782 KWH 2 STEAM 6500 MT/DAY 3 GROUND WATER 3650000 M3/YEAR 4 RECYCLED WATER 1095000 M3/YEAR 5 CO2 EMISSION 199429 TON CO2 EQ
  • 5.
    Projects for FY2013-2014 S.No. Project Name UOM Baseline Target 1 Reduction in specific power consumption in pulp area KWH/MT 317 264 2 Reduction in specific steam consumption in pulp area MT/MT 2.68 2.41 3 To improve the condensate return from towel and paper % 66 74 4 Reduction in specific power consumption in Paper machine KWH/MT 344 335 5 Reduction in specific steam consumption in Paper machine MT/MT 2.11 2.07 6 Reduction in specific power consumption in towel manufactring KWH/MT 2.69 2.41 7 Reduction in specific Steam consumption in towel manufactring MT/MT 7.08 6.2 To increase the usage of Hot water consumtion( from 850 Kl/day to 1000 Kl/day) and reduction in soft water consumption(102lt/kg 8 to 95 lt/kg) in Dye House by 31st July,2013 KL/day 850 1000 To reduce the power consumption in WFL from 293 Kw-h/MT to 9 264 Kw-h/MT by Septermber-13 KWH/MT 293 264 To reduce the soft water consumption(From 102lt/kg to 95 lt/kg) 10 in Dye House by 31st July,2013 LTR/kg 102 95
  • 6.
    Initiatives Linked toenergy conservation projects ENERGY CONSERVATION PLANNER 2013-2014 Approx.Investment Estimated Savings* S no Project Title Implementation Area ( in Lacs) UOM Saving Value Reduction in Power consumption of Pm-1 drives by changing PM I 225 KW / year 336384 1 the present open gear system with Silent drive system Steam savings from Blow heat Recovery System, converting PULP 320 MT / year 100 vent system from batch digesters to heat water. 2 Reduction in steam Consumption by commissioning of closed PM I 100 MT / year 8760 3 hood with heat recovery system Reduction in steam Consumption by modification of PM-1 PM I 125 MT / year 9000 4 steam & condensate system KW / year 566940 Rope less tail treading system to reduce tail treading time 5 PM-2 395 MT / year 2244 6 Replacement of poor MC pumps (3) with efficient MC pumps WFL 180 KW / year 378432 7 Blow Heat Recovery project WFL 334 MT / year 23800 8 MC PUMPS 9nos (VFD to be provide ) SFL 40 KW / year 578160 Installation of the additional finisher effect in Evap-2 for MT / year 3432 increasing the production 9 Rec-2 500 KW / year 262500 10 Modification & up gradation of the RB-2 Rec-2 100 MT / year 1890 Improving the firing liquor concentration ( mix feed from evap- 1&2) , furnace stability & improving the asset condition ( Like 11 ESP internal & casing, Air & FG ducting, SBs) Rec-1 70 MT / year 23800 12 Installation of VFD on FD Fan of Boiler 2/3 Energy 2/3 40 KW/year 326400
  • 7.
    Initiatives Linked toenergy conservation projects Energy Conservation planner (2013-2014) Investment Estimated Savings* S no Project Title (Tentative in Lacs) UOM Saving Value Replacement of Electrical heater by 1 3 KW / year 350000 Steam Radiator Installation of main header of size 6" in 2 place of 4" to improve the water flow in 6 KW / year 72000 process house with lower pump running Installation of new ss line of 10" for 3 Effluent transfer from shortest route to 14 KW / year 70000 reduce power consumption Replacement/Modification of Sot water 4 line for Dye house for reduction in 1.5 KW / year 73000 energy of Pumping at pump house. Installation of VFD 2 nos. for Blowers on 5 1.5 KW / year 87600 Stenter machine no 2. 6 Atomization of soft water transfer system 2 KW / year 36500 Introduction of LED technology for lighting 7 1.53 KW / year 18250 Total 30 49.5145 707350
  • 8.
    Summary of initiatives No.of initiatives – 60 Total investment involved- 3.53 crores Estimated savings- 7.32 crores Payback Period- 6months
  • 9.
  • 10.
  • 11.
    Improvement In Grey Folding Process by Value Stream Mapping through Low Cost Automation under TPM pillar KK Kobetsu Kaizen 11