Extensive Presentation with 14 Case Studies from High Voltage Assets Preventative Maintenance by Non-intrusive testing using Partial Discharge detection and monitoring equipment. This Presentation contains: Author's Key Facts, Integrated Steelworks Plants brief overview of processes and Biggest Private HV Network in the UK Single Line Diagram - to highlight importance of HV Assets importance to the whole site uninterrupted operations, 14 case studies showing various High Voltage Switchgear and Transformers Partial Discharge issues detected, located and eliminated by prompt action.
Partial discharge monitoring of High Voltage Assets - TATA Steel Scunthorpe
1. EA Technology Partial Discharge Forum 26 03 2015
Partial Discharge monitoring of HV assets
- experience from Tata Steel site, Scunthorpe.
Highlighting defects with specific switchgear which led to Partial Discharge, and the methods
implemented to manage these assets.
Mikolaj Kukawski MIET
Customer Networks Manager
ESM Power
2. Content of presentation
• My background
• TATA Steel HV Distribution Network
• Integrated Steelworks Processes
• Partial Discharge Case Studies (14)
• Special thanks and questions
3. My background
Education:
• 2001-2006 - University of Lublin, Poland
- Master’s degree in Electrical Engineering – Power Systems
Work experience:
• 2006-2007 - Elektromontaz Lublin, Poland
- Design Engineer for MV Switchgear Manufacturer – 1 year
• 2007-2008 - Corus Power & Distribution (P&D), Scunthorpe, UK
- HV Electrician Team Member – 18 months
4. My background
Work experience:
• 2008-2014 - Corus / TATA Steel P&D, Scunthorpe, UK
- Distribution Engineer - 6 years
• 2014 Dec - currently - ESM Power, Scunthorpe, UK
- Customer Networks Manager
42. Case Study 1 - Central Power Station 33 kV Substation
Affected Asset details:
1. Equipment Circuit VT
2. Make Reyrolle
3. Model L800T
4. Operating voltage 33kV
5. Number of panels 13 (Section 3 only 2 circuits)
6. Age 40 years
49. Case Study 1 - Central Power Station 33 kV Substation
Investigation details:
1. Partial discharge initial detection method - CPS power controller detected red TEV
using hand held UltraTEV detector during daily substation checks – informed duty
engineer
2. Follow up investigation method – Distribution Engineer and Team Leader joint
investigation using UltraTEV +. Switchboard tested Left to Right, Front to Rear and
Top to Bottom. Conclusion: On the circuit: 33/11kV 12/24MVA Transformer No.3 (T3)
the higher the measurement was taken the higher the TEV reading was (up to 50dB).
Decided to test Circuit VT located on the top of the switchgear. Confirmed that the
TEV reading was even higher (60dB).
3. Action taken - decided to isolate T3 circuit
57. Case Study 1 - Central Power Station 33 kV Substation
Outage requirement to enable investigation and repair
1. Equipment Section 3 bus bars at CPS 33kV, CPS 33/11kV 12/24MVA
Transformer No.3 circuit, CPS to HPM 33kV Interconnector
2. Timescale 2 hours on the T3 circuit, 15 minutes HPM stopped rolling to
enable T3 33kV OCB re-closure without its circuit VT.
58. Case Study 1 - Central Power Station 33 kV Substation
Actions taken to rectify the fault
1. Resources Investigation TATA, Siemens for VT repair
2. Discharge elimination Circuit VT withdrawn,
3. Repair method Cracked VT bushing to be replaced
4. Estimated cost of repair circa £ 10k
Has PD activity stopped? YES – TEV level went back to green
Possible cause of partial discharge VT Bushing damaged during installation
Loss estimation in worst case scenario:
Circa £ 200k for 2 33kV switchgear panels replacement and potentially HPM production loss and
internal generation limited due to 1 of 3 33/11kV transformers outage.
59. Case Study 2 - Central Power Station 3.3 kV
Affected Asset details:
1. Equipment Single core 3.3kV unarmoured cable
2. Make GEC
3. Model BTVP17 and HMC
4. Operating voltage 3.3kV
5. Number of panels 15
6. Age 40 years
65. Case Study 2 - Central Power Station 3.3 kV
Investigation details:
1. Partial discharge initial detection method - CPS power controller detected red TEV on
Incomer from 5MVA No.1 Transformer using hand held UltraTEV detector during daily
substation checks – informed duty engineer
2. Follow up investigation method – Distribution Engineer investigated the switchboard using
UltraTEV +. Switchboard tested Left to Right, Front to Rear and Top to Bottom. Conclusion:
On the Incomer No.1 circuit the lower the measurement was taken the higher the TEV
reading was (up to 44dB). Decided to Inspect cable box. No evidence of Partial Discharge
found. Tested switchboard Using Partial Discharge Monitor. Tested switchboard again using
UltraTEV + and realised that that the TEV reading was even higher on the bottom of cable
box support channel – near the floor (60dB). Question asked: What is underneath the
substation? It turned out to be mezzanine floor with cables installed on metal trays system.
Found one core stuck against metal support construction channel with signs of partial
discharge.
67. Case Study 2 - Central Power Station 3.3 kV
Investigation details:
3. Action taken – Circuit isolated, tested IR of the cable – 4 Mega Ohms - asked
experienced jointer for advice – suggested using triple layer of HV heat shrink
tape around damaged area of the cable. Cable repaired. Circuit reenergised. TEV
levels dropped down to 30dB at the repair point and down to 27 dB above the
repair point, investigated further the cable route – found cables tightened with
twisted steel wire armouring to form two trefoil formations (instead of using
proper trefoil cleats). Steel wire armouring is cutting through PVC insulation of
unarmoured cables on the majority of the cable routes. Decided to replace all
3.3kV cables for both No.1 and No.2 5MVA Transformers Incomers.
77. Case Study 2 - Central Power Station 3.3 kV
Outage requirement to enable investigation and repair
1. Equipment No.1 5MVA 11/3.3kV Transformer at CPS 3.3kV,
2. Timescale 6 hours for the cable box inspection, 4 hours for cable repair
78. Case Study 2 - Central Power Station 3.3 kV
Actions taken to rectify the fault
1. Resources Investigation TATA, SPEC for cable repair
2. Discharge elimination Cable replacement,
3. Repair method New cables installation with correct trefoil cleats
4. Estimated cost of repair circa £ 20k
Has PD activity stopped? NO – however TEV level reduced to amber level on the
switchboard
Possible cause of partial discharge Cable damaged due to incorrect installation method
Loss estimation in worst case scenario:
Potentially loss of internal generation since 3.3kV switchboard feeds auxiliary equipment essential for
steam raising processes. Possible knock on effect on process steam system for the whole site.
79. Case Study 3 - Blast Furnaces 11 kV
Affected Asset details:
1. Equipment Vacuum Circuit Breakers (VCB)
2. Make GEC
3. Model VMX
4. Operating voltage 11kV
5. Number of panels 19 (5 VCB’s affected)
6. Age 26 years
88. Case Study 3 - Blast Furnaces 11 kV
Investigation details:
1. Partial discharge initial detection method – TATA Steel Power and Distribution
craftsmen detected red TEV using hand held UltraTEV detector during weekly
substation checks – informed duty engineer
2. Follow up investigation method – Distribution Engineer investigated switchboard
using UltraTEV +. Switchboard tested Left to Right, Front to Rear and Top to Bottom.
Conclusion: On the circuit: 33/11kV 12/24MVA Transformer Incomer No.1 the
highest TEV level measured was at the front of VCB (up to 40dB). In conjunction with
BF Engineers decided to take the suspected VCB out of service.
3. Action taken – Incomer No.1 VCB isolated and retested the switchboard with
UltraTEV + - TEV level back to green
89. Incomer No.1 GEC VMX
11kV VCB L2 (yellow phase)
front isolating contact
front – busbar,
rear - circuit
91. New VMX unit for Incomer No.1 - showing L2 (yellow phase) front isolating contact
92. Case Study 3 - Blast Furnaces 11 kV
Outage requirement to enable investigation and repair
1. Equipment Incomer No.1 from 33/11kV 12/24MVA Transformer circuit
2. Timescale 2 hours to replace VCB with the new or refurbished unit from
Schneider
93. Case Study 3 - Blast Furnaces 11 kV
Actions taken to rectify the fault
1. Resources Investigation TATA, new or refurbished VMX unit – Schneider
2. Discharge elimination VMX VCB replacement,
3. Repair method VMX body moulding replaced and ball bearing added to the
drive shaft
Estimated cost of repair VMX refurbishment circa £ 5k, new VMX unit circa £ 14k
Has PD activity stopped? Yes
Possible cause of partial discharge – partial discharge possibly due to continuous charging and
discharging of unearthed metal drive shaft which goes through the middle of VMX body
moulding.
Loss estimation in worst case scenario:
Potentially loss of production on crucial iron making plant since 11kV switchboard feeds
charging side of all four blast furnaces essential for iron making processes. Possible site-wide
knock on effect including steelmaking and mills.
94. Other VMX circuit breakers affected by partial discharge – bus section
95. Other VMX circuit breakers affected by partial discharge – bus section
98. Other VMX circuit
breakers affected by
partial discharge –
Substation Auxiliary
2MVA Transformer
No.2 VCB
99. Other VMX circuit breakers affected by partial discharge – incomer No.2
100. Other VMX circuit breakers
affected by partial discharge
– incomer No.2
101. Case Study 4 - Bloom Mill 11 kV
Affected Asset details:
1. Equipment Busbar Voltage Transformer (VT)
2. Make GEC
3. Model BVP17
4. Operating voltage 11kV
5. Number of panels 16 (Section 2 Busbar VT affected)
6. Age 45 years
102.
103.
104. Bloom Mill 11kV
Substation GEC BVP17
11kV Switchgear
(single busbar system)
- showing Section 2 of
the switchboard
isolated and Section 2
busbars earthed
112. Case Study 4 - Bloom Mill 11 kV
Investigation details:
1. Partial discharge initial detection method – BBM engineer informed duty engineer
about audible discharge in Section 2 Switchroom of Bloom Mill 11kV Substation.
2. Follow up investigation method – Distribution Engineer arrived on site and located
the discharge near Section 2 Busbar VT.
3. Action taken - decided to isolate suspected Section 2 Busbar VT
113. Case Study 5 - BOS Waste Gas Recovery 11 kV
Affected Asset details:
1. Equipment Vacuum Circuit Breakers (VCB)
2. Make GEC
3. Model VMX
4. Operating voltage 11kV
5. Number of panels 9 (5 VCB’s affected)
6. Age 26 years
114. BOS Waste Gas Recovery 11 kV
Substation - bus section GEC
VMX VCB L2 (yellow phase)
front isolating contact
115. Bus section GEC VMX 11kV VCB L2 (yellow phase) front isolating contact
122. Case Study 6 - Ore Blending Plant Main 11 kV
Affected Asset details:
1. Equipment Current Transformers (CT’s)
2. Make GEC
3. Model BVP17
4. Operating voltage 11kV
5. Number of panels 6 (1 OCB panel circuit chamber affected)
6. Age 27 years
126. Ore Blending Plant Main 11 kV Substation Incomer No.1 CT’s
affected by partial discharge
127. Case Study 6 - Ore Blending Plant Main 11 kV
Actions taken to rectify the fault
1. Resources Investigation TATA, CT’s & bushings repairs – Schneider
2. Discharge elimination Incomer No.1 circuit isolated
3. Repair method CT’s removed, repaired and fitted by OEM
Estimated cost of repair CT’s repairs: labour circa £ 8k, materials circa £ 2.5k
Has PD activity stopped? Yes
Possible cause of partial discharge – partial discharge possibly due to broken CT’s earth
clamps. It is likely that high humidity within substation was a contributing factor.
Loss estimation in worst case scenario:
Potential loss of production on Ore Blending Plant – crucial for Sinter making process.
Possible site-wide knock on effect including ironmaking, steelmaking and mills.
128. Case Study 7 - Blast Furnaces No. 2 6.6 kV
Affected Asset details:
1. Equipment Cable terminations
2. Make Brush
3. Model VMVD
4. Operating voltage 6.6kV
5. Number of panels 23 (2 VCB panels cable terminations affected)
6. Age 25 years
134. Case Study 7 - Blast Furnaces No. 2 6.6 kV
Actions taken to rectify the fault
1. Resources Investigation TATA, cable terminations repairs – SPEC
2. Discharge elimination 2 circuits isolated
3. Repair method cable terminations removed, cables cut, jointed new
pieces of cable in the basement and terminated with
Raychem heat shrink termination kits
Estimated cost of repair new cables, joints and terminations circa £ 7k
Has PD activity stopped? Yes
Possible cause of partial discharge – partial discharge possibly due to substandard cable
terminations.
Loss estimation in worst case scenario:
Potential loss of production on ironmaking. Possible site-wide knock on effect including
steelmaking and mills.
141. Case Study 8 - BOS Waste Gas Recovery 11 kV Busbar Outage
Affected Asset details:
1. Equipment Air insulated busbars
2. Make GEC
3. Model VMX
4. Operating voltage 11kV
5. Number of panels 9
6. Age 26 years
155. Case Study 9 - Heavy Section Mill to Scunthorpe Rod Mill 33 kV
Interconnector Reactor Terminations
Affected Asset details:
1. Equipment 33kV cable terminations inside air cable box of reactor
2. Make Yorkshire Electric Transformer Company Ltd.
3. Model 21 MVA to British Standard Specification 171/1956
4. Operating voltage 33kV
5. Number of panels N/A
6. Age 41 years (refurbished by SPEC in 2006)
156.
157.
158. Blast Furnace to Scunthorpe Rod Mill 33 kV Interconnector Reactor
159. Blast Furnace to Scunthorpe Rod Mill 33 kV Interconnector Reactor
160. Heavy Section Mill to Scunthorpe Rod Mill 33 kV Interconnector Reactor Terminations
161. Heavy Section Mill to Scunthorpe Rod Mill
33 kV Interconnector Reactor Terminations
162. Heavy Section Mill to
Scunthorpe Rod Mill
33 kV Interconnector
Reactor Terminations
163. Heavy Section Mill to Scunthorpe
Rod Mill 33 kV Interconnector
Reactor Terminations
164. Heavy Section Mill to
Scunthorpe Rod Mill
33 kV Interconnector
Reactor Terminations
165. Heavy Section Mill to
Scunthorpe Rod Mill 33 kV
Interconnector Reactor
Terminations
166. Case Study 9 - Heavy Section Mill to Scunthorpe Rod Mill 33 kV
Interconnector Reactor Terminations
Actions taken to rectify the fault
1. Resources Investigation TATA, cable terminations repairs – SPEC
2. Discharge elimination 33kV Interconnector circuit isolated
3. Repair method cables re-terminated
Estimated cost of repair new terminations circa £ 7k
Has PD activity stopped? Yes
Possible cause of partial discharge – partial discharge possibly due to substandard cable
terminations (i.e. clearances between termination sheds not sufficient)
Loss estimation in worst case scenario:
Security of site power supplies compromised – SRM down to 3 out of 4 Interconnectors.
167. Blast Furnace to Rod Mill 33 kV Interconnector Reactor Cable Terminations Failure
168. Blast Furnace to Rod Mill 33 kV Interconnector Reactor Cable Terminations Failure
169. Blast Furnace to Rod Mill 33 kV Interconnector Reactor Cable Terminations Partial Discharge
170. Blast Furnace to Rod Mill 33 kV Interconnector Reactor Cable Terminations Partial Discharge
171. Case Study 10 - Broughton to Seraphim 33 kV Interconnector VT and
Case Study 11 - Seraphim to BF Interconnector VT
Affected Asset details:
1. Equipment Circuit VT
2. Make Reyrolle
3. Model L42T
4. Operating voltage 33kV
5. Number of panels 23
6. Age circa 40 years
174. Reyrolle L42T 33kV Switchgear
Circuit VT removed from traversing carriage
onto mono rail in readiness to be removed from
site and tested at Siemens Hepburn Works
177. UltraTEV Alarm System
with SCADA interface
(remote I/O connection)
Installed at Grid Supply
Point Broughton 33kV
Substation – 1 system
per Section
180. Case Study 12 - CONCAST Water Treatment Plant 11 kV Busbars
Affected Asset details:
1. Equipment Busbars
2. Make GEC
3. Model BVP17
4. Operating voltage 11kV
5. Number of panels 11
6. Age circa 40 years
188. Case Study 12 - CONCAST Water Treatment Plant 11 kV Busbars
Actions taken to rectify the fault
1. Resources Investigation & busbars removal/installation – TATA,
busbars repairs and new busbar spacing materials –
Schneider
2. Discharge elimination 11kV busbars Sections 1&2, 2nd outage sections 2&3
isolated.
3. Repair method busbars re-sleeved and new busbar spacing fitted
Estimated cost of repair total cost of all repairs circa £ 25k
Has PD activity stopped? Yes
Possible cause of partial discharge – PD due to poor substation heating in winter time
which led to high humidity levels (90%) and water condensation on substation ceiling.
Loss estimation in worst case scenario:
Slab caster loss of production with possible knock on effect on Plate Mill.
189. Case Study 13 - Heavy Plate Mill Roughing Mill Transformer Cast
Resin Transformer 33 kV
Affected Asset details:
1. Equipment Cast Resin Transformer
2. Make ABB
3. Model 4.1MVA
4. Operating voltage 33/1kV
5. Number of panels N/A
6. Age 7 years
192. Heavy Plate Mill
Roughing Mill
Main Drive Cast
Resin Transformer
33/1 kV 4.1MVA –
loose eye bolt nut
193. Heavy Plate Mill
Roughing Mill
Main Drive Cast
Resin Transformer
33/1 kV 4.1MVA –
substandard LV
cable connection
194. Heavy Plate Mill Roughing Mill Main Drive
Cast Resin Transformer 33/1 kV 4.1MVA –
PD found on 33kV CT’s connections
195. Case Study 14 - Bloom Caster 11 kV
Affected Asset details:
1. Equipment Vacuum Circuit Breakers (VCB)
2. Make GEC
3. Model VMX
4. Operating voltage 11kV
5. Number of panels 11 (2 VCB’s affected)
6. Age 19 years
203. This presentation was made thanks to 8 years of experience in
maintaining on one of the largest private HV network – TATA Steel in
Scunthorpe, North Lincolnshire, UK
Presentation prepared with permission of:
John Simpson – TATA Steel Scunthorpe Electrical Infrastructure, SRCS
and DSEAR Engineer, HV Engineer in Charge for Scunthorpe &
Immingham Works
Special thanks to Paul Wilson for Scunthorpe Steelworks photographs