SlideShare a Scribd company logo
Success Bulletin
Name (s) Finish DateStart Date
‘Before’ picture (sketch/photo):
‘After’ picture (sketch/photo):
Problem Description: Solution Description:
Loss (Reasons for Improvement): Benefits (Results Achieved):
S Q P C D M Circle relevant
Ref No
‘Continuously Challenge the Status Quo’
Dept./ Function:
LES FRITH, ATTILLA SZABO,NEIL
HARDINGHAM,ANDY GILLARD
SUTR A3 25/05/2015 30/01/2016
PICKLES LINE 5
MULTIPLE CHANGEOVERS TIME CONSUMING VARYING RAMP UP TIMES AND FREQUENT TUNING TO
GET TO EXPECTED RUN RATES EXCESSIVE WASTE DURING FINE TUNING AND RAMP UP'S. 729 GBP
PER WEEK OVERTIME AVOIDANCE (1 HR PER WEEK = 243 GBP PER HR O/T avoidance based on a ten
man crew having to work 3 hours O/T on line 5 @ 1.5 HRs per hour off shift.) Total annual avoidance of £37,179.
NUMEROUS RUNS ON LINE 5 WITH MULTIPLE CHANGEOVERS
MORALE IS LOW AS CHANGEOVERS ARE TIME CONSUMING
WITH VARYING RAMP UP TIMES AND FREQUENT TUNING
REQUIRED TO GET TO EXPECTED RUN TIMES/OUTPUTS WITH
EXCESSIVE WASTE DURING FINE TUNING AND RAMP UP'S.
SET UP TIME AVERAGES 9 HOURS PER WEEK.
STANDARDISED CHANGEOVERS FOR LINE 5 PRODUCTS WITH
EASY, QUICK AND SAFE PROCESSES WITH LITTLE OR NO
TUNING REQUIRED ALLOWING RAMP UP TIME AND WASTE TO
BE REDUCED, EMBRACING SMALLER BATCH RUNS WITH NEW
STANDARDISED PROCESS. REDUCE SET UP TIME FROM 9 -6
HOURS PER WEEK.
STANDARDISED CHANGEOVERS FOR LINE 5 PRODUCTS,
LITTLE OR NO TUNING REQUIRED C/O TIME REDUCED 90
MINS TO 70 MINS & FROM 60 MINS to 45 MINS. EMBRACING
SMALLER BATCH RUNS WITH NEW STANDARDISED
PROCESS. REDUCED SET UP TIME FROM AVERAGE 9 HOURS
PER WEEK TO SIX HOURS PER WEEK, A REDUCTION OF 33%
= 3 HOURS PER WEEK SOFT SAVING OF £37,179 p.a.
High Variation C/O’s
Reduced Variation C/O
Change over times varied and non-standardised Consistent & Standardised Change over times visible

More Related Content

Similar to CI Project Success Bulletin - SUTR LINE 5 2015

Combined Pat Presentation Oct - Copy
Combined Pat Presentation  Oct  - CopyCombined Pat Presentation  Oct  - Copy
Combined Pat Presentation Oct - Copy
John Osborne
 
PARESH KUMAR DASH-RESUME-BOILER (1)
PARESH KUMAR   DASH-RESUME-BOILER (1)PARESH KUMAR   DASH-RESUME-BOILER (1)
PARESH KUMAR DASH-RESUME-BOILER (1)
PARESH DASH
 
CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...
CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...
CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...
Arun Chowdhury
 
Ground Support Equipment Efficiency & Innovation Project
Ground Support Equipment Efficiency & Innovation ProjectGround Support Equipment Efficiency & Innovation Project
Ground Support Equipment Efficiency & Innovation Project
Steve Nails
 
Implémentation Méthode Single Minute Exchange of Dies(SMED)
Implémentation Méthode Single Minute Exchange of Dies(SMED)Implémentation Méthode Single Minute Exchange of Dies(SMED)
Implémentation Méthode Single Minute Exchange of Dies(SMED)
MohammedLahssaini1
 

Similar to CI Project Success Bulletin - SUTR LINE 5 2015 (20)

Development of fixture_to_reduce_the_cycle_time_of_c_8_griding_machine
Development of fixture_to_reduce_the_cycle_time_of_c_8_griding_machineDevelopment of fixture_to_reduce_the_cycle_time_of_c_8_griding_machine
Development of fixture_to_reduce_the_cycle_time_of_c_8_griding_machine
 
Production & Operarions Management Compre Review
Production & Operarions Management Compre ReviewProduction & Operarions Management Compre Review
Production & Operarions Management Compre Review
 
How to unlock productivity savings in mining operations part 2. "Show me the ...
How to unlock productivity savings in mining operations part 2. "Show me the ...How to unlock productivity savings in mining operations part 2. "Show me the ...
How to unlock productivity savings in mining operations part 2. "Show me the ...
 
session 1
session 1session 1
session 1
 
Julius job details report
Julius job details report Julius job details report
Julius job details report
 
BueScape & MIRATECH EPA RICE NESHAP the Meter is Running Webinar 4-08-14
BueScape & MIRATECH EPA RICE NESHAP the Meter is Running Webinar 4-08-14BueScape & MIRATECH EPA RICE NESHAP the Meter is Running Webinar 4-08-14
BueScape & MIRATECH EPA RICE NESHAP the Meter is Running Webinar 4-08-14
 
Cost reduction in sugar mill a case study
Cost reduction in sugar mill  a case studyCost reduction in sugar mill  a case study
Cost reduction in sugar mill a case study
 
PLC problem troubleshooting
PLC problem troubleshooting PLC problem troubleshooting
PLC problem troubleshooting
 
Combined Pat Presentation Oct - Copy
Combined Pat Presentation  Oct  - CopyCombined Pat Presentation  Oct  - Copy
Combined Pat Presentation Oct - Copy
 
PARESH KUMAR DASH-RESUME-BOILER (1)
PARESH KUMAR   DASH-RESUME-BOILER (1)PARESH KUMAR   DASH-RESUME-BOILER (1)
PARESH KUMAR DASH-RESUME-BOILER (1)
 
Proposal Wide Blower No.1 & 2 with inverter
Proposal Wide Blower No.1 & 2  with inverterProposal Wide Blower No.1 & 2  with inverter
Proposal Wide Blower No.1 & 2 with inverter
 
OEE
OEEOEE
OEE
 
2014 PV Performance Modeling Workshop: Optimization strategies with Pvsyst fo...
2014 PV Performance Modeling Workshop: Optimization strategies with Pvsyst fo...2014 PV Performance Modeling Workshop: Optimization strategies with Pvsyst fo...
2014 PV Performance Modeling Workshop: Optimization strategies with Pvsyst fo...
 
CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...
CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...
CV - 19 yrs exp at HOT ROLLING MILL operation with DME & MBA in Operation Man...
 
Mechanical maintenance-of-cement-rotary-kiln
Mechanical maintenance-of-cement-rotary-kilnMechanical maintenance-of-cement-rotary-kiln
Mechanical maintenance-of-cement-rotary-kiln
 
Well completion workshop april-2018
Well completion workshop april-2018Well completion workshop april-2018
Well completion workshop april-2018
 
Ground Support Equipment Efficiency & Innovation Project
Ground Support Equipment Efficiency & Innovation ProjectGround Support Equipment Efficiency & Innovation Project
Ground Support Equipment Efficiency & Innovation Project
 
JULIAN KALAC -EXAMPLES OF LEAN SIX SIGMA BLACK BELT PROJECTS
JULIAN KALAC -EXAMPLES OF LEAN SIX SIGMA BLACK BELT PROJECTS JULIAN KALAC -EXAMPLES OF LEAN SIX SIGMA BLACK BELT PROJECTS
JULIAN KALAC -EXAMPLES OF LEAN SIX SIGMA BLACK BELT PROJECTS
 
Implémentation Méthode Single Minute Exchange of Dies(SMED)
Implémentation Méthode Single Minute Exchange of Dies(SMED)Implémentation Méthode Single Minute Exchange of Dies(SMED)
Implémentation Méthode Single Minute Exchange of Dies(SMED)
 
Design improvements and costing analysis
Design improvements and costing analysisDesign improvements and costing analysis
Design improvements and costing analysis
 

CI Project Success Bulletin - SUTR LINE 5 2015

  • 1. Success Bulletin Name (s) Finish DateStart Date ‘Before’ picture (sketch/photo): ‘After’ picture (sketch/photo): Problem Description: Solution Description: Loss (Reasons for Improvement): Benefits (Results Achieved): S Q P C D M Circle relevant Ref No ‘Continuously Challenge the Status Quo’ Dept./ Function: LES FRITH, ATTILLA SZABO,NEIL HARDINGHAM,ANDY GILLARD SUTR A3 25/05/2015 30/01/2016 PICKLES LINE 5 MULTIPLE CHANGEOVERS TIME CONSUMING VARYING RAMP UP TIMES AND FREQUENT TUNING TO GET TO EXPECTED RUN RATES EXCESSIVE WASTE DURING FINE TUNING AND RAMP UP'S. 729 GBP PER WEEK OVERTIME AVOIDANCE (1 HR PER WEEK = 243 GBP PER HR O/T avoidance based on a ten man crew having to work 3 hours O/T on line 5 @ 1.5 HRs per hour off shift.) Total annual avoidance of £37,179. NUMEROUS RUNS ON LINE 5 WITH MULTIPLE CHANGEOVERS MORALE IS LOW AS CHANGEOVERS ARE TIME CONSUMING WITH VARYING RAMP UP TIMES AND FREQUENT TUNING REQUIRED TO GET TO EXPECTED RUN TIMES/OUTPUTS WITH EXCESSIVE WASTE DURING FINE TUNING AND RAMP UP'S. SET UP TIME AVERAGES 9 HOURS PER WEEK. STANDARDISED CHANGEOVERS FOR LINE 5 PRODUCTS WITH EASY, QUICK AND SAFE PROCESSES WITH LITTLE OR NO TUNING REQUIRED ALLOWING RAMP UP TIME AND WASTE TO BE REDUCED, EMBRACING SMALLER BATCH RUNS WITH NEW STANDARDISED PROCESS. REDUCE SET UP TIME FROM 9 -6 HOURS PER WEEK. STANDARDISED CHANGEOVERS FOR LINE 5 PRODUCTS, LITTLE OR NO TUNING REQUIRED C/O TIME REDUCED 90 MINS TO 70 MINS & FROM 60 MINS to 45 MINS. EMBRACING SMALLER BATCH RUNS WITH NEW STANDARDISED PROCESS. REDUCED SET UP TIME FROM AVERAGE 9 HOURS PER WEEK TO SIX HOURS PER WEEK, A REDUCTION OF 33% = 3 HOURS PER WEEK SOFT SAVING OF £37,179 p.a. High Variation C/O’s Reduced Variation C/O Change over times varied and non-standardised Consistent & Standardised Change over times visible