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Copyright2013-2014
PROJECT SEMESTER REVIEW
Name: Zorawar Singh Nandwal
Roll No: 401257013
Organization: Munjal Showa, Manesar
Department: Rear Assy, I.E
Project Guide: Mr. Narinder Madan
Copyright2013-2014
Munjal Showa in very few years of its existence has become a national leader
in manufacturing of Suspensions for 2 & 4-Wheelers. Since its formation in
1987 with Showa group of Japan it has grown substantially and has achieved
success in both national and international markets. Today Munjal Showa
Limited is one of the largest suppliers of shock absorbers to major auto giants.
Copyright2013-2014
PROJECT TITLES
1. Improvements in Rear Assembly
2. Air Pollution Control in machine shop
3. Value Stream Mapping
Copyright2013-2014
ACTIVITY PLAN
S.N
O ACTIVITY JAN FEB MAR APR MAY JUN
1 IMPROVEMENTS IN REAR ASSEMBLY
2 AIR POLLUTION CONTROL IN MACHINE SHOP
3 VALUE STREAM MAPPING
Copyright2013-2014
Objectives
1. Productivity Improvement
2. Reduce man-material movement
3. Manpower Management
4. Observing Standard Operating Procedure (SOP)
5. Maintenance of newly installed features
6. Improving cleanliness in the new air tight enclosure
IMPROVEMENT IN REAR
ASSEMBLY
Copyright2013-2014
PRODCUTIVITY IMPROVEMENTS
 Calculated cycle time of all 6 lines.
 Compared cycle times of each line to set a standardized way of operating
the same equipment on different lines.
 Found out rod guide pressing of line-5 was taking longer time than others
 Located a fault in ECU of the equipment.
 Excess cycle time of piece bottom pressing in Line-3 i.e. 4.4 secs as
compared to 1.5-1.75 in other lines.
 Maintenance dept informed about the fault. ..MunjalShowa
AssemblyRear
AssyLayoutRe
ar
AssyLayoutLine
5.xlsx..MunjalShowaAss
emblyRearAssyCycl
eTimeRear
AssyLine5KSPGCy
cleTimeline5.xlsx
Copyright2013-2014
OBSERVING SOP
 In rod guide pressing the worker had to keep on pressing the buttons till
the time the process was not completed.
 Whereas in other machines the operator just presses the button once and
during the processing time he/she unloads the next piece from the bin.
 Maintenance dept was informed and necessary action was taken.
4.4
1.75
Cycle Time
OLD NEW
Copyright2013-2014
Reduce man-material movement
 Often wrong raw material is brought to the work station due to which time is
wasted.
 Naming done on raw material.
 Newly installed chute should have particular rack for the same type of raw material.
 This will lead to worker’s proper understanding.
Copyright2013-2014
In oil filling trolley movement was reduced by making the RM available
at a shorter distance. Also by creating side racks the need for a trolley at all
times was eliminated.
0
20
40
60
Initial Final
Initial
Final
54
14
S
T
E
P
S
Copyright2013-2014
MANPOWER MANAGEMENT
 Between Rod guide pressing and rolling the manpower is 3. 1st workers
operates the RGP m/c, 2nd worker places the end plate & checks the
moment and the 3rd worker operates the rolling m/c.
 The rod guide pressing operator can insert the end plate and can place in
the loading bin of rolling worker.
0
0.5
1
1.5
2
2.5
3
3.5
Existing New
M
A
N
P
O
W
E
R
Copyright2013-2014
Maintenance & Improvement of Newly
installed features
 The new chute installed which is used to slide down the final assembled
part outside the air-tight enclosure had started bending after 2-3 days of
use.
 A support was provided in between the chute so that it doesn’t bend and the
smooth flow continues.
 The rack installed in the air tight system which allows the trolley operator
to load the raw material without entering the air tight enclosure. Thus
saving man and material movement.
 Here there no particular rack for a particular raw material. Therefore a
proper description was provided on each rack.
Copyright2013-2014
Improving cleanliness level in the new
air tight enclosure
 In gas shock absorbers an air gun is used to clean the remains of oil on the
part. This led to accumulation of oil droplets on the wall and the floor.
 This also led to accumulation of oil on the conveyor which further would
effect the work piece.
 Therefore a bin was created. Now the operator will use the air gun while
pointing towards the bin
Copyright2013-2014
Improving cleanliness level in the new air
tight enclosure
Date 26/12 29/12 2/1 6/1 10/1 17/1 23/1 23/2 23/3 23/4 23/5
DFT Dirty Dirty Clean Clean Clean Clean Clean Clean Clean Clean Clean
Oil
Filling
Dirty Dirty Clean Clean Dirty Dirty Clean Clean Clean Clean Clean
Air Gun Very
Dirty
Very
Dirty
Very
Dirty
Dirty Dirty Clean Clean Dirty Clean Clean Clean
 In oil filling machine where the chances of contamination are the highest it
was ensured that the workplace will be cleaned at regular intervals by the
operator.
 Also in the Dampening Force Testing Machine due to the presence of heat
exchanger the water used to get collected on the equipment. Though it
happened very rarely but when it did it was ignored
Copyright2013-2014
Reducing Rust in DAMPER CASE pipe
 Rust inside the D/C pipe is a major problem which leads to contamination
of oil and thus effects the performance of the shocker.
 To reduce this damper case washing is done on a in-house manufactured
machine. This process is the first step of any line in Rear Assembly.
 A brush is used to clean the inside of the pipe.
 The brush used to clean is only suitable for 30,000 cycles.
Therefore it has to be changed every 3 days.
Copyright2013-2014
Air Pollution Control in machine shop
Objectives
1. To update data regarding number of exhaust fans working.
2. To control pollution in Welding Shop & Buffing shop.
Copyright2013-2014
ELECTRICAL EXHAUST FANS
Copyright2013-2014
NATURAL EXHAUST FANS
Copyright2013-2014
Air Pollution Control in machine shop
 Data regarding Electric exhaust and natural exhaust fans was updated and
reported to the industrial coordinator.
 Ducts were introduced at every work station.
 As the raw material consisted of oil and grease
It caused excess release of fumes during welding.
Therefore it was made mandatory for all operators to
First dip the RM in thinner(SOKLIN)
 Also ducts were introduced above WIP
collecting trolleys
Copyright2013-2014
The D/C parts that are sent by the vendors are full of oil and grease particles. When the
operator starts to weld these parts the pollution caused is high because the electrode now
has to penetrate through the oil layer as well.
Therefore the workers were instructed to dip the RM first inside thinner for 10-15
seconds and then take the lot to the work station.
Copyright2013-2014
Air Pollution Control in machine shop
 In buffing shop where bottom case is buffed, lot of dust is produced.
 The ducts installed are not effective.
 Some repairs were made to reduce dust inside
the shop.
Copyright2013-2014
Value Stream Mapping(AAHA)
Objective
 To eliminate the avoidable NVA and to minimize unavoidable NVA
 To understand Process Flow.
Copyright2013-2014
CAUSE & EFFECT
Copyright2013-2014
PROCESS FLOW
Damper Case
Welding Line
Loading/Unloading
Loading/Unloading
Store
Piston
Rod Line
Piston Rod
Cutting Piston Rod
Plating
U/S Washing
Assembly
Begins
Assembly
Ends
Despatch
Area
Copyright2013-2014
Copyright2013-2014
ELIMINIATING AVOIDABLE NVA &
MINIMIZING UNAVOIDABLE NVA
1.The standard stoppage time is 50 mins for 1 shift. Though the average break time
comes out to be more than 76 mins. There is a difference of 26 mins.
 Keeping this in mind targets were given to each line each hour. If the line in
consideration fails to achieve the target on regular basis, the HOD provides them
with training.
2. Paint shop is located at the farther end of the plant. Due to this any major/minor
breakdown takes time to be checked and corrected.
 Many times the hose air pipe gets damaged and it takes more than 15 minutes to
inform the maintenance dept and bring a new pipe for replacement. For this the
supervisors and the operators were trained by the TPM dept. to take quick action if
any such situation arises and the replacement pipes were present at the paint shop..
This would prevent line stoppage.
Copyright2013-2014
ELIMINIATING AVOIDABLE NVA &
MINIMIZING UNAVOIDABLE NVA
3. Due to the unavailability of trolley at the unloading station of the excise store the
worker first had to place the goods on the floor and then wait for the trolley to be
free. Then he loaded the goods on to the trolley.
 Therefore two trolleys were made available to the workers. This would reduce the
fatigue and increase productivity.
4.To reduce man material movement a new path was allocated for taking the piston
rods to the plating line.
 This lead to a decrease of 61% in man material movement.
Copyright2013-2014
REDUCING MAN MOVEMENT &
FATIGUE
Copyright2013-2014
PREVIOUS PATH FOLLOWED (PISTON ROD LINE-->>PISTON
ROD PLATING)
Copyright2013-2014
NEW PATH FOLLOWED (PISTON ROD LINE-->>PISTON ROD
PLATING)
Copyright2013-2014
REDUCTION IN MAN MATERIAL MOVEMENT
Copyright2013-2014
Thank You!

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  • 1. Copyright2013-2014 PROJECT SEMESTER REVIEW Name: Zorawar Singh Nandwal Roll No: 401257013 Organization: Munjal Showa, Manesar Department: Rear Assy, I.E Project Guide: Mr. Narinder Madan
  • 2. Copyright2013-2014 Munjal Showa in very few years of its existence has become a national leader in manufacturing of Suspensions for 2 & 4-Wheelers. Since its formation in 1987 with Showa group of Japan it has grown substantially and has achieved success in both national and international markets. Today Munjal Showa Limited is one of the largest suppliers of shock absorbers to major auto giants.
  • 3. Copyright2013-2014 PROJECT TITLES 1. Improvements in Rear Assembly 2. Air Pollution Control in machine shop 3. Value Stream Mapping
  • 4. Copyright2013-2014 ACTIVITY PLAN S.N O ACTIVITY JAN FEB MAR APR MAY JUN 1 IMPROVEMENTS IN REAR ASSEMBLY 2 AIR POLLUTION CONTROL IN MACHINE SHOP 3 VALUE STREAM MAPPING
  • 5. Copyright2013-2014 Objectives 1. Productivity Improvement 2. Reduce man-material movement 3. Manpower Management 4. Observing Standard Operating Procedure (SOP) 5. Maintenance of newly installed features 6. Improving cleanliness in the new air tight enclosure IMPROVEMENT IN REAR ASSEMBLY
  • 6. Copyright2013-2014 PRODCUTIVITY IMPROVEMENTS  Calculated cycle time of all 6 lines.  Compared cycle times of each line to set a standardized way of operating the same equipment on different lines.  Found out rod guide pressing of line-5 was taking longer time than others  Located a fault in ECU of the equipment.  Excess cycle time of piece bottom pressing in Line-3 i.e. 4.4 secs as compared to 1.5-1.75 in other lines.  Maintenance dept informed about the fault. ..MunjalShowa AssemblyRear AssyLayoutRe ar AssyLayoutLine 5.xlsx..MunjalShowaAss emblyRearAssyCycl eTimeRear AssyLine5KSPGCy cleTimeline5.xlsx
  • 7. Copyright2013-2014 OBSERVING SOP  In rod guide pressing the worker had to keep on pressing the buttons till the time the process was not completed.  Whereas in other machines the operator just presses the button once and during the processing time he/she unloads the next piece from the bin.  Maintenance dept was informed and necessary action was taken. 4.4 1.75 Cycle Time OLD NEW
  • 8. Copyright2013-2014 Reduce man-material movement  Often wrong raw material is brought to the work station due to which time is wasted.  Naming done on raw material.  Newly installed chute should have particular rack for the same type of raw material.  This will lead to worker’s proper understanding.
  • 9. Copyright2013-2014 In oil filling trolley movement was reduced by making the RM available at a shorter distance. Also by creating side racks the need for a trolley at all times was eliminated. 0 20 40 60 Initial Final Initial Final 54 14 S T E P S
  • 10. Copyright2013-2014 MANPOWER MANAGEMENT  Between Rod guide pressing and rolling the manpower is 3. 1st workers operates the RGP m/c, 2nd worker places the end plate & checks the moment and the 3rd worker operates the rolling m/c.  The rod guide pressing operator can insert the end plate and can place in the loading bin of rolling worker. 0 0.5 1 1.5 2 2.5 3 3.5 Existing New M A N P O W E R
  • 11. Copyright2013-2014 Maintenance & Improvement of Newly installed features  The new chute installed which is used to slide down the final assembled part outside the air-tight enclosure had started bending after 2-3 days of use.  A support was provided in between the chute so that it doesn’t bend and the smooth flow continues.  The rack installed in the air tight system which allows the trolley operator to load the raw material without entering the air tight enclosure. Thus saving man and material movement.  Here there no particular rack for a particular raw material. Therefore a proper description was provided on each rack.
  • 12. Copyright2013-2014 Improving cleanliness level in the new air tight enclosure  In gas shock absorbers an air gun is used to clean the remains of oil on the part. This led to accumulation of oil droplets on the wall and the floor.  This also led to accumulation of oil on the conveyor which further would effect the work piece.  Therefore a bin was created. Now the operator will use the air gun while pointing towards the bin
  • 13. Copyright2013-2014 Improving cleanliness level in the new air tight enclosure Date 26/12 29/12 2/1 6/1 10/1 17/1 23/1 23/2 23/3 23/4 23/5 DFT Dirty Dirty Clean Clean Clean Clean Clean Clean Clean Clean Clean Oil Filling Dirty Dirty Clean Clean Dirty Dirty Clean Clean Clean Clean Clean Air Gun Very Dirty Very Dirty Very Dirty Dirty Dirty Clean Clean Dirty Clean Clean Clean  In oil filling machine where the chances of contamination are the highest it was ensured that the workplace will be cleaned at regular intervals by the operator.  Also in the Dampening Force Testing Machine due to the presence of heat exchanger the water used to get collected on the equipment. Though it happened very rarely but when it did it was ignored
  • 14. Copyright2013-2014 Reducing Rust in DAMPER CASE pipe  Rust inside the D/C pipe is a major problem which leads to contamination of oil and thus effects the performance of the shocker.  To reduce this damper case washing is done on a in-house manufactured machine. This process is the first step of any line in Rear Assembly.  A brush is used to clean the inside of the pipe.  The brush used to clean is only suitable for 30,000 cycles. Therefore it has to be changed every 3 days.
  • 15. Copyright2013-2014 Air Pollution Control in machine shop Objectives 1. To update data regarding number of exhaust fans working. 2. To control pollution in Welding Shop & Buffing shop.
  • 18. Copyright2013-2014 Air Pollution Control in machine shop  Data regarding Electric exhaust and natural exhaust fans was updated and reported to the industrial coordinator.  Ducts were introduced at every work station.  As the raw material consisted of oil and grease It caused excess release of fumes during welding. Therefore it was made mandatory for all operators to First dip the RM in thinner(SOKLIN)  Also ducts were introduced above WIP collecting trolleys
  • 19. Copyright2013-2014 The D/C parts that are sent by the vendors are full of oil and grease particles. When the operator starts to weld these parts the pollution caused is high because the electrode now has to penetrate through the oil layer as well. Therefore the workers were instructed to dip the RM first inside thinner for 10-15 seconds and then take the lot to the work station.
  • 20. Copyright2013-2014 Air Pollution Control in machine shop  In buffing shop where bottom case is buffed, lot of dust is produced.  The ducts installed are not effective.  Some repairs were made to reduce dust inside the shop.
  • 21. Copyright2013-2014 Value Stream Mapping(AAHA) Objective  To eliminate the avoidable NVA and to minimize unavoidable NVA  To understand Process Flow.
  • 23. Copyright2013-2014 PROCESS FLOW Damper Case Welding Line Loading/Unloading Loading/Unloading Store Piston Rod Line Piston Rod Cutting Piston Rod Plating U/S Washing Assembly Begins Assembly Ends Despatch Area
  • 25. Copyright2013-2014 ELIMINIATING AVOIDABLE NVA & MINIMIZING UNAVOIDABLE NVA 1.The standard stoppage time is 50 mins for 1 shift. Though the average break time comes out to be more than 76 mins. There is a difference of 26 mins.  Keeping this in mind targets were given to each line each hour. If the line in consideration fails to achieve the target on regular basis, the HOD provides them with training. 2. Paint shop is located at the farther end of the plant. Due to this any major/minor breakdown takes time to be checked and corrected.  Many times the hose air pipe gets damaged and it takes more than 15 minutes to inform the maintenance dept and bring a new pipe for replacement. For this the supervisors and the operators were trained by the TPM dept. to take quick action if any such situation arises and the replacement pipes were present at the paint shop.. This would prevent line stoppage.
  • 26. Copyright2013-2014 ELIMINIATING AVOIDABLE NVA & MINIMIZING UNAVOIDABLE NVA 3. Due to the unavailability of trolley at the unloading station of the excise store the worker first had to place the goods on the floor and then wait for the trolley to be free. Then he loaded the goods on to the trolley.  Therefore two trolleys were made available to the workers. This would reduce the fatigue and increase productivity. 4.To reduce man material movement a new path was allocated for taking the piston rods to the plating line.  This lead to a decrease of 61% in man material movement.
  • 28. Copyright2013-2014 PREVIOUS PATH FOLLOWED (PISTON ROD LINE-->>PISTON ROD PLATING)
  • 29. Copyright2013-2014 NEW PATH FOLLOWED (PISTON ROD LINE-->>PISTON ROD PLATING)