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Talbros automotive component ltd. (FBD)
Mobile No: 9818682164
E-mail: ajay_sharma@talbros.com
Best Business Practice
Photo
Photo
Ajay Sharma
Corporate QA-Head
SonuTyagi
Customer Support
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QMS Certification
with validity
Major Esteem Customers and KOEL Share of Business
in %
Family of Parts Manufactured
( Attach Photographs )
Future Business Plan Future Infrastructure Improvement
1. Adding new customer MSIL and Hyundai in heat shield segment. o Plant re-layout to increase the space .
o Extension of plant to increase capacity by adding new
power press for heat shield segment .
Photo Photo
QMS Certificate &
Date of Validity
Supplier Name: Talbros Automotive Components Ltd.
COMPANY PROFILE
TATA
CUMMINS
28%
HERO
23%
VOLVO
14%
TATA
MOTORS
13%
SIMPSON
3%
ASHOK
LEYLAND
2%
ESCORTS
2%
MSIL
2%
KO
Others
11.5%
TATA CUMMINS HERO
VOLVO TATA MOTORS
SIMPSON ASHOK LEYLAND
ESCORTS MSIL
KOEL Others
Date of Certification: 19 Jan ‘2022
Date of expiration: 18 Jan’ 2025
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3
5230 5230
0 0 0 0 0 0
0
1000
2000
3000
4000
5000
6000
PPM Trend
FY 20-21 FY 21-22 Monthly PPM Trend
100% 96% 96% 96% 96% 96% 96% 96% 100%
0%
20%
40%
60%
80%
100%
Composite Score Overall %
FY 21-22 Monthly Composite Score
100 100 100 100 100 100 100 100 100
0 0 0 0 0
0
20
40
60
80
100
EHS Score
FY 21-22 Monthly EHS Score
Enabler and Result Matrix
0 0
1
0 0 0 0 0
0
1
2
NC Count
FY 20-21 FY 21-22 Monthly PPM Trend
100 92
76
100 100 100 100 100 100
0
20
40
60
80
100
120
Performance Index
FY 20-21 FY 21-22 Monthly PPM Trend
18
7
2 2 1 1 0 1
2 2 1 1 0 1
0
5
10
15
20
Zero Defect Projects
FY 20-21 Project Identified Project Completed
Part no . 4H.007.11.0.00
Defect-RF open issue
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MANUFACTURING PROCESS MAPPING THROUGH TURTLE DIAGRAM / VDA FMEA
NUMBEROF PROCESS
MAPPED/ TOTAL
PROCESS
NUMBEROF PROJECTS IDENTIFIED IN THE EACH ELEMENT OF THE TURTLE
INPUT
INFRA. &
MEASR
PROCESS RISKS
INVOLVED
PROCESS OWNER
COMPETENCY
PROCESS
DOC./ REC
PROCESS
EFFI./ EFFE
TOTAL
14 (Nos.) / 20 (Nos.)
0 (Nos.) 11 (Nos.) 5 (Nos.) 1 (Nos.) 2 (Nos.) 0 (Nos.) 19 (Nos.)
BUSINESS PROCESS MAPPING THROUGH TURTLE DIAGRAM / VDA FMEA
NUMBEROF PROCESS
MAPPED/ TOTAL
PROCESS
NUMBEROF PROJECTS IDENTIFIED IN THE EACH ELEMENTOF THE TURTLE
INPUT
INFRA. &
MEASR
PROCESS
RISKS
INVOLVED
PROCESS
OWNER
COMPETENCY
PROCESS
DOC./ REC
PROCESS
EFFI./ EFFE
TOTAL
9 (Nos.) / 41 (Nos.)
2 (Nos.) 9 (Nos.) 4 (Nos.) 2 (Nos.) 6 (Nos.) (Nos.) 23 (Nos.)
IMPROVEMENT PROJECTS IDENTIFIED OTHER THAN ABOVE TWO METHODOLOGIES
NUMBEROF PROJECTS IDENTIFIED IN THE LISTED BELOW
Composite Score Customer Feedback Other( Specify if any)
2 (Nos.) (Nos.) (Nos.)
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SERIAL
NUMBER
PROJECT DESCRIPTION
PROJECT BELONGS TO
WHICH PROCESS
PROJECT
RATING FROM
SDM SHEET
IMPACTON
NUMBER OF
PROCESS
COMPLETION
STATUS
1 Excel based monitoring system for calibration Business Process 265 1
2 QR code marking on part. Business Process 165 1
3 Energy (Electricity) consumption reduction Business Process 174 1
4 Packaging recycling initiatives -Returnable packaging Business Process 174 1
5 Reduction in water consumption Business Process 174 1
6 Set up single piece flow line in heat shield Business Process 308 1
7 Capacity enhancement by optimization of plant layout Business Process 148 1
8 Quality specific skill upgradation through Jagriti- Volume-3 Business Process 240 1
9 Rejection reduction in riveting process Manufacturing Process 170 1
10 Reduction in rejection Injection molding –IWH ( New Tech.) Manufacturing Process 153 1
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īąDefine
īƒ˜ Calibration due was being monitored in hard copy may cause non adherence of the
calibration schedule.
īąMeasure
īƒ˜ Approx. 700 no’s equipment calibration process review is difficult to monitor by
manually method , which may lead to non-adherence of the calibration schedule.
īą Analyze
īƒ˜ Alarming system is required to make alert before scheduled calibration date.
īąImprovement
īƒ˜ We have made conditional formatting in excel that give us alarm in following manner-
1. If calibration due date is less than 30 – Green signal will turn on
2. If calibration due date is less than 2weeks – Yellow light will turn on
3. If calibration due date is less than 1 week - Red light will turn on
īƒ˜Control
īƒ˜ Regular monitoring to review the calibration Plan vs actual via Formatting based excel
sheet.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
BEFORE
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
AFTER
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- Apr’ 22
â€ĸ Cut of Date: Apr’ 22
RESULT YES / NO
Productivity Improvement
System Improvement :
Quality Improvement :
Environment & Safety:
Moral:
Name of Process: Calibration- Business Process
Project Title -Excel based monitoring system for calibration
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Before After
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Name of Process: CSR & Composite Score Business Process
īąDefine
īƒ˜ Implementation of QR code as it is requirement of customer , compliance
requirement of composite score sheet .
īąMeasure
īƒ˜ Identify the customer requirements for traceability by QR code.
īąAnalyze
īƒ˜ We have identify the part list where we can implement the QR code requirement.
īąImprovement
īƒ˜ QR code implement in gasket for traceability to meet the customer requirement.
īąControl
īƒ˜ Updating the relevant document – Control plan , Drawing etc.
īƒ˜ Also upgrade the machine and installed the scanner to read the QR code to ensure
the readability of QR code 100 %
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- July ‘22
â€ĸ Cut of Date: Continuous
RESULT YES / NO
Productivity Improvement
CSR – QualityImprovement:
Cost Reduction (Yearly) :
Environment& Safety:
Moral:
BEFORE
AFTER
Name of Process: CSR & Composite Score- Business Process
Project Description-QR code marking on part.
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Before After
12 12
0
2
4
6
8
10
12
14
Part Identified QR code implement
Out of 12 QR code
implement parts one
part is for KOEL
“GP-3 Model “
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Name of Process: ISO 45001 & ISO 14001-EHS Business Process
īąDefine
īƒ˜ Initiative has been taken to reduce the electricity consumption to save electricity.
īąMeasure
īƒ˜ Data collected of previous year consumption of electricity.
īąAnalyze
īƒ˜ Brain storming done to identify the gaps and new initiative decided to reduce the
consumption of electricity.
īąImprovement
īƒ˜ Individual heat exchangers installed in on all batch ovens to reduce the PNG
consumption
īƒ˜ Old ACs replaced with new ones having R32 gas low power consumption and ozone
free depletion safe
īƒ˜ Cooling tower water PHE connected in circuit of MTC & chiller water line to reduce
the power consumption
īƒ˜ Switch off when not in used campaign.
īąControl
īƒ˜ We have linked the initiative with company objective of EHS for monitoring.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- Apr ‘22
â€ĸ Cut of Date: Continuous
RESULT YES / NO
Productivity Improvement
QualityImprovement:
Cost Reduction (Yearly) :
Environment& Safety:
Moral:
BEFORE
AFTER
Project Description-Reduce the consumption of electricity energy
Name of Process: -EHS- Business Process
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148,860
108,276
40,584
-
50,000
100,000
150,000
200,000
FY 2021-22 FY 2022-23 FY 2022-23-
Saving
Saving -40,584
Units annually
848,640
606,528
242,112
-
200,000
400,000
600,000
800,000
1,000,000
FY 2021-22 FY 2022-23 FY 2022-23-
Saving
Saving -
2,42,112 Units
annually
PNG consumption Reduction- SCM
Electricity consumption Reduction- KWh
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Name of Process: Packing Business Process
īąDefine
īƒ˜ Reduction in wooden pallet & carton for packaging and transportation of parts to save
the natural resources.
īąMeasure
īƒ˜ Initiative has been taken to reduce the consumption of wooden pallet and carton for
packaging and transportation of material.
īąAnalyze
īƒ˜ Wastage of natural resources.
īƒ˜ Space required for storage of wooden pallets.
īƒ˜ Damage during transportation need to scrap after few supply.
īąImprovement
īƒ˜ Implementation of returnable bins against the wooden pallets / Carton.
īąControl
īƒ˜ Sign the PSDS with customer to make it part of system.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Environment & Safety:
Moral:
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- May 22
â€ĸ Cut of Date: Continue process
BEFORE
AFTER
Project Description-Packaging Initiatives.
Name of Process: Packing- Business Process
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Before After
Part identified
for Returnable
packaging
instead of
wooden block
Returnable bins
implemented in
new projects
12 Lacs
Rupees
saving
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īąDefine
īƒ˜ Wastage of natural resources, Initiative has been taken to save the water.
īąMeasure
īƒ˜ Collect the data and measure the wastage of water after RO, and STP treatment .
īąAnalyze
īƒ˜ Analysis the gap and find the new initiative to save the water.
īąImprovement
īƒ˜ Wastage of RO water use in toilet flushing.
īƒ˜ STP treatment water used in gardening.
īƒ˜ Increase capacity of rain water harvesting to save water.
īąControl
īƒ˜ Linked with department MP under the EHS standard.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
QualityImprovement:
Cost Reduction (Yearly) :
Environment& Safety:
Moral:
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- Apr ‘21
â€ĸ Cut of Date: March’22
BEFORE
AFTER
Project Description- Reduction in water consumption
Name of Process: -EHS- Business Process
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0
3,432,000 3,432,000
0
1000000
2000000
3000000
4000000
FY 2021-22 FY 2022-23 FY 2022-23-
Saving
34.5 Lacs litre
water saving
annually
Reduction in Water Consumption- Litres
1
2 2
-
-
1
1
2
2
3
FY 2020-21 FY 2021-22 FY 2022-23
Increase the capacity of Rain water harvesting well –No’s
Total Capacity
of RHW is 16
Lakhs litres.
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īąDefine
īƒ˜ We are having batch production system resulting space required for storage of WIP
of material.
īąMeasure
īƒ˜ We have measured that we are consuming 100 sq ft area for WIP of batch
production.
īąAnalyze
īƒ˜ Due to batch production following hurdle were observed .
ī‚§ 100 sq ft area used
ī‚§ Operator fatigue was more.
ī‚§ No. of trolley is required keep the material.
ī‚§ Non adherence of 5S.
īąImprovement
īƒ˜ Set up a single piece flow lline.
īƒ˜ Reduce the operator fatigue.
īƒ˜ Reduce the die changeover time, reduction in material handling time.
īƒ˜ Save no. of bins/ trolleys of storage of material.
īƒ˜ Reduction in mix of process part, reduce the rejection risk.
īƒ˜ Production capacity increased. ( SPM 2.5 to SPM 3.5 ) increase stroke in per day is
1280 No’s , Monthly -32,250 No’s.
īąControl
īƒ˜ Conveyor belt setup done between the machine to flow the single part flow .
īƒ˜ Balancing the line according to operation and set up done for single piece flow.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Saving of Area
Moral:
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- Jun ‘22
â€ĸ Cut of Date: Jun’ 22
BEFORE
AFTER
Project Description-Set up single piece flow line in heat shield
Name of Process: Continual Improvement- Business Process
SPM increased
2.5 to 3.5
Stroke saving
32,250 monthly
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īąDefine
īƒ˜ Space constraint in shop floor area.
īƒ˜ 5’S not adhere.
īąMeasure
īƒ˜ Layout review and D2D approach.
īƒ˜ Adding new customers in basket.
īƒ˜ New machine need to installed to enhance the capacity
īąAnalyze
īƒ˜ Need to change existing layout for space optimization.
īąImprovement
īƒ˜ Plant layout changed & improved the 5’S.
īƒ˜ Mezzanine concept implement in FGS area.
īƒ˜ 200 Ton three new machine added in existing area.
īƒ˜ 3 No’s new riveting machine added in existing area.
īƒ˜ Synchronize the Heat shield process.
īƒ˜ Centralize the all inspection and packing area under one roof.
īąControl
īƒ˜ All the changes incorporated in plant layout.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Environment & Safety:
Space capacity :
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- Dec ‘21
â€ĸ Cut of Date: Oct 22
BEFORE
AFTER
Space
Save
1117.8 sq.
meter
Project Description-Capacity enhancement by optimization of plant layout
Name of Process: Plant Layout-Business Process
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Glimpse of Plant Layout changes.
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Before After
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Before After
Plant Layout
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â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- Sept’ 22
â€ĸ Cut of Date:-Sept’22
īąDefine
īƒ˜ To escalating the human skill up to next level & meeting the customer expectations
quality related module is not available
īąMeasure
īƒ˜ As per customer expectations it observed that quality specific training module is not
available
īąAnalyze
īƒ˜ Theoretical understanding of the operators /inspectors are not so good related to
instruments or other concepts like RBA, OEE, LPA..
īąImprovement
īƒ˜ We have drafted Jagriti Volume-3 specific to the quality function requirements
īƒ˜ Control
īƒ˜ No of trained operators/inspectors
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Environment & Safety:
Moral:
BEFORE
AFTER
Project Description-Quality specific skill upgradation through Jagriti-3
Name of Process: Human Resource- Business Process
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Jagriti-01
īļ Product Knowledge
īļ Type of Defect
īļ Failure of Gasket
īļ 5S
īļ 3M
īļ Rules Of Factory
Jagriti-02
īļ Introduction of shop floor
īļ Type of machine
īļ Handling of abnormal situation
īļ Work order
īļ SOP- All process
īļ Check sheet
īļ Type of Gasket
Jagriti-03
īļ Knowledge of Quality
Instrument
īļ Set Up approval
īļ RCA
īļ Shift Handover
īļ RBA
īļ LPA
īļ Kaizen
īļ Type of breakdown
īļ PPM
īļ OEE
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īąDefine
īƒ˜ Caution mark fitment in wrong direction and assembly more than one caution
mark on one heat shield.
īąMeasure
īƒ˜ Data collection done from red bin analysis.
īą Analyze
īƒ˜ Due to child part assembly our whole part get rejected which cost is much higher
than the child part.
īąImprovement
īƒ˜ Vision Poka Yoke add in machine which prevent the wrong direction of caution mark .
īƒ˜ Shooting panel provided in machine to prevent the assembly of two child part at a
same time.
īƒ˜Control
īƒ˜ Check point added in process check sheet for verification of Poka Yoke.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
BEFORE
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
AFTER
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- May ‘22
â€ĸ Cut of Date: May ’22
RESULT YES / NO
Productivity Improvement
System Improvement :
Quality Improvement :
Environment & Safety:
Moral:
98
41
26 25
6 0 0 0 0 0
0
20
40
60
80
100
2022
Jan-22
Feb-22
Mar-22
Apr-22
May-22
Jun-22
Jul-22
Aug-22
Sep-22
Before After
Project Title –Rejection reduction in riveting process
Name of Process: Riveting Process- Manufacturing Process
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īąDefine
īƒ˜ Huge rejection in Injection molding.
īąMeasure
īƒ˜ Data collection done from red bin analysis.
īą Analyze
īƒ˜ Brainstorming done to identified related tool & machine during RBA
īąImprovement
īƒ˜ Huge reduction in rejection form 37 % to 3.5 %
īƒ˜ Increase the productivity in final inspection. ( Current cycle time is 1.30 min earlier it
was 2.30 min ) with automated recording of reports in system itself.
īƒ˜Control
īƒ˜ All the identified gaps updated in concern documents & same have been adhered
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
BEFORE
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
AFTER
â€ĸ Tool Used: DMAIC & Turtle diagram
â€ĸ Project Start:- Jan ‘21
â€ĸ Cut of Date: Continue Process
RESULT YES / NO
Productivity Improvement
System Improvement :
Quality Improvement :
Environment & Safety:
Moral:
Project Title –Reduction in rejection of Injection molding –IWH ( New Tech.)
Name of Process: Injection Molding- Manufacturing Process
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1540 787 523 479 284 188 157 160 147 104 88 79 44 23 19 7
33
50
62
72
78 82 86 89 92 94 96 98 99 99 100 100
0
10
20
30
40
50
60
70
80
90
100
0
200
400
600
800
1000
1200
1400
1600
Pareto FY 2021-22
481 411 240 139 116 114 71 11 20 5
30
55
70
79
86
93
98 98 100 100
0
10
20
30
40
50
60
70
80
90
100
0
200
400
600
800
1000
1200
1400
1600
Short
moulding
Wire cut Rubber cut Leakage on
wire
Bonding fail Crack Air bubble Under cure Damage Burn mark
Pareto FY 2022-23
4630 1608
0
500
1000
1500
2000
2500
3000
3500
4000
4500
5000
FY 2021-22 Fy 2022-23
Rejection Qty.
16 10
0
2
4
6
8
10
12
14
16
18
FY 2021-22 Fy 2022-23
Defect Elimination
6/25/2023 52
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 52
Cable Cut
Loose tie
Continuity
Failure
Wrong QR code
Leakage on wire
Carrier Crack
Air bubble
Part damage
Short Moulding
Man Machine
Material
Method
Unskilled Operator
Manual cutting of tie.
Tie Cutting length not fixed
Manual process tie fastening. Tie cutting method not define
Tie location not define
Un aware about the continuity process ( Nut to Nut & Nut to terminal )
Resistance test not define in SOP
Part resistance test method not define
Manual test of Continuity
Manual process of application
Nut rotation check point not added in SOP
Nut rotation check point not added in SOP
No inspection at Receipt stage
Wire cut generated in parts during deflashing , due to routing of wire done before
deflashing
Wire locking provision not provide in tool
Pillar length of tool is more .
Sharp edges & Play in magnet clamp
Wrong method of wire bundling during taping
Material leakage on wire due to Mould temp high
Material leakage on wire due to Cushion high
Raw Material Not proper pre-heating due to material
not loading In hopper simultaneously
Mould design and terminal pin design not
compatible
Wire cut from supplier end
Wire insulation material degrade
Insulation Thickness less
ML lower side
Rheo gates not validated
Expired chemlok used
Rubber High Hardness
Nut cage & thimble sharp edges
Material Not proper pre-heating
Unskilled for tie operation
Operator not aware about the SOP
Brain storming & Root Cause Analysis
6/25/2023 53
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 53
Before After
No extra guide lock available for wire routing Extra guide locking provided in tool
Action on wire cut
6/25/2023 54
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 54
Before
Tool design improved
Sharp edge in insert
After
Action on wire cut
6/25/2023 55
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 55
Before After
Action on wire cut
L Type support provided in mould
No support
6/25/2023 56
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 56
Before
Wire cut generating during deflashing due to
Flash generated near to wire area moulding
process
After
Mould design improved
Action On Wire cut
6/25/2023 57
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 57
Before After
Cutter used for extra flash removing Flashes removal method changed
Action on wire cut
6/25/2023 58
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 58
Before
Correct wire taping method developed
Wrong method of wire Taping –if wire stretch in
this condition then wire cut will generate in part
After
Action on wire cut
6/25/2023 59
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 59
Before After
Manual cutter
Tie cutter gun provided instead of manual
cutter
Action on tie loose / cut
6/25/2023 60
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 60
Before After
Wire wound over the sharp edges of plastic
carrier
Method developed ,no wire routing over the
sharp edges of plastic carrier.
Action on wire cut in routing process
6/25/2023 61
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 61
Before After
Material Loading in hopper manually
Material loader provided in carrier injection
moulding
Action on leakage of wire
6/25/2023 62
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 62
Before After
Buzzer not available Buzzer provided for spray frequency Adherence
NA
Action on Rubber cut in injection Moulding
6/25/2023 63
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 63
Installation of continuity testing machine
Continuity machine installed to check the continuity earlier
manual method used
Inspection Cycle time
Cycle time earlier – 2.3 min
Now cycle time -1.3 min
6/25/2023 64
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 64
Wrong QR code on gasket – Install leakage testing machine linkage with QR code.
1-Barcode Printer interlink with system after ok result from machine QR code print
2.To avoid wrong barcode printing Make model wise program & sensor mounting
6/25/2023 65
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 65
BEFORE AFTER
Adhesive applied on terminal without fixture
Fixture made for application of chemlok on
terminal pin which is cover 75 % area of pin ,
earlier brush was used which cover 100 % area
of pin which leads continuity issue
100%
Action On Continuity Issue
6/25/2023 66
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 66
Before After
No provision of holding part in mould Part holding provision added in mould
Action on crack in carrier
6/25/2023 67
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 67
Before After
Lock crack due to no clearance in mould during
butting
Chamfer provided in mould
Action on Crack Issue
6/25/2023 68
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 68
Before After
No chrome plating on mould that create weld
line
Chrome Plating provided in mould to avoid weld
line issue
Action on air bubble
6/25/2023 69
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 69
Before
Material handling in bin with separator
Material handling in bin with out separator
After
Action on part damage
6/25/2023 70
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 70
Before After
No strip guide loader available
Strip guide stand loader provide to continues
feeding of rubber in feeder
Action- Short Moulding
6/25/2023 71
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 71
Before After
No grub screw provision in mould
Grub screw provision provided in mould to
balance rubber flow cavity wise
Action on Short Moulding
6/25/2023 72
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 72
Before After
Operator have to go behind the machine to
check the rubber strip condition
Convex mirror provided to check the rubber
strip condition
No before pic available
Action- Short Moulding
6/25/2023 73
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 73
Before
Process parameter freeze after validation
HRTC temperature maintain b/w(40 ~50) which
reduce the short moulding defect
HRTC temperature not maintain
After
Action on short moulding
6/25/2023 74
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 74
Before
Process parameter freeze after validation
Cushion max 7.7 & min 0.7 fixed to reduce the
short moulding defect.
Cushion max 16.6 & min 0.7
After
Action on short moulding
6/25/2023 75
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 75
36.95
7.47
3.5
5.5 4.5 3.5 3.1 2.8 2.7 2.5
0
5
10
15
20
25
30
35
40
FY
20-21
FY
21-22
FY
22-23
Apr-22
May-22
Jun-22
Jul-22
Aug-22
Sep-22
Oct-22
IWH – Rejection %
Development
Time
Increased productivity by
continuity machine .
Earlier 626 No’s
Now 1107 No’s
Saving 481 no’s / day
Monthly -12025 no’s
6/25/2023 76
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 76
Project 1
Excel based
monitoring
system for
calibration
Effective
monitoring of
calibration
plan vs actual
Meet the
customer
requirement
Traceability of
part.
Project 2
QR code
marking on
part
Project 3
Reduction in
Electricity
consumption.
Saving of of
40,584 unit in
PNG & 2,42
lacs Units in
electricity
Natural
Resource
saving
Saving of 12
lacs rupees
annually
Natural
Resource
saving
Project-4
Packaging
recycling
initiatives
Learning / Take Away
Project 5
Reduction in
water
consumption
Saving of 34
lacs liters
water
annually
Increase RHW
capacity 16
lacs liters
Natural
Resource
saving
Production
capacity
increased.
( SPM 2.5 to
SPM 3.5 )
Saving of
32,250 stroke
monthly
Project 6
Set up single
piece flow line
in heat shield
Project 7
Capacity
enhancement by
optimization of
plant layout
Space Save of
1117.8 sq.
meter
Adding new
machine in
existing
Skill
upgradation of
employee
Project-8
Introduction
of Jagriti 3
Project 9
Rejection
reduction in
riveting
process
Reduction of
rejection from
98 no’s to
zero.
Reduction in
rejection form
37 % to 3.5 %
Increase the
productivity at
final
inspection
stage
Monthly
12,025 no’s
Project 10
Reduction in
rejection in
Injection
molding -IWH
6/25/2023 77
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 77
Thank You
Zero Defect journey Continueâ€Ļ

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Best Business Practice @ Nov 22.pptx

  • 1. 6/25/2023 1 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 1 Talbros automotive component ltd. (FBD) Mobile No: 9818682164 E-mail: ajay_sharma@talbros.com Best Business Practice Photo Photo Ajay Sharma Corporate QA-Head SonuTyagi Customer Support
  • 2. 6/25/2023 2 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 2 QMS Certification with validity Major Esteem Customers and KOEL Share of Business in % Family of Parts Manufactured ( Attach Photographs ) Future Business Plan Future Infrastructure Improvement 1. Adding new customer MSIL and Hyundai in heat shield segment. o Plant re-layout to increase the space . o Extension of plant to increase capacity by adding new power press for heat shield segment . Photo Photo QMS Certificate & Date of Validity Supplier Name: Talbros Automotive Components Ltd. COMPANY PROFILE TATA CUMMINS 28% HERO 23% VOLVO 14% TATA MOTORS 13% SIMPSON 3% ASHOK LEYLAND 2% ESCORTS 2% MSIL 2% KO Others 11.5% TATA CUMMINS HERO VOLVO TATA MOTORS SIMPSON ASHOK LEYLAND ESCORTS MSIL KOEL Others Date of Certification: 19 Jan ‘2022 Date of expiration: 18 Jan’ 2025
  • 3. 6/25/2023 3 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 3 3 5230 5230 0 0 0 0 0 0 0 1000 2000 3000 4000 5000 6000 PPM Trend FY 20-21 FY 21-22 Monthly PPM Trend 100% 96% 96% 96% 96% 96% 96% 96% 100% 0% 20% 40% 60% 80% 100% Composite Score Overall % FY 21-22 Monthly Composite Score 100 100 100 100 100 100 100 100 100 0 0 0 0 0 0 20 40 60 80 100 EHS Score FY 21-22 Monthly EHS Score Enabler and Result Matrix 0 0 1 0 0 0 0 0 0 1 2 NC Count FY 20-21 FY 21-22 Monthly PPM Trend 100 92 76 100 100 100 100 100 100 0 20 40 60 80 100 120 Performance Index FY 20-21 FY 21-22 Monthly PPM Trend 18 7 2 2 1 1 0 1 2 2 1 1 0 1 0 5 10 15 20 Zero Defect Projects FY 20-21 Project Identified Project Completed Part no . 4H.007.11.0.00 Defect-RF open issue
  • 4. 6/25/2023 4 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 4 MANUFACTURING PROCESS MAPPING THROUGH TURTLE DIAGRAM / VDA FMEA NUMBEROF PROCESS MAPPED/ TOTAL PROCESS NUMBEROF PROJECTS IDENTIFIED IN THE EACH ELEMENT OF THE TURTLE INPUT INFRA. & MEASR PROCESS RISKS INVOLVED PROCESS OWNER COMPETENCY PROCESS DOC./ REC PROCESS EFFI./ EFFE TOTAL 14 (Nos.) / 20 (Nos.) 0 (Nos.) 11 (Nos.) 5 (Nos.) 1 (Nos.) 2 (Nos.) 0 (Nos.) 19 (Nos.) BUSINESS PROCESS MAPPING THROUGH TURTLE DIAGRAM / VDA FMEA NUMBEROF PROCESS MAPPED/ TOTAL PROCESS NUMBEROF PROJECTS IDENTIFIED IN THE EACH ELEMENTOF THE TURTLE INPUT INFRA. & MEASR PROCESS RISKS INVOLVED PROCESS OWNER COMPETENCY PROCESS DOC./ REC PROCESS EFFI./ EFFE TOTAL 9 (Nos.) / 41 (Nos.) 2 (Nos.) 9 (Nos.) 4 (Nos.) 2 (Nos.) 6 (Nos.) (Nos.) 23 (Nos.) IMPROVEMENT PROJECTS IDENTIFIED OTHER THAN ABOVE TWO METHODOLOGIES NUMBEROF PROJECTS IDENTIFIED IN THE LISTED BELOW Composite Score Customer Feedback Other( Specify if any) 2 (Nos.) (Nos.) (Nos.)
  • 5. 6/25/2023 5 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 5 SERIAL NUMBER PROJECT DESCRIPTION PROJECT BELONGS TO WHICH PROCESS PROJECT RATING FROM SDM SHEET IMPACTON NUMBER OF PROCESS COMPLETION STATUS 1 Excel based monitoring system for calibration Business Process 265 1 2 QR code marking on part. Business Process 165 1 3 Energy (Electricity) consumption reduction Business Process 174 1 4 Packaging recycling initiatives -Returnable packaging Business Process 174 1 5 Reduction in water consumption Business Process 174 1 6 Set up single piece flow line in heat shield Business Process 308 1 7 Capacity enhancement by optimization of plant layout Business Process 148 1 8 Quality specific skill upgradation through Jagriti- Volume-3 Business Process 240 1 9 Rejection reduction in riveting process Manufacturing Process 170 1 10 Reduction in rejection Injection molding –IWH ( New Tech.) Manufacturing Process 153 1
  • 6. 6/25/2023 6 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 6 īąDefine īƒ˜ Calibration due was being monitored in hard copy may cause non adherence of the calibration schedule. īąMeasure īƒ˜ Approx. 700 no’s equipment calibration process review is difficult to monitor by manually method , which may lead to non-adherence of the calibration schedule. īą Analyze īƒ˜ Alarming system is required to make alert before scheduled calibration date. īąImprovement īƒ˜ We have made conditional formatting in excel that give us alarm in following manner- 1. If calibration due date is less than 30 – Green signal will turn on 2. If calibration due date is less than 2weeks – Yellow light will turn on 3. If calibration due date is less than 1 week - Red light will turn on īƒ˜Control īƒ˜ Regular monitoring to review the calibration Plan vs actual via Formatting based excel sheet. Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s BEFORE Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s AFTER â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- Apr’ 22 â€ĸ Cut of Date: Apr’ 22 RESULT YES / NO Productivity Improvement System Improvement : Quality Improvement : Environment & Safety: Moral: Name of Process: Calibration- Business Process Project Title -Excel based monitoring system for calibration
  • 7. 6/25/2023 7 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 7 Before After
  • 8. 6/25/2023 8 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 8 Name of Process: CSR & Composite Score Business Process īąDefine īƒ˜ Implementation of QR code as it is requirement of customer , compliance requirement of composite score sheet . īąMeasure īƒ˜ Identify the customer requirements for traceability by QR code. īąAnalyze īƒ˜ We have identify the part list where we can implement the QR code requirement. īąImprovement īƒ˜ QR code implement in gasket for traceability to meet the customer requirement. īąControl īƒ˜ Updating the relevant document – Control plan , Drawing etc. īƒ˜ Also upgrade the machine and installed the scanner to read the QR code to ensure the readability of QR code 100 % Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- July ‘22 â€ĸ Cut of Date: Continuous RESULT YES / NO Productivity Improvement CSR – QualityImprovement: Cost Reduction (Yearly) : Environment& Safety: Moral: BEFORE AFTER Name of Process: CSR & Composite Score- Business Process Project Description-QR code marking on part.
  • 9. 6/25/2023 9 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 9 Before After 12 12 0 2 4 6 8 10 12 14 Part Identified QR code implement Out of 12 QR code implement parts one part is for KOEL “GP-3 Model “
  • 10. 6/25/2023 10 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 10 Name of Process: ISO 45001 & ISO 14001-EHS Business Process īąDefine īƒ˜ Initiative has been taken to reduce the electricity consumption to save electricity. īąMeasure īƒ˜ Data collected of previous year consumption of electricity. īąAnalyze īƒ˜ Brain storming done to identify the gaps and new initiative decided to reduce the consumption of electricity. īąImprovement īƒ˜ Individual heat exchangers installed in on all batch ovens to reduce the PNG consumption īƒ˜ Old ACs replaced with new ones having R32 gas low power consumption and ozone free depletion safe īƒ˜ Cooling tower water PHE connected in circuit of MTC & chiller water line to reduce the power consumption īƒ˜ Switch off when not in used campaign. īąControl īƒ˜ We have linked the initiative with company objective of EHS for monitoring. Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- Apr ‘22 â€ĸ Cut of Date: Continuous RESULT YES / NO Productivity Improvement QualityImprovement: Cost Reduction (Yearly) : Environment& Safety: Moral: BEFORE AFTER Project Description-Reduce the consumption of electricity energy Name of Process: -EHS- Business Process
  • 11. 6/25/2023 11 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 11 148,860 108,276 40,584 - 50,000 100,000 150,000 200,000 FY 2021-22 FY 2022-23 FY 2022-23- Saving Saving -40,584 Units annually 848,640 606,528 242,112 - 200,000 400,000 600,000 800,000 1,000,000 FY 2021-22 FY 2022-23 FY 2022-23- Saving Saving - 2,42,112 Units annually PNG consumption Reduction- SCM Electricity consumption Reduction- KWh
  • 12. 6/25/2023 12 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 12 Name of Process: Packing Business Process īąDefine īƒ˜ Reduction in wooden pallet & carton for packaging and transportation of parts to save the natural resources. īąMeasure īƒ˜ Initiative has been taken to reduce the consumption of wooden pallet and carton for packaging and transportation of material. īąAnalyze īƒ˜ Wastage of natural resources. īƒ˜ Space required for storage of wooden pallets. īƒ˜ Damage during transportation need to scrap after few supply. īąImprovement īƒ˜ Implementation of returnable bins against the wooden pallets / Carton. īąControl īƒ˜ Sign the PSDS with customer to make it part of system. Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s RESULT YES / NO Productivity Improvement Quality Improvement : Cost Reduction (Yearly) : Environment & Safety: Moral: â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- May 22 â€ĸ Cut of Date: Continue process BEFORE AFTER Project Description-Packaging Initiatives. Name of Process: Packing- Business Process
  • 13. 6/25/2023 13 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 13 Before After Part identified for Returnable packaging instead of wooden block Returnable bins implemented in new projects 12 Lacs Rupees saving
  • 14. 6/25/2023 14 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 14 īąDefine īƒ˜ Wastage of natural resources, Initiative has been taken to save the water. īąMeasure īƒ˜ Collect the data and measure the wastage of water after RO, and STP treatment . īąAnalyze īƒ˜ Analysis the gap and find the new initiative to save the water. īąImprovement īƒ˜ Wastage of RO water use in toilet flushing. īƒ˜ STP treatment water used in gardening. īƒ˜ Increase capacity of rain water harvesting to save water. īąControl īƒ˜ Linked with department MP under the EHS standard. Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s RESULT YES / NO Productivity Improvement QualityImprovement: Cost Reduction (Yearly) : Environment& Safety: Moral: â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- Apr ‘21 â€ĸ Cut of Date: March’22 BEFORE AFTER Project Description- Reduction in water consumption Name of Process: -EHS- Business Process
  • 15. 6/25/2023 15 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 15 0 3,432,000 3,432,000 0 1000000 2000000 3000000 4000000 FY 2021-22 FY 2022-23 FY 2022-23- Saving 34.5 Lacs litre water saving annually Reduction in Water Consumption- Litres 1 2 2 - - 1 1 2 2 3 FY 2020-21 FY 2021-22 FY 2022-23 Increase the capacity of Rain water harvesting well –No’s Total Capacity of RHW is 16 Lakhs litres.
  • 16. 6/25/2023 16 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 16 īąDefine īƒ˜ We are having batch production system resulting space required for storage of WIP of material. īąMeasure īƒ˜ We have measured that we are consuming 100 sq ft area for WIP of batch production. īąAnalyze īƒ˜ Due to batch production following hurdle were observed . ī‚§ 100 sq ft area used ī‚§ Operator fatigue was more. ī‚§ No. of trolley is required keep the material. ī‚§ Non adherence of 5S. īąImprovement īƒ˜ Set up a single piece flow lline. īƒ˜ Reduce the operator fatigue. īƒ˜ Reduce the die changeover time, reduction in material handling time. īƒ˜ Save no. of bins/ trolleys of storage of material. īƒ˜ Reduction in mix of process part, reduce the rejection risk. īƒ˜ Production capacity increased. ( SPM 2.5 to SPM 3.5 ) increase stroke in per day is 1280 No’s , Monthly -32,250 No’s. īąControl īƒ˜ Conveyor belt setup done between the machine to flow the single part flow . īƒ˜ Balancing the line according to operation and set up done for single piece flow. Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s RESULT YES / NO Productivity Improvement Quality Improvement : Cost Reduction (Yearly) : Saving of Area Moral: â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- Jun ‘22 â€ĸ Cut of Date: Jun’ 22 BEFORE AFTER Project Description-Set up single piece flow line in heat shield Name of Process: Continual Improvement- Business Process SPM increased 2.5 to 3.5 Stroke saving 32,250 monthly
  • 17. 6/25/2023 17 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 17 īąDefine īƒ˜ Space constraint in shop floor area. īƒ˜ 5’S not adhere. īąMeasure īƒ˜ Layout review and D2D approach. īƒ˜ Adding new customers in basket. īƒ˜ New machine need to installed to enhance the capacity īąAnalyze īƒ˜ Need to change existing layout for space optimization. īąImprovement īƒ˜ Plant layout changed & improved the 5’S. īƒ˜ Mezzanine concept implement in FGS area. īƒ˜ 200 Ton three new machine added in existing area. īƒ˜ 3 No’s new riveting machine added in existing area. īƒ˜ Synchronize the Heat shield process. īƒ˜ Centralize the all inspection and packing area under one roof. īąControl īƒ˜ All the changes incorporated in plant layout. Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s RESULT YES / NO Productivity Improvement Quality Improvement : Cost Reduction (Yearly) : Environment & Safety: Space capacity : â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- Dec ‘21 â€ĸ Cut of Date: Oct 22 BEFORE AFTER Space Save 1117.8 sq. meter Project Description-Capacity enhancement by optimization of plant layout Name of Process: Plant Layout-Business Process
  • 18. 6/25/2023 18 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 18
  • 19. 6/25/2023 19 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 19 Glimpse of Plant Layout changes.
  • 20. 6/25/2023 20 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 20
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  • 34. 6/25/2023 34 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 34
  • 35. 6/25/2023 35 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 35 Before After
  • 36. 6/25/2023 36 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 36 Before After Plant Layout
  • 37. 6/25/2023 37 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 37 â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- Sept’ 22 â€ĸ Cut of Date:-Sept’22 īąDefine īƒ˜ To escalating the human skill up to next level & meeting the customer expectations quality related module is not available īąMeasure īƒ˜ As per customer expectations it observed that quality specific training module is not available īąAnalyze īƒ˜ Theoretical understanding of the operators /inspectors are not so good related to instruments or other concepts like RBA, OEE, LPA.. īąImprovement īƒ˜ We have drafted Jagriti Volume-3 specific to the quality function requirements īƒ˜ Control īƒ˜ No of trained operators/inspectors Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s RESULT YES / NO Productivity Improvement Quality Improvement : Cost Reduction (Yearly) : Environment & Safety: Moral: BEFORE AFTER Project Description-Quality specific skill upgradation through Jagriti-3 Name of Process: Human Resource- Business Process
  • 38. 6/25/2023 38 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 38 Jagriti-01 īļ Product Knowledge īļ Type of Defect īļ Failure of Gasket īļ 5S īļ 3M īļ Rules Of Factory Jagriti-02 īļ Introduction of shop floor īļ Type of machine īļ Handling of abnormal situation īļ Work order īļ SOP- All process īļ Check sheet īļ Type of Gasket Jagriti-03 īļ Knowledge of Quality Instrument īļ Set Up approval īļ RCA īļ Shift Handover īļ RBA īļ LPA īļ Kaizen īļ Type of breakdown īļ PPM īļ OEE
  • 39. 6/25/2023 39 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 39
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  • 43. 6/25/2023 43 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 43
  • 44. 6/25/2023 44 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 44
  • 45. 6/25/2023 45 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 45
  • 46. 6/25/2023 46 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 46
  • 47. 6/25/2023 47 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 47
  • 48. 6/25/2023 48 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 48
  • 49. 6/25/2023 49 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 49 īąDefine īƒ˜ Caution mark fitment in wrong direction and assembly more than one caution mark on one heat shield. īąMeasure īƒ˜ Data collection done from red bin analysis. īą Analyze īƒ˜ Due to child part assembly our whole part get rejected which cost is much higher than the child part. īąImprovement īƒ˜ Vision Poka Yoke add in machine which prevent the wrong direction of caution mark . īƒ˜ Shooting panel provided in machine to prevent the assembly of two child part at a same time. īƒ˜Control īƒ˜ Check point added in process check sheet for verification of Poka Yoke. Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s BEFORE Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s AFTER â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- May ‘22 â€ĸ Cut of Date: May ’22 RESULT YES / NO Productivity Improvement System Improvement : Quality Improvement : Environment & Safety: Moral: 98 41 26 25 6 0 0 0 0 0 0 20 40 60 80 100 2022 Jan-22 Feb-22 Mar-22 Apr-22 May-22 Jun-22 Jul-22 Aug-22 Sep-22 Before After Project Title –Rejection reduction in riveting process Name of Process: Riveting Process- Manufacturing Process
  • 50. 6/25/2023 50 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 50 īąDefine īƒ˜ Huge rejection in Injection molding. īąMeasure īƒ˜ Data collection done from red bin analysis. īą Analyze īƒ˜ Brainstorming done to identified related tool & machine during RBA īąImprovement īƒ˜ Huge reduction in rejection form 37 % to 3.5 % īƒ˜ Increase the productivity in final inspection. ( Current cycle time is 1.30 min earlier it was 2.30 min ) with automated recording of reports in system itself. īƒ˜Control īƒ˜ All the identified gaps updated in concern documents & same have been adhered Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s BEFORE Input Infrastructure resource Risk Involved in process Process owner competency Process documents & records Process efficiency & effectivenes s AFTER â€ĸ Tool Used: DMAIC & Turtle diagram â€ĸ Project Start:- Jan ‘21 â€ĸ Cut of Date: Continue Process RESULT YES / NO Productivity Improvement System Improvement : Quality Improvement : Environment & Safety: Moral: Project Title –Reduction in rejection of Injection molding –IWH ( New Tech.) Name of Process: Injection Molding- Manufacturing Process
  • 51. 6/25/2023 51 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 51 1540 787 523 479 284 188 157 160 147 104 88 79 44 23 19 7 33 50 62 72 78 82 86 89 92 94 96 98 99 99 100 100 0 10 20 30 40 50 60 70 80 90 100 0 200 400 600 800 1000 1200 1400 1600 Pareto FY 2021-22 481 411 240 139 116 114 71 11 20 5 30 55 70 79 86 93 98 98 100 100 0 10 20 30 40 50 60 70 80 90 100 0 200 400 600 800 1000 1200 1400 1600 Short moulding Wire cut Rubber cut Leakage on wire Bonding fail Crack Air bubble Under cure Damage Burn mark Pareto FY 2022-23 4630 1608 0 500 1000 1500 2000 2500 3000 3500 4000 4500 5000 FY 2021-22 Fy 2022-23 Rejection Qty. 16 10 0 2 4 6 8 10 12 14 16 18 FY 2021-22 Fy 2022-23 Defect Elimination
  • 52. 6/25/2023 52 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 52 Cable Cut Loose tie Continuity Failure Wrong QR code Leakage on wire Carrier Crack Air bubble Part damage Short Moulding Man Machine Material Method Unskilled Operator Manual cutting of tie. Tie Cutting length not fixed Manual process tie fastening. Tie cutting method not define Tie location not define Un aware about the continuity process ( Nut to Nut & Nut to terminal ) Resistance test not define in SOP Part resistance test method not define Manual test of Continuity Manual process of application Nut rotation check point not added in SOP Nut rotation check point not added in SOP No inspection at Receipt stage Wire cut generated in parts during deflashing , due to routing of wire done before deflashing Wire locking provision not provide in tool Pillar length of tool is more . Sharp edges & Play in magnet clamp Wrong method of wire bundling during taping Material leakage on wire due to Mould temp high Material leakage on wire due to Cushion high Raw Material Not proper pre-heating due to material not loading In hopper simultaneously Mould design and terminal pin design not compatible Wire cut from supplier end Wire insulation material degrade Insulation Thickness less ML lower side Rheo gates not validated Expired chemlok used Rubber High Hardness Nut cage & thimble sharp edges Material Not proper pre-heating Unskilled for tie operation Operator not aware about the SOP Brain storming & Root Cause Analysis
  • 53. 6/25/2023 53 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 53 Before After No extra guide lock available for wire routing Extra guide locking provided in tool Action on wire cut
  • 54. 6/25/2023 54 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 54 Before Tool design improved Sharp edge in insert After Action on wire cut
  • 55. 6/25/2023 55 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 55 Before After Action on wire cut L Type support provided in mould No support
  • 56. 6/25/2023 56 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 56 Before Wire cut generating during deflashing due to Flash generated near to wire area moulding process After Mould design improved Action On Wire cut
  • 57. 6/25/2023 57 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 57 Before After Cutter used for extra flash removing Flashes removal method changed Action on wire cut
  • 58. 6/25/2023 58 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 58 Before Correct wire taping method developed Wrong method of wire Taping –if wire stretch in this condition then wire cut will generate in part After Action on wire cut
  • 59. 6/25/2023 59 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 59 Before After Manual cutter Tie cutter gun provided instead of manual cutter Action on tie loose / cut
  • 60. 6/25/2023 60 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 60 Before After Wire wound over the sharp edges of plastic carrier Method developed ,no wire routing over the sharp edges of plastic carrier. Action on wire cut in routing process
  • 61. 6/25/2023 61 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 61 Before After Material Loading in hopper manually Material loader provided in carrier injection moulding Action on leakage of wire
  • 62. 6/25/2023 62 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 62 Before After Buzzer not available Buzzer provided for spray frequency Adherence NA Action on Rubber cut in injection Moulding
  • 63. 6/25/2023 63 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 63 Installation of continuity testing machine Continuity machine installed to check the continuity earlier manual method used Inspection Cycle time Cycle time earlier – 2.3 min Now cycle time -1.3 min
  • 64. 6/25/2023 64 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 64 Wrong QR code on gasket – Install leakage testing machine linkage with QR code. 1-Barcode Printer interlink with system after ok result from machine QR code print 2.To avoid wrong barcode printing Make model wise program & sensor mounting
  • 65. 6/25/2023 65 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 65 BEFORE AFTER Adhesive applied on terminal without fixture Fixture made for application of chemlok on terminal pin which is cover 75 % area of pin , earlier brush was used which cover 100 % area of pin which leads continuity issue 100% Action On Continuity Issue
  • 66. 6/25/2023 66 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 66 Before After No provision of holding part in mould Part holding provision added in mould Action on crack in carrier
  • 67. 6/25/2023 67 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 67 Before After Lock crack due to no clearance in mould during butting Chamfer provided in mould Action on Crack Issue
  • 68. 6/25/2023 68 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 68 Before After No chrome plating on mould that create weld line Chrome Plating provided in mould to avoid weld line issue Action on air bubble
  • 69. 6/25/2023 69 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 69 Before Material handling in bin with separator Material handling in bin with out separator After Action on part damage
  • 70. 6/25/2023 70 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 70 Before After No strip guide loader available Strip guide stand loader provide to continues feeding of rubber in feeder Action- Short Moulding
  • 71. 6/25/2023 71 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 71 Before After No grub screw provision in mould Grub screw provision provided in mould to balance rubber flow cavity wise Action on Short Moulding
  • 72. 6/25/2023 72 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 72 Before After Operator have to go behind the machine to check the rubber strip condition Convex mirror provided to check the rubber strip condition No before pic available Action- Short Moulding
  • 73. 6/25/2023 73 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 73 Before Process parameter freeze after validation HRTC temperature maintain b/w(40 ~50) which reduce the short moulding defect HRTC temperature not maintain After Action on short moulding
  • 74. 6/25/2023 74 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 74 Before Process parameter freeze after validation Cushion max 7.7 & min 0.7 fixed to reduce the short moulding defect. Cushion max 16.6 & min 0.7 After Action on short moulding
  • 75. 6/25/2023 75 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 75 36.95 7.47 3.5 5.5 4.5 3.5 3.1 2.8 2.7 2.5 0 5 10 15 20 25 30 35 40 FY 20-21 FY 21-22 FY 22-23 Apr-22 May-22 Jun-22 Jul-22 Aug-22 Sep-22 Oct-22 IWH – Rejection % Development Time Increased productivity by continuity machine . Earlier 626 No’s Now 1107 No’s Saving 481 no’s / day Monthly -12025 no’s
  • 76. 6/25/2023 76 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 76 Project 1 Excel based monitoring system for calibration Effective monitoring of calibration plan vs actual Meet the customer requirement Traceability of part. Project 2 QR code marking on part Project 3 Reduction in Electricity consumption. Saving of of 40,584 unit in PNG & 2,42 lacs Units in electricity Natural Resource saving Saving of 12 lacs rupees annually Natural Resource saving Project-4 Packaging recycling initiatives Learning / Take Away Project 5 Reduction in water consumption Saving of 34 lacs liters water annually Increase RHW capacity 16 lacs liters Natural Resource saving Production capacity increased. ( SPM 2.5 to SPM 3.5 ) Saving of 32,250 stroke monthly Project 6 Set up single piece flow line in heat shield Project 7 Capacity enhancement by optimization of plant layout Space Save of 1117.8 sq. meter Adding new machine in existing Skill upgradation of employee Project-8 Introduction of Jagriti 3 Project 9 Rejection reduction in riveting process Reduction of rejection from 98 no’s to zero. Reduction in rejection form 37 % to 3.5 % Increase the productivity at final inspection stage Monthly 12,025 no’s Project 10 Reduction in rejection in Injection molding -IWH
  • 77. 6/25/2023 77 ZERO DEFECT SUPPLIER REVIEW 6/25/2023 77 Thank You Zero Defect journey Continueâ€Ļ

Editor's Notes

  1. “Samay ki jalti silla ke upper sulag rhi a ek chingari , Sitam ki chaon me sir jukha kar kabhio jawani nhi kategi “ Good Morning First of all we would like to cordially thanks to KOEL team from entire Talbros family to have this wonder full and glorious opportunity to express our improvement journey towards the best business practices I am Sonu Tyagi taking care of customer support along with Mr Ajay Sharma taking care Corporate quality function.
  2. We are maintaining Zero Non conformance from Apr 22 to till now
  3. We have identified the Top 10 project from SDM sheet .
  4. We followed the DMAIC approach through all the project. It very difficult to monitor the huge no of calibration equipment via manual base work . So ,we developed and implement the Microsoft excel software to monitoring the calibration of equipment which give us the alarm at a certain frequency which help us to monitor the plan vs actual . Now , It is fully functional in the plant.
  5. We feel & respect earth & human beings are complementary, where earth gives us life and natural resources ,same time earth existence is also in our hand so we identified the project to move one step forward in direction of reduction of electrical energy resources, with the drive of this project.
  6. With the drive of this we saves 40,584 unit in PNG consumption & 2,42,112 Units in electricity consumption .
  7. Our management take the initiative to do the recycle of packaging. With the joint effort between customers and our management , we took the one step forward to save the natural resources.
  8. It is call of time to save the water on earth , “Pani nhi to jindgani nhi” With the project we take one more forward to save the natural resources.
  9. In our company we have batch production system, which having lot of gray area,
  10. We have added new customer in our basket so we have lot of challenges to meet the customer supply demand with in available resources. With the support of our management we changed the layout of our plant.
  11. Lets have a look the transition in our plant layout
  12. We have elaborate the training module in form of jagriti to upgrade the people skills to cascade the people quality in product quality ,
  13. Jagriti – basis topic , Jagriti 2- shop floor working topic, Jagrity- Quality focus topic , in upcoming slide there is glimpse of jagrti 3.
  14. This is new tech for us , this project we have identified under the Made in India campaign. This is we called integrated wire harness.
  15. We have done lot of exercise and find out the n no of possible cause through out the 1 year journey. We have taken the action on all possible cause .
  16. We have drastically reduce rejection after taking the counter measure on above possible causes. But hunger is still on.
  17. Kushi mili itni ke dilme nah samye Me palak band kr lun Kahi chalak hi nah jaye kahin chalak hi nah jaye. ek bar fir se talbros family ke taraf se yahan pe upasthit sabhi logo ka dil se dyanyewad deta hun. Anth mein mein bus ab ye hi khena chunga , ki ab mein kuch nhi kaung. Bahut bahut dynawad. Yug parivertan ka sanket hai Badlav ke sath apne apne ko intgrate karna behad jarurri hai