1. 6/25/2023 1
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 1
Talbros automotive component ltd. (FBD)
Mobile No: 9818682164
E-mail: ajay_sharma@talbros.com
Best Business Practice
Photo
Photo
Ajay Sharma
Corporate QA-Head
SonuTyagi
Customer Support
2. 6/25/2023 2
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 2
QMS Certification
with validity
Major Esteem Customers and KOEL Share of Business
in %
Family of Parts Manufactured
( Attach Photographs )
Future Business Plan Future Infrastructure Improvement
1. Adding new customer MSIL and Hyundai in heat shield segment. o Plant re-layout to increase the space .
o Extension of plant to increase capacity by adding new
power press for heat shield segment .
Photo Photo
QMS Certificate &
Date of Validity
Supplier Name: Talbros Automotive Components Ltd.
COMPANY PROFILE
TATA
CUMMINS
28%
HERO
23%
VOLVO
14%
TATA
MOTORS
13%
SIMPSON
3%
ASHOK
LEYLAND
2%
ESCORTS
2%
MSIL
2%
KO
Others
11.5%
TATA CUMMINS HERO
VOLVO TATA MOTORS
SIMPSON ASHOK LEYLAND
ESCORTS MSIL
KOEL Others
Date of Certification: 19 Jan â2022
Date of expiration: 18 Janâ 2025
4. 6/25/2023 4
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 4
MANUFACTURING PROCESS MAPPING THROUGH TURTLE DIAGRAM / VDA FMEA
NUMBEROF PROCESS
MAPPED/ TOTAL
PROCESS
NUMBEROF PROJECTS IDENTIFIED IN THE EACH ELEMENT OF THE TURTLE
INPUT
INFRA. &
MEASR
PROCESS RISKS
INVOLVED
PROCESS OWNER
COMPETENCY
PROCESS
DOC./ REC
PROCESS
EFFI./ EFFE
TOTAL
14 (Nos.) / 20 (Nos.)
0 (Nos.) 11 (Nos.) 5 (Nos.) 1 (Nos.) 2 (Nos.) 0 (Nos.) 19 (Nos.)
BUSINESS PROCESS MAPPING THROUGH TURTLE DIAGRAM / VDA FMEA
NUMBEROF PROCESS
MAPPED/ TOTAL
PROCESS
NUMBEROF PROJECTS IDENTIFIED IN THE EACH ELEMENTOF THE TURTLE
INPUT
INFRA. &
MEASR
PROCESS
RISKS
INVOLVED
PROCESS
OWNER
COMPETENCY
PROCESS
DOC./ REC
PROCESS
EFFI./ EFFE
TOTAL
9 (Nos.) / 41 (Nos.)
2 (Nos.) 9 (Nos.) 4 (Nos.) 2 (Nos.) 6 (Nos.) (Nos.) 23 (Nos.)
IMPROVEMENT PROJECTS IDENTIFIED OTHER THAN ABOVE TWO METHODOLOGIES
NUMBEROF PROJECTS IDENTIFIED IN THE LISTED BELOW
Composite Score Customer Feedback Other( Specify if any)
2 (Nos.) (Nos.) (Nos.)
5. 6/25/2023 5
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 5
SERIAL
NUMBER
PROJECT DESCRIPTION
PROJECT BELONGS TO
WHICH PROCESS
PROJECT
RATING FROM
SDM SHEET
IMPACTON
NUMBER OF
PROCESS
COMPLETION
STATUS
1 Excel based monitoring system for calibration Business Process 265 1
2 QR code marking on part. Business Process 165 1
3 Energy (Electricity) consumption reduction Business Process 174 1
4 Packaging recycling initiatives -Returnable packaging Business Process 174 1
5 Reduction in water consumption Business Process 174 1
6 Set up single piece flow line in heat shield Business Process 308 1
7 Capacity enhancement by optimization of plant layout Business Process 148 1
8 Quality specific skill upgradation through Jagriti- Volume-3 Business Process 240 1
9 Rejection reduction in riveting process Manufacturing Process 170 1
10 Reduction in rejection Injection molding âIWH ( New Tech.) Manufacturing Process 153 1
6. 6/25/2023 6
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 6
īąDefine
ī Calibration due was being monitored in hard copy may cause non adherence of the
calibration schedule.
īąMeasure
ī Approx. 700 noâs equipment calibration process review is difficult to monitor by
manually method , which may lead to non-adherence of the calibration schedule.
īą Analyze
ī Alarming system is required to make alert before scheduled calibration date.
īąImprovement
ī We have made conditional formatting in excel that give us alarm in following manner-
1. If calibration due date is less than 30 â Green signal will turn on
2. If calibration due date is less than 2weeks â Yellow light will turn on
3. If calibration due date is less than 1 week - Red light will turn on
īControl
ī Regular monitoring to review the calibration Plan vs actual via Formatting based excel
sheet.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
BEFORE
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
AFTER
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- Aprâ 22
âĸ Cut of Date: Aprâ 22
RESULT YES / NO
Productivity Improvement
System Improvement :
Quality Improvement :
Environment & Safety:
Moral:
Name of Process: Calibration- Business Process
Project Title -Excel based monitoring system for calibration
8. 6/25/2023 8
ZERO DEFECT SUPPLIER REVIEW
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Name of Process: CSR & Composite Score Business Process
īąDefine
ī Implementation of QR code as it is requirement of customer , compliance
requirement of composite score sheet .
īąMeasure
ī Identify the customer requirements for traceability by QR code.
īąAnalyze
ī We have identify the part list where we can implement the QR code requirement.
īąImprovement
ī QR code implement in gasket for traceability to meet the customer requirement.
īąControl
ī Updating the relevant document â Control plan , Drawing etc.
ī Also upgrade the machine and installed the scanner to read the QR code to ensure
the readability of QR code 100 %
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- July â22
âĸ Cut of Date: Continuous
RESULT YES / NO
Productivity Improvement
CSR â QualityImprovement:
Cost Reduction (Yearly) :
Environment& Safety:
Moral:
BEFORE
AFTER
Name of Process: CSR & Composite Score- Business Process
Project Description-QR code marking on part.
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Before After
12 12
0
2
4
6
8
10
12
14
Part Identified QR code implement
Out of 12 QR code
implement parts one
part is for KOEL
âGP-3 Model â
10. 6/25/2023 10
ZERO DEFECT SUPPLIER REVIEW
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Name of Process: ISO 45001 & ISO 14001-EHS Business Process
īąDefine
ī Initiative has been taken to reduce the electricity consumption to save electricity.
īąMeasure
ī Data collected of previous year consumption of electricity.
īąAnalyze
ī Brain storming done to identify the gaps and new initiative decided to reduce the
consumption of electricity.
īąImprovement
ī Individual heat exchangers installed in on all batch ovens to reduce the PNG
consumption
ī Old ACs replaced with new ones having R32 gas low power consumption and ozone
free depletion safe
ī Cooling tower water PHE connected in circuit of MTC & chiller water line to reduce
the power consumption
ī Switch off when not in used campaign.
īąControl
ī We have linked the initiative with company objective of EHS for monitoring.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- Apr â22
âĸ Cut of Date: Continuous
RESULT YES / NO
Productivity Improvement
QualityImprovement:
Cost Reduction (Yearly) :
Environment& Safety:
Moral:
BEFORE
AFTER
Project Description-Reduce the consumption of electricity energy
Name of Process: -EHS- Business Process
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Name of Process: Packing Business Process
īąDefine
ī Reduction in wooden pallet & carton for packaging and transportation of parts to save
the natural resources.
īąMeasure
ī Initiative has been taken to reduce the consumption of wooden pallet and carton for
packaging and transportation of material.
īąAnalyze
ī Wastage of natural resources.
ī Space required for storage of wooden pallets.
ī Damage during transportation need to scrap after few supply.
īąImprovement
ī Implementation of returnable bins against the wooden pallets / Carton.
īąControl
ī Sign the PSDS with customer to make it part of system.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Environment & Safety:
Moral:
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- May 22
âĸ Cut of Date: Continue process
BEFORE
AFTER
Project Description-Packaging Initiatives.
Name of Process: Packing- Business Process
13. 6/25/2023 13
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Before After
Part identified
for Returnable
packaging
instead of
wooden block
Returnable bins
implemented in
new projects
12 Lacs
Rupees
saving
14. 6/25/2023 14
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īąDefine
ī Wastage of natural resources, Initiative has been taken to save the water.
īąMeasure
ī Collect the data and measure the wastage of water after RO, and STP treatment .
īąAnalyze
ī Analysis the gap and find the new initiative to save the water.
īąImprovement
ī Wastage of RO water use in toilet flushing.
ī STP treatment water used in gardening.
ī Increase capacity of rain water harvesting to save water.
īąControl
ī Linked with department MP under the EHS standard.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
QualityImprovement:
Cost Reduction (Yearly) :
Environment& Safety:
Moral:
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- Apr â21
âĸ Cut of Date: Marchâ22
BEFORE
AFTER
Project Description- Reduction in water consumption
Name of Process: -EHS- Business Process
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0
3,432,000 3,432,000
0
1000000
2000000
3000000
4000000
FY 2021-22 FY 2022-23 FY 2022-23-
Saving
34.5 Lacs litre
water saving
annually
Reduction in Water Consumption- Litres
1
2 2
-
-
1
1
2
2
3
FY 2020-21 FY 2021-22 FY 2022-23
Increase the capacity of Rain water harvesting well âNoâs
Total Capacity
of RHW is 16
Lakhs litres.
16. 6/25/2023 16
ZERO DEFECT SUPPLIER REVIEW
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īąDefine
ī We are having batch production system resulting space required for storage of WIP
of material.
īąMeasure
ī We have measured that we are consuming 100 sq ft area for WIP of batch
production.
īąAnalyze
ī Due to batch production following hurdle were observed .
ī§ 100 sq ft area used
ī§ Operator fatigue was more.
ī§ No. of trolley is required keep the material.
ī§ Non adherence of 5S.
īąImprovement
ī Set up a single piece flow lline.
ī Reduce the operator fatigue.
ī Reduce the die changeover time, reduction in material handling time.
ī Save no. of bins/ trolleys of storage of material.
ī Reduction in mix of process part, reduce the rejection risk.
ī Production capacity increased. ( SPM 2.5 to SPM 3.5 ) increase stroke in per day is
1280 Noâs , Monthly -32,250 Noâs.
īąControl
ī Conveyor belt setup done between the machine to flow the single part flow .
ī Balancing the line according to operation and set up done for single piece flow.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Saving of Area
Moral:
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- Jun â22
âĸ Cut of Date: Junâ 22
BEFORE
AFTER
Project Description-Set up single piece flow line in heat shield
Name of Process: Continual Improvement- Business Process
SPM increased
2.5 to 3.5
Stroke saving
32,250 monthly
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ZERO DEFECT SUPPLIER REVIEW
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īąDefine
ī Space constraint in shop floor area.
ī 5âS not adhere.
īąMeasure
ī Layout review and D2D approach.
ī Adding new customers in basket.
ī New machine need to installed to enhance the capacity
īąAnalyze
ī Need to change existing layout for space optimization.
īąImprovement
ī Plant layout changed & improved the 5âS.
ī Mezzanine concept implement in FGS area.
ī 200 Ton three new machine added in existing area.
ī 3 Noâs new riveting machine added in existing area.
ī Synchronize the Heat shield process.
ī Centralize the all inspection and packing area under one roof.
īąControl
ī All the changes incorporated in plant layout.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Environment & Safety:
Space capacity :
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- Dec â21
âĸ Cut of Date: Oct 22
BEFORE
AFTER
Space
Save
1117.8 sq.
meter
Project Description-Capacity enhancement by optimization of plant layout
Name of Process: Plant Layout-Business Process
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âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- Septâ 22
âĸ Cut of Date:-Septâ22
īąDefine
ī To escalating the human skill up to next level & meeting the customer expectations
quality related module is not available
īąMeasure
ī As per customer expectations it observed that quality specific training module is not
available
īąAnalyze
ī Theoretical understanding of the operators /inspectors are not so good related to
instruments or other concepts like RBA, OEE, LPA..
īąImprovement
ī We have drafted Jagriti Volume-3 specific to the quality function requirements
ī Control
ī No of trained operators/inspectors
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
RESULT YES / NO
Productivity Improvement
Quality Improvement :
Cost Reduction (Yearly) :
Environment & Safety:
Moral:
BEFORE
AFTER
Project Description-Quality specific skill upgradation through Jagriti-3
Name of Process: Human Resource- Business Process
38. 6/25/2023 38
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Jagriti-01
īļ Product Knowledge
īļ Type of Defect
īļ Failure of Gasket
īļ 5S
īļ 3M
īļ Rules Of Factory
Jagriti-02
īļ Introduction of shop floor
īļ Type of machine
īļ Handling of abnormal situation
īļ Work order
īļ SOP- All process
īļ Check sheet
īļ Type of Gasket
Jagriti-03
īļ Knowledge of Quality
Instrument
īļ Set Up approval
īļ RCA
īļ Shift Handover
īļ RBA
īļ LPA
īļ Kaizen
īļ Type of breakdown
īļ PPM
īļ OEE
49. 6/25/2023 49
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īąDefine
ī Caution mark fitment in wrong direction and assembly more than one caution
mark on one heat shield.
īąMeasure
ī Data collection done from red bin analysis.
īą Analyze
ī Due to child part assembly our whole part get rejected which cost is much higher
than the child part.
īąImprovement
ī Vision Poka Yoke add in machine which prevent the wrong direction of caution mark .
ī Shooting panel provided in machine to prevent the assembly of two child part at a
same time.
īControl
ī Check point added in process check sheet for verification of Poka Yoke.
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
BEFORE
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
AFTER
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- May â22
âĸ Cut of Date: May â22
RESULT YES / NO
Productivity Improvement
System Improvement :
Quality Improvement :
Environment & Safety:
Moral:
98
41
26 25
6 0 0 0 0 0
0
20
40
60
80
100
2022
Jan-22
Feb-22
Mar-22
Apr-22
May-22
Jun-22
Jul-22
Aug-22
Sep-22
Before After
Project Title âRejection reduction in riveting process
Name of Process: Riveting Process- Manufacturing Process
50. 6/25/2023 50
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 50
īąDefine
ī Huge rejection in Injection molding.
īąMeasure
ī Data collection done from red bin analysis.
īą Analyze
ī Brainstorming done to identified related tool & machine during RBA
īąImprovement
ī Huge reduction in rejection form 37 % to 3.5 %
ī Increase the productivity in final inspection. ( Current cycle time is 1.30 min earlier it
was 2.30 min ) with automated recording of reports in system itself.
īControl
ī All the identified gaps updated in concern documents & same have been adhered
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
BEFORE
Input
Infrastructure
resource
Risk
Involved in
process
Process owner
competency
Process
documents &
records
Process
efficiency &
effectivenes
s
AFTER
âĸ Tool Used: DMAIC & Turtle diagram
âĸ Project Start:- Jan â21
âĸ Cut of Date: Continue Process
RESULT YES / NO
Productivity Improvement
System Improvement :
Quality Improvement :
Environment & Safety:
Moral:
Project Title âReduction in rejection of Injection molding âIWH ( New Tech.)
Name of Process: Injection Molding- Manufacturing Process
52. 6/25/2023 52
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 52
Cable Cut
Loose tie
Continuity
Failure
Wrong QR code
Leakage on wire
Carrier Crack
Air bubble
Part damage
Short Moulding
Man Machine
Material
Method
Unskilled Operator
Manual cutting of tie.
Tie Cutting length not fixed
Manual process tie fastening. Tie cutting method not define
Tie location not define
Un aware about the continuity process ( Nut to Nut & Nut to terminal )
Resistance test not define in SOP
Part resistance test method not define
Manual test of Continuity
Manual process of application
Nut rotation check point not added in SOP
Nut rotation check point not added in SOP
No inspection at Receipt stage
Wire cut generated in parts during deflashing , due to routing of wire done before
deflashing
Wire locking provision not provide in tool
Pillar length of tool is more .
Sharp edges & Play in magnet clamp
Wrong method of wire bundling during taping
Material leakage on wire due to Mould temp high
Material leakage on wire due to Cushion high
Raw Material Not proper pre-heating due to material
not loading In hopper simultaneously
Mould design and terminal pin design not
compatible
Wire cut from supplier end
Wire insulation material degrade
Insulation Thickness less
ML lower side
Rheo gates not validated
Expired chemlok used
Rubber High Hardness
Nut cage & thimble sharp edges
Material Not proper pre-heating
Unskilled for tie operation
Operator not aware about the SOP
Brain storming & Root Cause Analysis
53. 6/25/2023 53
ZERO DEFECT SUPPLIER REVIEW
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Before After
No extra guide lock available for wire routing Extra guide locking provided in tool
Action on wire cut
54. 6/25/2023 54
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 54
Before
Tool design improved
Sharp edge in insert
After
Action on wire cut
55. 6/25/2023 55
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 55
Before After
Action on wire cut
L Type support provided in mould
No support
56. 6/25/2023 56
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 56
Before
Wire cut generating during deflashing due to
Flash generated near to wire area moulding
process
After
Mould design improved
Action On Wire cut
57. 6/25/2023 57
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 57
Before After
Cutter used for extra flash removing Flashes removal method changed
Action on wire cut
58. 6/25/2023 58
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 58
Before
Correct wire taping method developed
Wrong method of wire Taping âif wire stretch in
this condition then wire cut will generate in part
After
Action on wire cut
59. 6/25/2023 59
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 59
Before After
Manual cutter
Tie cutter gun provided instead of manual
cutter
Action on tie loose / cut
60. 6/25/2023 60
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 60
Before After
Wire wound over the sharp edges of plastic
carrier
Method developed ,no wire routing over the
sharp edges of plastic carrier.
Action on wire cut in routing process
61. 6/25/2023 61
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 61
Before After
Material Loading in hopper manually
Material loader provided in carrier injection
moulding
Action on leakage of wire
62. 6/25/2023 62
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 62
Before After
Buzzer not available Buzzer provided for spray frequency Adherence
NA
Action on Rubber cut in injection Moulding
63. 6/25/2023 63
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 63
Installation of continuity testing machine
Continuity machine installed to check the continuity earlier
manual method used
Inspection Cycle time
Cycle time earlier â 2.3 min
Now cycle time -1.3 min
64. 6/25/2023 64
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 64
Wrong QR code on gasket â Install leakage testing machine linkage with QR code.
1-Barcode Printer interlink with system after ok result from machine QR code print
2.To avoid wrong barcode printing Make model wise program & sensor mounting
65. 6/25/2023 65
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 65
BEFORE AFTER
Adhesive applied on terminal without fixture
Fixture made for application of chemlok on
terminal pin which is cover 75 % area of pin ,
earlier brush was used which cover 100 % area
of pin which leads continuity issue
100%
Action On Continuity Issue
66. 6/25/2023 66
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 66
Before After
No provision of holding part in mould Part holding provision added in mould
Action on crack in carrier
67. 6/25/2023 67
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 67
Before After
Lock crack due to no clearance in mould during
butting
Chamfer provided in mould
Action on Crack Issue
68. 6/25/2023 68
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 68
Before After
No chrome plating on mould that create weld
line
Chrome Plating provided in mould to avoid weld
line issue
Action on air bubble
69. 6/25/2023 69
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 69
Before
Material handling in bin with separator
Material handling in bin with out separator
After
Action on part damage
70. 6/25/2023 70
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 70
Before After
No strip guide loader available
Strip guide stand loader provide to continues
feeding of rubber in feeder
Action- Short Moulding
71. 6/25/2023 71
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 71
Before After
No grub screw provision in mould
Grub screw provision provided in mould to
balance rubber flow cavity wise
Action on Short Moulding
72. 6/25/2023 72
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 72
Before After
Operator have to go behind the machine to
check the rubber strip condition
Convex mirror provided to check the rubber
strip condition
No before pic available
Action- Short Moulding
73. 6/25/2023 73
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 73
Before
Process parameter freeze after validation
HRTC temperature maintain b/w(40 ~50) which
reduce the short moulding defect
HRTC temperature not maintain
After
Action on short moulding
74. 6/25/2023 74
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 74
Before
Process parameter freeze after validation
Cushion max 7.7 & min 0.7 fixed to reduce the
short moulding defect.
Cushion max 16.6 & min 0.7
After
Action on short moulding
76. 6/25/2023 76
ZERO DEFECT SUPPLIER REVIEW
6/25/2023 76
Project 1
Excel based
monitoring
system for
calibration
Effective
monitoring of
calibration
plan vs actual
Meet the
customer
requirement
Traceability of
part.
Project 2
QR code
marking on
part
Project 3
Reduction in
Electricity
consumption.
Saving of of
40,584 unit in
PNG & 2,42
lacs Units in
electricity
Natural
Resource
saving
Saving of 12
lacs rupees
annually
Natural
Resource
saving
Project-4
Packaging
recycling
initiatives
Learning / Take Away
Project 5
Reduction in
water
consumption
Saving of 34
lacs liters
water
annually
Increase RHW
capacity 16
lacs liters
Natural
Resource
saving
Production
capacity
increased.
( SPM 2.5 to
SPM 3.5 )
Saving of
32,250 stroke
monthly
Project 6
Set up single
piece flow line
in heat shield
Project 7
Capacity
enhancement by
optimization of
plant layout
Space Save of
1117.8 sq.
meter
Adding new
machine in
existing
Skill
upgradation of
employee
Project-8
Introduction
of Jagriti 3
Project 9
Rejection
reduction in
riveting
process
Reduction of
rejection from
98 noâs to
zero.
Reduction in
rejection form
37 % to 3.5 %
Increase the
productivity at
final
inspection
stage
Monthly
12,025 noâs
Project 10
Reduction in
rejection in
Injection
molding -IWH
âSamay ki jalti silla ke upper
sulag rhi a ek chingari ,
Sitam ki chaon me sir jukha kar kabhio jawani nhi kategi â
Good Morning
First of all we would like to cordially thanks to KOEL team from entire Talbros family to have this wonder full and glorious opportunity to express our improvement journey towards the best business practices
I am Sonu Tyagi taking care of customer support along with Mr Ajay Sharma taking care Corporate quality function.
We are maintaining Zero Non conformance from Apr 22 to till now
We have identified the Top 10 project from SDM sheet .
We followed the DMAIC approach through all the project.
It very difficult to monitor the huge no of calibration equipment via manual base work .
So ,we developed and implement the Microsoft excel software to monitoring the calibration of equipment which give us the alarm at a certain frequency which help us to monitor the plan vs actual .
Now , It is fully functional in the plant.
We feel & respect earth & human beings are complementary, where earth gives us life and natural resources ,same time earth existence is also in our hand so we identified the project to move one step forward in direction of reduction of electrical energy resources, with the drive of this project.
With the drive of this we saves 40,584 unit in PNG consumption & 2,42,112 Units in electricity consumption .
Our management take the initiative to do the recycle of packaging.
With the joint effort between customers and our management , we took the one step forward to save the natural resources.
It is call of time to save the water on earth , âPani nhi to jindgani nhiâ
With the project we take one more forward to save the natural resources.
In our company we have batch production system, which having lot of gray area,
We have added new customer in our basket so we have lot of challenges to meet the customer supply demand with in available resources. With the support of our management we changed the layout of our plant.
Lets have a look the transition in our plant layout
We have elaborate the training module in form of jagriti to upgrade the people skills to cascade the people quality in product quality ,
Jagriti â basis topic , Jagriti 2- shop floor working topic, Jagrity- Quality focus topic , in upcoming slide there is glimpse of jagrti 3.
This is new tech for us , this project we have identified under the Made in India campaign.
This is we called integrated wire harness.
We have done lot of exercise and find out the n no of possible cause through out the 1 year journey. We have taken the action on all possible cause .
We have drastically reduce rejection after taking the counter measure on above possible causes. But hunger is still on.
Kushi mili itni ke dilme nah samye
Me palak band kr lun
Kahi chalak hi nah jaye kahin chalak hi nah jaye.
ek bar fir se talbros family ke taraf se yahan pe upasthit sabhi logo ka dil se dyanyewad deta hun.
Anth mein mein bus ab ye hi khena chunga , ki ab mein kuch nhi kaung. Bahut bahut dynawad.
Yug parivertan ka sanket hai
Badlav ke sath apne apne ko intgrate karna behad jarurri hai