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QUALITY CIRCLE PRESENTATION
18/11/2022
Team Members:
PRODUCTIVITY IMPROVEMENT IN REC BANDED BELT
GRINDING MACHINE
 Mr. N.Karthik – Technology & Development
 Mr. Rajasekaran – REC Manufacturing  Mr. L.Raja- Engineering Department
 Mr. G.Rajesh – Technical Department
Trail
Implemen
-tation
QUALITY
CIRCLE
Identification
of
Problem
Select the
Problem
Understand
the
Problem
Problem
Analysis
Identify
possible
Causes
Root cause
Analysis
Data
Analysis
Developing
Solutions
Foreseeing
Probable
Resistance
Regular
Implementa
-tion
Follow up/
Review
1
2
3
4
5
12
11
10
9
8
7 6
METHODOLOGY
STEP - 1
1
IDENTIFICATION OF PROBLEM
STEP-1
IDENTIFICATION OF WORK RELATED PROBLEM
Problem Statement
 Machine adherence: Delivery adherence is poor
 Rework is greater than 40% of actual coding value.
 Asset utilization: Cycle time is high compare to Vertical grinding machine.
 To meet the budgeted value of 2022-2023 and create capacity to failure
0
1000
2000
3000
4000
5000
6000
Qty
in
Nos.
Oct-21 Nov-21 Dec-21 Jan-22 Feb-22 Mar-22
Supply 2500 2500 2862 2132 4041 3633
Demand 3500 3500 4000 3000 5000 5000
Demand Vs Supply of Banded belt
Supply Demand
STEP - 2
1
SELECTION OF PROBLEM
STEP – 2
SELECTION OF PROBLEM
Phase 1: Machine Throughput to be increase- Machine Parameters record, Machine actual
mode, Rework is high : Target : 35 % - 0% for CX & SPCX section
Phase 2: Cycle time improvement for different varieties: Target : 35 % by 2022 – 23
Phase 3: Horizontal deployment of improvements in other grinding machines
PHASE 1: REWORK TO BE REDUCE AND
ELIMINATE
35
0
0
40
Rework
Percentage
REWORK-CX Section
Existing Target
PHASE 2: CYCLE TIME REDUCTION
Target: 30%
903
589
0
150
300
450
600
750
900
1050
Cycle
time
in
CX
CYCLE TIME
Existing Target
TARGET
STEP - 3
1
DEFINE THE PROBLEM
STEP – 3
DEFINE THE PROBLEM
1) Unable to achieve the current
customer demand of 60000 / annum
where our current productivity is
13000 belts per annum.
2) High rework generation: 35%
STEP – 4
1
ANALYSE THE PROBLEM
STEP – 4
ANALYSE THE PROBLEM
High cycle time and
Rework
WHAT is the problem?
WHERE does this problem
occur ?
Grinding Process
WHEN does it occur ? During grinding operation
WHO notices this problem ? Production department
HOW can solve this problem ?
By study and improving the
Grinding Methodology
BRAINSTROMING
01
02
03
04
05
06
0
7
08
09
10
Coupling
Lock
system
Nuts can be
removed using
Wrench
Hand wheel
elimination
Grinding
wheel Setup
change time
Dead weight
arrangement: Stroke
Grinding
wheel speed
Pressure pad
Alignment
Horizontal grinding m/c
to Profile grinding m/c
Pulley alignment to be
perfect
Cycle time
of grinding
STEP – 5
1
IDENTIFCIATION OF CAUSES
STEP – 5
IDENTIFCIATION OF CAUSES
BRAINSTORMING POINTS SPECIFICATION IMPROVEMENT PLANNED RESULT
Coupling lock system Locking made on separate link Found Ok Insignificant
Cycle time in Grinding Cycle time– 903 Seconds
Grinding time can be
optimized
Significant
Pressure pad Alignment
All groove OD in pressure pad
to be equal size
Groove OD to be turned to
required size
Significant
Grinding wheel Setup change time
Setup changeover time: 12 mins
avg
Reasonable time Insignificant
Hand wheel elimination Belt Tensioning time: 33s
Time can optimize with
automated mechanism
Significant
Pulley alignment to be perfect
Pulley and belt seating area to
be align
Found Ok Insignificant
Nuts can be removed using Auto
Wrench
Using manual wrenches nut
removal happening
Found Ok Insignificant
Dead weight arrangement: Stroke
length
Stroke length of shaft: 200mm
Can be increase to some
range
Significant
Horizontal m/c to Profile grinding
machine
Loading belts in current setup
for grinding
To overcome order quantity
utilizing the asset
Significant
Grinding wheel speed Speed: 1390 rpm Reached maximum capacity Insignificant
STEP – 6
1
FINDING OUT THE ROOT CAUSES
STEP – 6 FINDING OUT THE ROOT CAUSES
( Why)
( Why)
COUNTER MEASURE Throughput improvement
Delay in belt delivery
High cycle time and Belt
Rework generation
Improper Pressure pad/More
number of grinding steps
( Why)
Existing method
WHY WHY ANALYSIS
STEP – 7
1
DATA ANALYSIS
STEP – 7: DATA ANALYSIS
1000.00
350.00
0
2000
Jul-22 Aug-
22
Sep-
22
Oct-
22
Nov-
22
Plan
Avg.
Belt
Numbers
Qty
REC Grinding m/c– ProductionTrend
Avg
G.W Motor Rating Kw 15 Drive pulley dia 148 mm
Maximum Load
Calculated
Amps 26 Drive Pulley RPM 134 rpm
Motor reduction 1:1 Belt linear speed 62.30 m/min
GW. Speed rpm 1390 Direction of rotation Clockwise
G.W dia mm 138
Pressure pad linear
speed
0.04 mm/sec
G.W. linear speed m/min 603
Belt Sec: CX 85 2159 Profile Banded
Top width 21.7 mm GW 1664.2 603m/min
Thickness 14.8 mm Anvil 1.92 62.30m/min
Belt Sec: Diff speed 865.3 9.7
0.001 0.103
Step
Depth
Area of material
removal
Belt Contact
with grinding
wheel
Grinding
wheel
temperature
Load Time - secs
Belt
rotation
mm Sq.mm mm deg C
Amps Pr.Pad
movement
Dwell
time
Step
Time
Nos
Min Max
Loading Time 33
Grinding
1 2.0 1.4 2.1 34.1 6.4 7.3 50.0 44.4 94 45.40
2 2.0 8.4 4.3 46.7 6.5 7.1 50.0 44.4 94 45.40
3 1.5 9.2 5.9 57.3 7.0 8.1 37.5 44.4 82 39.39
4 1.5 6.8 7.4 72.9 7.9 9.8 37.5 44.4 82 39.39
5 1.0 5.4 8.5 95.4 8.9 11.2 25.0 44.4 69 33.38
6 1.0 6.0 9.6 107.0 9.4 12.2 25.0 44.4 69 33.38
7 0.8 5.4 10.4 122.4 11.8 12.9 20.0 44.4 64 30.97
8 0.8 5.9 11.3 124.1 10.9 15.0 20.0 44.4 64 30.97
9 0.8 6.4 12.1 127.5 11.1 15.2 20.0 44.4 64 30.97
10 0.6 5.1 12.8 146.3 11.0 15.2 15.0 44.4 59 28.57
11 0.5 4.4 13.3 145.1 10.7 11.7 12.5 44.4 57 27.37
Auto run - Deburring 43 20.68
Unloading 16
12.5 64.4 312.5 488.4 893 405.86
STEP – 8
1
DEVELOPING SOLUTION
STEP – 8: DEVELOPING SOLUTION
Act.
No
ACTIVITY
Cycle Time in
Secs
(Existing)
1
Setting the parameters in
HMI 10
2 Belt Loading Time 20
3
Closing the lid and press
RUN in HMI 3
4 Step 1-2 95
5 Step 2-3 92
6 Step 3-4 79
7 Step 4-5 79
8 Step 5-6 66
9 Step 6-7 69
10 Step 7-8 62
11 Step 8-9 62
12 Step 9-10 61
13 Step 10-11 60
14 Step 11- 12 51
15 Step 12-Grinding complete 35
16 Reversal-End 43
17 Unloading Time 16
Cycle time, seconds 903
HORIZONTAL GRINDING MACHINE
STEP – 8: DEVELOPING SOLUTION
BEFORE AFTER
HAND WHEEL
 Belts are Loaded in machine and belt
tension given to belt with hand wheel for 4
belts.
 Cycle time 33 secs
 Simple mechanism provided by eliminating
the hand wheel with Motor mechanism-Easy
tensioning.
 Cycle time 3 Sec
Simplify
Action : 1 HAND WHEEL ELIMINATION
STEP – 8: DEVELOPING SOLUTION
KAIZEN IDEA - SHEET
STEP – 8: DEVELOPING SOLUTION
BEFORE AFTER
Stroke length
increased to
meet the
correct Belt
Tension
 The dead weight is not arranged properly
 Tension variation is high due to stroke
length deviation
 Dead weight- 240 Kg
Action : 2 DEAD WEIGHT ARRANGEMENT: STROKE LENGTH
STEP – 8: DEVELOPING SOLUTION
BEFOR
E
AFTE
R
Equal
surface
achieved
Tape
removed
AFTER
BELT CODING NOT OK
BELT CODING OK
BEFORE
35% THROUGHPUT
IMPROVED
Action : 3 UNEVEN PRESSURE PAD
RESULT IMPACT: THROUGHPUT IMPROVEMENT
STEP – 8: DEVELOPING SOLUTION
Action : 4 REDUCTION IN GRINDING STEPS
35% Reduction time for Target, From 903 Sec to 589 Sec – Reduction 314 Sec.
The Reduction plan is based on idea generation in brain storming points identified through SCAMPER
approach
VA – Value
Added Activity,
NVA –Non Value
Added Activities
Act. No. Activities
Actual
Time taken
(sec)
Time
Reduction
plan(Sec)
Saving
time in
(Sec)
Category
VA NVA
4 Grinding Step 1-2 95 94 1
1
5 Grinding Step 2-3 92 86 6
6 Grinding Step 3-4 79 70 9
7 Grinding Step 4-5 79 66 13
8 Grinding Step 5-6 66 62 4
9 Grinding Step 6-7 69 60 9
10 Grinding Step 7-8 62 55 7
11 Grinding Step 8-9 62 0 62
12 Grinding Step 9-10 61 0 61
13 Grinding Step 10-11 60 0 60
14 Grinding Step 11- 12 51 0 51
16 Reversal-End 43 22 21
2
15 Grinding Step 12-Grinding complete 35 55 -20
17 Belt Unloading Time 16 3 13 3
2 Belt Loading time 20 3 17 4
1 Setting parameters in HMI 10 10 0 5
3
Closing the lid and press RUN in
HMI
3 3 0 6
Total time in secs 903 589 314
90%
10%
VA NVA
STEP – 8: DEVELOPING SOLUTION
BEFORE AFTER
AFTER
Step Depth Step Grinding time
1 2.6 1-2 94
2 2.5 2-3 86
3 1.8 3-4 70
4 1.5 4-5 66
5 1.2 5-6 62
6 1 6-7 60
7 0.8 7-8 55
8 0.5 8-Grinding completed 55
Depth 12.5 Reversal-End 22
Total Grinding time (AFTER) 570
GRINDING MATERIAL REMOVAL
SIMULATION STUDY
BEFORE
Step Depth Step Grinding tme
1 2.0 1-2 95
2 2.0 2-3 92
3 1.5 3-4 79
4 1.5 4-5 79
5 1.0 5-6 66
6 1.0 6-7 69
7 0.8 7-8 62
8 0.8 8-9 62
9 0.8 9-10 61
10 0.6 10-11 60
11 0.5 11-Grinding completed 51
Depth 12.5 Reversal-End 35
Total Grinding time (BEFORE) 854
Action : 4 REDUCTION IN GRINDING STEPS
STEP – 9
1
FORSEEING PROBLEM OF RESISTANCE
STEP – 9 FORSEEING PROBLEM OF RESISTANCE
Sl.
No
Implemented actions Resistance
Raised
by
Corrective
actions
Status
1 Hand wheel elimination Hand wheel -
Introduced motor
mechanism
Completed and
implemented
2 Rework elimination Pressure pad -
Even Surface finish
achieved through
lathe operation
Completed and
implemented
actions are
followed
3 Stroke length Adjustment Dead weight -
Stroke length
increased to meet the
correct belt tension
Completed and
implemented
actions are
followed
4
Grinding steps reduced
for CX section
More steps in
grinding
-
Performed Load and
temperature study
and reduced the
grinding steps
Completed and
implemented
actions are
followed
STEP – 10
1
TRAIL IMPLEMENTATION & CHECK PERFORMANCE
STEP – 10
TRAIL IMPLEMENTATION & CHECK PERFORMANCE
After
Act.No ACTIVITY
CycleTime in
Secs (Existing)
1 Setting the parameters in HMI 10
2 Belt Loading Time 20
3
Closing the lid and press RUN in
HMI 03
4 Step 1-2 94
5 Step 2-3 86
6 Step 3-4 70
7 Step 4-5 66
8 Step 5-6 62
9 Step 6-7 60
10 Step 7-8 55
11 Step 8-9 0
12 Step 9-10 0
13 Step 10-11 0
14 Step 11- 12 0
15 Step 12-Grinding complete 55
16 Reversal-End 22
17 Unloading Time 03
Cycle time, seconds 589
STEP – 10
TRAIL IMPLEMENTATION & CHECK PERFORMANCE
S.No Activities
Before
(In
Secs)
After
(In
Secs)
%Reduction
in time
Action taken
1 VA 854 570 33.25%
1. Pressure pad outer diameter turned
to achieve even surface
2. Stroke length increased with simple
mechanism to withstand the dead
weight in proper way
3. Introduced Load, frequency meter
and modified the rpm. Performed
temperature simulation study on
machine
2 RNVA 49 19 61.22%
Introduced Motor feed mechanism by
eliminating manual hand wheel
operation
Total
time in
secs
903 589 34.78%
95%
5%
VA RNVA
97%
3%
VA RNVA
BEFORE CYCLETIME
AFTER CYCLETIME
STEP – 11: REGULAR IMPLEMENTATION
1
REGULAR IMPLEMENTATION
NO DEFECT - NO WASTE - NO DELAY
STEP – 11
REGULAR IMPLEMENTATION
Results
1000.00
1080.00
0
200
400
600
800
1000
1200
1400
Jun-22 Jul-22 Aug-22 Sep-22 Oct-22 Plan Avg.
Belt
Numbers
Qty
REC Grinding m/c– ProductionTrend Avg Plan Actual
PHASE 1: REWORK ELIMINATED
35
0
0
40
Rework
Percentage
REWORK-CX Section
Existing Target
PHASE 2: CYCLE TIME REDUCTION
Achieved: 35%
903
589
0
150
300
450
600
750
900
1050
Cycle
time
in
CX
CYCLE TIME
Existing Target
STEP – 11
REGULAR IMPLEMENTATION
P - PRODUCTIVITY
Q - QUALITY
C - COST
D - DELIVERY
S - SAFETY
M - MORALE
Achieved the daily production Norms and
No loss due to implemented action
STEP – 11
REGULAR IMPLEMENTATION
P - PRODUCTIVITY
Q - QUALITY
C - COST
D - DELIVERY
S - SAFETY
M - MORALE
Cost Savings :
1500000/- per annum Cost savings
Expected by reducing the cycle time of
Grinding process in CX Section
Investment Cost : 10000
Return Of Investment : 1 Months
STEP – 11
REGULAR IMPLEMENTATION
P - PRODUCTIVITY
Q - QUALITY
C - COST
D - DELIVERY
S - SAFETY
M - MORALE
100% Internal customer and External Customer
delivery improved
P - PRODUCTIVITY
Q - QUALITY
C - COST
D - DELIVERY
S - SAFETY
M - MORALE
100% Internal customer and External Customer
delivery improved
STEP - 11
REGULAR IMPLEMENTATION
FENNER SUPER KINGS 36
15-Sep-23
STEP – 12
1
FOLLOW - UP / REVIEW
STEP – 12 FOLLOW - UP / REVIEW
 Work Instruction Updated (WI) and issued to Internal customer
 PCN documented and issued
CONCLUSION
RADAR CHART
INTANGIBLE BENEFITS
0
20
40
60
80
100
AFTER
BEFORE
TEAM WORK
PROBLEM
SOLVING ABILITY
CREATIVITY
COMMUNICATION
SKILLS
INVOLVEMENT
QC KNOWLEDGE
TIME
MANAGEMENT
MORALE
INITIATIVE
UNDERSTAND
CUSTOMER NEEDS
CONCLUSION
Communication skills
Inter Personal Relations
Team Spirit
Product Knowledge
200
195
190
185
180
175
170
165
160
155
150
M
ill
io
n
s
o
f
D
o
lla
r
s
1992
1991
1990
Pr oduc t i
on C
os t s
U
ni
t Pr i
c e
Pr of i
t s
Self Confidence
Computer Skills Improved

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QC CIRCLE PRESENTATION (1).pptx

  • 1. QUALITY CIRCLE PRESENTATION 18/11/2022 Team Members: PRODUCTIVITY IMPROVEMENT IN REC BANDED BELT GRINDING MACHINE  Mr. N.Karthik – Technology & Development  Mr. Rajasekaran – REC Manufacturing  Mr. L.Raja- Engineering Department  Mr. G.Rajesh – Technical Department
  • 4. STEP-1 IDENTIFICATION OF WORK RELATED PROBLEM Problem Statement  Machine adherence: Delivery adherence is poor  Rework is greater than 40% of actual coding value.  Asset utilization: Cycle time is high compare to Vertical grinding machine.  To meet the budgeted value of 2022-2023 and create capacity to failure 0 1000 2000 3000 4000 5000 6000 Qty in Nos. Oct-21 Nov-21 Dec-21 Jan-22 Feb-22 Mar-22 Supply 2500 2500 2862 2132 4041 3633 Demand 3500 3500 4000 3000 5000 5000 Demand Vs Supply of Banded belt Supply Demand
  • 5. STEP - 2 1 SELECTION OF PROBLEM
  • 6. STEP – 2 SELECTION OF PROBLEM Phase 1: Machine Throughput to be increase- Machine Parameters record, Machine actual mode, Rework is high : Target : 35 % - 0% for CX & SPCX section Phase 2: Cycle time improvement for different varieties: Target : 35 % by 2022 – 23 Phase 3: Horizontal deployment of improvements in other grinding machines PHASE 1: REWORK TO BE REDUCE AND ELIMINATE 35 0 0 40 Rework Percentage REWORK-CX Section Existing Target PHASE 2: CYCLE TIME REDUCTION Target: 30% 903 589 0 150 300 450 600 750 900 1050 Cycle time in CX CYCLE TIME Existing Target TARGET
  • 7. STEP - 3 1 DEFINE THE PROBLEM
  • 8. STEP – 3 DEFINE THE PROBLEM 1) Unable to achieve the current customer demand of 60000 / annum where our current productivity is 13000 belts per annum. 2) High rework generation: 35%
  • 9. STEP – 4 1 ANALYSE THE PROBLEM
  • 10. STEP – 4 ANALYSE THE PROBLEM High cycle time and Rework WHAT is the problem? WHERE does this problem occur ? Grinding Process WHEN does it occur ? During grinding operation WHO notices this problem ? Production department HOW can solve this problem ? By study and improving the Grinding Methodology
  • 11. BRAINSTROMING 01 02 03 04 05 06 0 7 08 09 10 Coupling Lock system Nuts can be removed using Wrench Hand wheel elimination Grinding wheel Setup change time Dead weight arrangement: Stroke Grinding wheel speed Pressure pad Alignment Horizontal grinding m/c to Profile grinding m/c Pulley alignment to be perfect Cycle time of grinding
  • 13. STEP – 5 IDENTIFCIATION OF CAUSES BRAINSTORMING POINTS SPECIFICATION IMPROVEMENT PLANNED RESULT Coupling lock system Locking made on separate link Found Ok Insignificant Cycle time in Grinding Cycle time– 903 Seconds Grinding time can be optimized Significant Pressure pad Alignment All groove OD in pressure pad to be equal size Groove OD to be turned to required size Significant Grinding wheel Setup change time Setup changeover time: 12 mins avg Reasonable time Insignificant Hand wheel elimination Belt Tensioning time: 33s Time can optimize with automated mechanism Significant Pulley alignment to be perfect Pulley and belt seating area to be align Found Ok Insignificant Nuts can be removed using Auto Wrench Using manual wrenches nut removal happening Found Ok Insignificant Dead weight arrangement: Stroke length Stroke length of shaft: 200mm Can be increase to some range Significant Horizontal m/c to Profile grinding machine Loading belts in current setup for grinding To overcome order quantity utilizing the asset Significant Grinding wheel speed Speed: 1390 rpm Reached maximum capacity Insignificant
  • 14. STEP – 6 1 FINDING OUT THE ROOT CAUSES
  • 15. STEP – 6 FINDING OUT THE ROOT CAUSES ( Why) ( Why) COUNTER MEASURE Throughput improvement Delay in belt delivery High cycle time and Belt Rework generation Improper Pressure pad/More number of grinding steps ( Why) Existing method WHY WHY ANALYSIS
  • 16. STEP – 7 1 DATA ANALYSIS
  • 17. STEP – 7: DATA ANALYSIS 1000.00 350.00 0 2000 Jul-22 Aug- 22 Sep- 22 Oct- 22 Nov- 22 Plan Avg. Belt Numbers Qty REC Grinding m/c– ProductionTrend Avg G.W Motor Rating Kw 15 Drive pulley dia 148 mm Maximum Load Calculated Amps 26 Drive Pulley RPM 134 rpm Motor reduction 1:1 Belt linear speed 62.30 m/min GW. Speed rpm 1390 Direction of rotation Clockwise G.W dia mm 138 Pressure pad linear speed 0.04 mm/sec G.W. linear speed m/min 603 Belt Sec: CX 85 2159 Profile Banded Top width 21.7 mm GW 1664.2 603m/min Thickness 14.8 mm Anvil 1.92 62.30m/min Belt Sec: Diff speed 865.3 9.7 0.001 0.103 Step Depth Area of material removal Belt Contact with grinding wheel Grinding wheel temperature Load Time - secs Belt rotation mm Sq.mm mm deg C Amps Pr.Pad movement Dwell time Step Time Nos Min Max Loading Time 33 Grinding 1 2.0 1.4 2.1 34.1 6.4 7.3 50.0 44.4 94 45.40 2 2.0 8.4 4.3 46.7 6.5 7.1 50.0 44.4 94 45.40 3 1.5 9.2 5.9 57.3 7.0 8.1 37.5 44.4 82 39.39 4 1.5 6.8 7.4 72.9 7.9 9.8 37.5 44.4 82 39.39 5 1.0 5.4 8.5 95.4 8.9 11.2 25.0 44.4 69 33.38 6 1.0 6.0 9.6 107.0 9.4 12.2 25.0 44.4 69 33.38 7 0.8 5.4 10.4 122.4 11.8 12.9 20.0 44.4 64 30.97 8 0.8 5.9 11.3 124.1 10.9 15.0 20.0 44.4 64 30.97 9 0.8 6.4 12.1 127.5 11.1 15.2 20.0 44.4 64 30.97 10 0.6 5.1 12.8 146.3 11.0 15.2 15.0 44.4 59 28.57 11 0.5 4.4 13.3 145.1 10.7 11.7 12.5 44.4 57 27.37 Auto run - Deburring 43 20.68 Unloading 16 12.5 64.4 312.5 488.4 893 405.86
  • 19. STEP – 8: DEVELOPING SOLUTION Act. No ACTIVITY Cycle Time in Secs (Existing) 1 Setting the parameters in HMI 10 2 Belt Loading Time 20 3 Closing the lid and press RUN in HMI 3 4 Step 1-2 95 5 Step 2-3 92 6 Step 3-4 79 7 Step 4-5 79 8 Step 5-6 66 9 Step 6-7 69 10 Step 7-8 62 11 Step 8-9 62 12 Step 9-10 61 13 Step 10-11 60 14 Step 11- 12 51 15 Step 12-Grinding complete 35 16 Reversal-End 43 17 Unloading Time 16 Cycle time, seconds 903 HORIZONTAL GRINDING MACHINE
  • 20. STEP – 8: DEVELOPING SOLUTION BEFORE AFTER HAND WHEEL  Belts are Loaded in machine and belt tension given to belt with hand wheel for 4 belts.  Cycle time 33 secs  Simple mechanism provided by eliminating the hand wheel with Motor mechanism-Easy tensioning.  Cycle time 3 Sec Simplify Action : 1 HAND WHEEL ELIMINATION
  • 21. STEP – 8: DEVELOPING SOLUTION KAIZEN IDEA - SHEET
  • 22. STEP – 8: DEVELOPING SOLUTION BEFORE AFTER Stroke length increased to meet the correct Belt Tension  The dead weight is not arranged properly  Tension variation is high due to stroke length deviation  Dead weight- 240 Kg Action : 2 DEAD WEIGHT ARRANGEMENT: STROKE LENGTH
  • 23. STEP – 8: DEVELOPING SOLUTION BEFOR E AFTE R Equal surface achieved Tape removed AFTER BELT CODING NOT OK BELT CODING OK BEFORE 35% THROUGHPUT IMPROVED Action : 3 UNEVEN PRESSURE PAD RESULT IMPACT: THROUGHPUT IMPROVEMENT
  • 24. STEP – 8: DEVELOPING SOLUTION Action : 4 REDUCTION IN GRINDING STEPS 35% Reduction time for Target, From 903 Sec to 589 Sec – Reduction 314 Sec. The Reduction plan is based on idea generation in brain storming points identified through SCAMPER approach VA – Value Added Activity, NVA –Non Value Added Activities Act. No. Activities Actual Time taken (sec) Time Reduction plan(Sec) Saving time in (Sec) Category VA NVA 4 Grinding Step 1-2 95 94 1 1 5 Grinding Step 2-3 92 86 6 6 Grinding Step 3-4 79 70 9 7 Grinding Step 4-5 79 66 13 8 Grinding Step 5-6 66 62 4 9 Grinding Step 6-7 69 60 9 10 Grinding Step 7-8 62 55 7 11 Grinding Step 8-9 62 0 62 12 Grinding Step 9-10 61 0 61 13 Grinding Step 10-11 60 0 60 14 Grinding Step 11- 12 51 0 51 16 Reversal-End 43 22 21 2 15 Grinding Step 12-Grinding complete 35 55 -20 17 Belt Unloading Time 16 3 13 3 2 Belt Loading time 20 3 17 4 1 Setting parameters in HMI 10 10 0 5 3 Closing the lid and press RUN in HMI 3 3 0 6 Total time in secs 903 589 314 90% 10% VA NVA
  • 25. STEP – 8: DEVELOPING SOLUTION BEFORE AFTER AFTER Step Depth Step Grinding time 1 2.6 1-2 94 2 2.5 2-3 86 3 1.8 3-4 70 4 1.5 4-5 66 5 1.2 5-6 62 6 1 6-7 60 7 0.8 7-8 55 8 0.5 8-Grinding completed 55 Depth 12.5 Reversal-End 22 Total Grinding time (AFTER) 570 GRINDING MATERIAL REMOVAL SIMULATION STUDY BEFORE Step Depth Step Grinding tme 1 2.0 1-2 95 2 2.0 2-3 92 3 1.5 3-4 79 4 1.5 4-5 79 5 1.0 5-6 66 6 1.0 6-7 69 7 0.8 7-8 62 8 0.8 8-9 62 9 0.8 9-10 61 10 0.6 10-11 60 11 0.5 11-Grinding completed 51 Depth 12.5 Reversal-End 35 Total Grinding time (BEFORE) 854 Action : 4 REDUCTION IN GRINDING STEPS
  • 26. STEP – 9 1 FORSEEING PROBLEM OF RESISTANCE
  • 27. STEP – 9 FORSEEING PROBLEM OF RESISTANCE Sl. No Implemented actions Resistance Raised by Corrective actions Status 1 Hand wheel elimination Hand wheel - Introduced motor mechanism Completed and implemented 2 Rework elimination Pressure pad - Even Surface finish achieved through lathe operation Completed and implemented actions are followed 3 Stroke length Adjustment Dead weight - Stroke length increased to meet the correct belt tension Completed and implemented actions are followed 4 Grinding steps reduced for CX section More steps in grinding - Performed Load and temperature study and reduced the grinding steps Completed and implemented actions are followed
  • 28. STEP – 10 1 TRAIL IMPLEMENTATION & CHECK PERFORMANCE
  • 29. STEP – 10 TRAIL IMPLEMENTATION & CHECK PERFORMANCE After Act.No ACTIVITY CycleTime in Secs (Existing) 1 Setting the parameters in HMI 10 2 Belt Loading Time 20 3 Closing the lid and press RUN in HMI 03 4 Step 1-2 94 5 Step 2-3 86 6 Step 3-4 70 7 Step 4-5 66 8 Step 5-6 62 9 Step 6-7 60 10 Step 7-8 55 11 Step 8-9 0 12 Step 9-10 0 13 Step 10-11 0 14 Step 11- 12 0 15 Step 12-Grinding complete 55 16 Reversal-End 22 17 Unloading Time 03 Cycle time, seconds 589
  • 30. STEP – 10 TRAIL IMPLEMENTATION & CHECK PERFORMANCE S.No Activities Before (In Secs) After (In Secs) %Reduction in time Action taken 1 VA 854 570 33.25% 1. Pressure pad outer diameter turned to achieve even surface 2. Stroke length increased with simple mechanism to withstand the dead weight in proper way 3. Introduced Load, frequency meter and modified the rpm. Performed temperature simulation study on machine 2 RNVA 49 19 61.22% Introduced Motor feed mechanism by eliminating manual hand wheel operation Total time in secs 903 589 34.78% 95% 5% VA RNVA 97% 3% VA RNVA BEFORE CYCLETIME AFTER CYCLETIME
  • 31. STEP – 11: REGULAR IMPLEMENTATION 1 REGULAR IMPLEMENTATION NO DEFECT - NO WASTE - NO DELAY
  • 32. STEP – 11 REGULAR IMPLEMENTATION Results 1000.00 1080.00 0 200 400 600 800 1000 1200 1400 Jun-22 Jul-22 Aug-22 Sep-22 Oct-22 Plan Avg. Belt Numbers Qty REC Grinding m/c– ProductionTrend Avg Plan Actual PHASE 1: REWORK ELIMINATED 35 0 0 40 Rework Percentage REWORK-CX Section Existing Target PHASE 2: CYCLE TIME REDUCTION Achieved: 35% 903 589 0 150 300 450 600 750 900 1050 Cycle time in CX CYCLE TIME Existing Target
  • 33. STEP – 11 REGULAR IMPLEMENTATION P - PRODUCTIVITY Q - QUALITY C - COST D - DELIVERY S - SAFETY M - MORALE Achieved the daily production Norms and No loss due to implemented action
  • 34. STEP – 11 REGULAR IMPLEMENTATION P - PRODUCTIVITY Q - QUALITY C - COST D - DELIVERY S - SAFETY M - MORALE Cost Savings : 1500000/- per annum Cost savings Expected by reducing the cycle time of Grinding process in CX Section Investment Cost : 10000 Return Of Investment : 1 Months
  • 35. STEP – 11 REGULAR IMPLEMENTATION P - PRODUCTIVITY Q - QUALITY C - COST D - DELIVERY S - SAFETY M - MORALE 100% Internal customer and External Customer delivery improved
  • 36. P - PRODUCTIVITY Q - QUALITY C - COST D - DELIVERY S - SAFETY M - MORALE 100% Internal customer and External Customer delivery improved STEP - 11 REGULAR IMPLEMENTATION FENNER SUPER KINGS 36 15-Sep-23
  • 37. STEP – 12 1 FOLLOW - UP / REVIEW
  • 38. STEP – 12 FOLLOW - UP / REVIEW  Work Instruction Updated (WI) and issued to Internal customer  PCN documented and issued
  • 39. CONCLUSION RADAR CHART INTANGIBLE BENEFITS 0 20 40 60 80 100 AFTER BEFORE TEAM WORK PROBLEM SOLVING ABILITY CREATIVITY COMMUNICATION SKILLS INVOLVEMENT QC KNOWLEDGE TIME MANAGEMENT MORALE INITIATIVE UNDERSTAND CUSTOMER NEEDS
  • 40. CONCLUSION Communication skills Inter Personal Relations Team Spirit Product Knowledge 200 195 190 185 180 175 170 165 160 155 150 M ill io n s o f D o lla r s 1992 1991 1990 Pr oduc t i on C os t s U ni t Pr i c e Pr of i t s Self Confidence Computer Skills Improved