This document discusses a study conducted at PT ABC to increase the production capacity of its rack steering line using Lean Six Sigma methodology. PT ABC was facing increasing customer demand but its normal daily production capacity of 744 units was insufficient, requiring overtime. The researchers applied the DMAIC process and identified opportunities to reduce cycle times through minimizing waste. They determined the longest process times were on machines OP-10, OP-20, OP-30 and OP-90. Improvements such as optimizing machine programs, replacing over-specified machines with more appropriate ones, improving tools, and modifying jig positions reduced cycle times from 1.1 minutes to 1 minute. This increased daily capacity to 818 units and reduced overtime costs.