2. INTRODUCTION
The Bhopal Disaster which is commonly referred to
as Bhopal Gas Tragedy was a gas leak incident in
India, considered one of the world’s worst industrial
catastrophes.
It occurred on the night of December 2-3,1984 at
the Union Carbide India Limited, a pesticide plant in
Bhopal, Madhya Pradesh, India.
A leak of methyl isocyanate gas and other
chemicals from the plant resulted in the exposure of
thousands of people.
3. UNION CARBIDE INDIA LIMITED
UCIL was the Indian subsidiary of Union Carbide
Corporation (UCC), with Indian Government
controlled banks and the Indian public holding a
49.1 percent stake.
It started in 1969 at the northern state of India.
Phosgene, Monomethlyamine, Methyl Isocyanate
(MIC) and the pesticide Carbaryl, also known as
Sevin were manufactured here.
4.
5. PLANT PRODUCTION PROCESS
UCC produced carbaryl using MIC as an
intermediate.
After the Bhopal plant was built, other
manufacturers including Bayer produced carbaryl
without MIC, though at a greater manufacturing
cost.
6. PLANT PRODUCTION PROCESS
Methylamine (1) reacts with phosgene (2)
producing methyl isocyanate (3)
which reacts with 1-naphthol (4) to yield
carbaryl (5)
7. CAUSE:-
According to one theory:
Water leaked into tank from valves while workers
were cleaning the clogged pipe which is 400 feet
above it.
According to another theory:
Water was directly introduced into tank intentionally
by a worker via a missing pressure gauge .
It resulted in exothermic reaction and finally to a
explosion.
8. OTHER CAUSE:-
Plant management deficiencies like :
Lack of skilled operators,
Reduction of safety management.
Insufficient maintenance and
Inadequate emergency action plans.
Use of a more dangerous pesticide manufacturing
method for decreasing generation cost.
Plant location close to a densely populated area.
9. CONTRIBUTION OF NEGLIGENCE:-
UCIL didn’t maintained safety rules.
A pipe leaked? Don't replace it.
MIC workers needed more training. They could do
with less.
The MIC tank alarms had not worked for four years.
The flare tower and the vent gas scrubber had been
out of service for five months before the disaster.
To reduce energy costs, the refrigeration system
was idle. The MIC was kept at 20 degrees Celsius,
not the 4.5 degrees advised by the manual.
10. The steam boiler, intended to clean the pipes, was
out of action for unknown reasons.
Carbon steel valves were used at the factory, even
though they corrode when exposed to acid.
According to the operators the MIC tank pressure
gauge had been malfunctioning for roughly a week.
UCC admitted in their own investigation report that
most of the safety systems were not functioning on
the night of December 3, 1984.