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International Journal of Electrical and Computer Engineering (IJECE)
Vol. 13, No. 4, August 2023, pp. 3969~3976
ISSN: 2088-8708, DOI: 10.11591/ijece.v13i4.pp3969-3976  3969
Journal homepage: http://ijece.iaescore.com
Design and implementation of a control system for a steel plate
cutting production line using programmable logic controller
Basheer Najemaldeen Shaheed, Nasir Hussein Selman
Al-Najaf Technical Engineering College/Najaf, Al-Furat Al-Awsat Technical University ATU, Najaf, Iraq
Article Info ABSTRACT
Article history:
Received Nov 12, 2022
Revised Dec 21, 2022
Accepted Dec 27, 2022
Most of the old machines installed in different industries are managed
manually by system operators. This action makes their productivity low and
not suitable to cover the needs in other sectors. In addition, these machines
are not without risks due to the proximity of the operators to them. The
installing a new full system instead of the old one on the same site requires
very high costs. So, modernizing the same old system by making its
operation automatic has become necessary to reduce the economic cost
significantly. In this paper, an automatic control system based on
programmable logic controller (PLC) for the cutting steel plate machine that
had been managed manually in a factory is designed. The system includes an
Encoder that is used to specify the length of the steel plate to be cut by
sending a signal to the PLC. The system operation is completed by using
human machine interface (HMI) unit to monitor and control the system
performance by the system operator. A practical test for the developed
system offered more productivity (more than 30%), more safety, reduces
human efforts and the total daily production cost (less than one third).
Keywords:
Encoder
Human machine interface
Ladder diagram
Programmable logic controller
Variable frequency drive
This is an open access article under the CC BY-SA license.
Corresponding Author:
Basheer Najemaldeen Shaheed
Al-Najaf Technical Engineering College/Najaf, Al-Furat Al-Awsat Technical University ATU
Najaf, Iraq
Email: basheernajem7@gmail.com
1. INTRODUCTION
Nowadays, developers are searching for numerous methods to minimize labor efforts, cost and time
[1], [2]. The idea of freshening conventional machines that managed manually is a popular rule in many
factories. Developing the same longstanding systems by adding automation to them has become vital to
increase the productivity and profits [3], [4]. Programmable logic controller (PLCs) are commonly employed
in manufacturing automation, and are characterized by high flexibility, accuracy, reliability and strong
real-time performance [5], [6].
Steel plate cutting machines are important machines that are installed in many factories and used in
many applications such as water tanks, cars bodywork, roof works for garages, and buildings. To increase
productivity and safety, PLC systems are used to control these machines. Also, a display tool such as a
computer or human machine interface (HMI) is used to monitor the progress operation of such systems [7].
In this paper, a control system for a conventional steel plate cutting machine located in a factory
using PLC and HMI is built. PLC system helps control the speed of the induction motor that responsible for
the movement of the steel plate by the variable frequency drive (VFD) and the encoder. The operator enters
the panel length and number of panels through the HMI to obtain the desired product.
The organization sections of this paper as: in section 2, literature review is given. In section 3 the
hardware tools that include mechanical and electrical parts are described. In section 4, architecture of control
 ISSN: 2088-8708
Int J Elec & Comp Eng, Vol. 13, No. 4, August 2023: 3969-3976
3970
strategy is illustrated. In section 5, software description is specified. In section 6 experiment results are
offered. Finally, the conclusions are given in section 7.
2. RELATED WORK
PLC and HMI are widely used to control many industrial processes. Therefore, many researchers
have addressed the use of PLC to control production lines in factories. Kumar and Prasad [5] presented a case
study of modifying automation system of a filament coiling machine to increase its activity and accuracy.
The developed machine was reducing the human labor and increasing the robustness of the system using
Delta PLC. The speed feedback control is designed by digital encoder for constant speed operation. VFD is
used to control the speed of an induction motor which drive the required load. The PLC monitors and
controls all the input and output apparatuses through HMI. Gafar and Said [7] discussed modifying a control
system using a PLC for a wire cutting machine used in an air cooler refrigerators plant. The paper was
focused on how the control system is able to increase production, safety, and benefits as well as decrease
workers, stopping time, failures, and waste. Kamau [8] proposed a case study to modify and control the
machine by using PLC. The electrical board that controls the machine was an old PCB board and the faults
were frequent and it was very expensive to repair. The new design with the help of Siemens PLC provides
more efficiency and higher production. Han et al. [9] introduced an automatic control system using PLC for
“cutting metal plates in the flame cutting machine”. The developed system is able to perform fixed lengths of
plates with high accuracy. The system has many operation modes and meets the requirements of many types
of products.
Syufrijal et al. [10] designed a system that controls a “pipe cutting machine” using PLC and HMI
with high accuracy. The system employed an “servo motor”. PLC received a signal from proximity and
Encoder. Proximity is used to detect the existence of pipe whereas the Encoder detects servo motor speed and
hence the pipe Length. The machine cuts pipes automatically depending on the number and length of the
pipes required. Bhatlawande et al. [11] proposed an automated system using a PLC to control on “Velcro
cutting machine” with the help of stepper motor and the encoder. The roller is controlled by stepper motor
rotations. The encoder is used for giving a pulse per each movement of the roller. Heater’s temperature is
sensed by temperature sensor that fed the feedback signal to the PLC to control the heat of the cutter which
cuts the product properly. Gadale et al. [12] presented a study on the importance of automation in the
traditional cutting machines used in industrialization. The cutting machine has lower execution time, greater
productivity, and less damage to the workers when using a PLC control system. Kumar et al. [13] designed a
control system for a “powder press machine” using PLC, servo motor and linear displacement Encoder.
Servo motor operation is controlled by VFD. LVDT device is used to send the servo motor positioning to the
PLC. The outputs terminals of PLC are connected to valves, VFD and HMI. PLC helps reduce the cost,
increase production, and save on energy.
3. DESCRIPTIONOF HARDWARE TOOLS
3.1. Mechanical parts
The mechanical parts of the cutting steel plate machine have been presented in Figure 1. The first
part is a steel coil that is rotated by a three-phase induction motor. The leveling parts pull the steel plate due
to the force of friction and make it flat and balanced. The plate passes through a cutting press that cuts the
plate to the desired length. The cutting section includes a three-phase induction motor and a saw blade. The
encoder, which is tangent to the steel plate, starts to rotate and sends pulses to the PLC to determine the
length of the steel plate continuously. Figure 2 shows a screenshot of the mechanical parts of the system.
Figure 1. Mechanical parts of the cutting steel plate
machine
Figure 2. Photograph of the mechanical parts of the
system
Int J Elec & Comp Eng ISSN: 2088-8708 
Design and implementation of a control system for a steel plate cutting … (Basheer Najemaldeen Shaheed)
3971
3.2. Electrical parts
The electrical parts of the system include several elements. The important part of the system is the
PLC unit, which is the main control for the rest of the parts. The VFD has the function of controlling
induction motors in the system. The system also contains an encoder whose function is to sense the
movement of the steel plate and to present its signal as input to the PLC. The HMI is an important part of the
integration of the system's work as it is used to monitor and enter all the required data.
The system contains secondary accessories that include motor protection circuit breaker (MPCB),
oil pump system, A 3-Pole miniature circuit breaker (MCB), switched-mode power supply (SMPS),
transformer and relays. The following sections describe the main electric parts.
3.2.1. Variable frequency drive
Variable frequency drive (VFD) is an electrical device that converts input AC power into AC with
adjustable voltage and frequency [14]. The VFD is used for speed control of a three-phase asynchronous
motor [15], [16]. The VFD has many advantages such as reliable energy saving, accurate speed control, and
easily realize automatic control [17], [18]. Figure 3 shows the block diagram of the VFD circuit [19].
In this work, VFD used to control the speed of leveling motor. At the beginning, the leveling motor
rotates at full speed and before the plate reaches the specified length, the motor slows down its speed and
finally break. Table 1 shows the VFD specifications.
Figure 3. Block diagram of the VFD
Table 1. VFD specifications
Rated power (KW) Rated voltage (V) Rated current (A) Frequency (Hz)
5.5 380 13 0-400
3.2.2. Encoder
An incremental rotary encoder is a device that converts mechanical movement into an electrical
signal. It is employed vastly in industrial automation systems like speed estimation of motors [20], [21]. It is
used in measuring lengths, angular position, and speed. The pulses generated by the encoder are proportional
to the variable to be measured [22]. Figure 4 gives a pictorial image of the encoder used in this work.
Specification of the encoder is given in Table 2.
Figure 4. Incremental rotary encoder
Table 2. Specification of the rotary encoder
Model Shaft external diameter Pulse number per revolution Phase type Voltage
E50S8 8 mm 500 3: A, B, Z 12-24 V DC
 ISSN: 2088-8708
Int J Elec & Comp Eng, Vol. 13, No. 4, August 2023: 3969-3976
3972
4. ARCHITECTURE OF THE CONTROL SYSTEM
The architecture of the whole system of cutting steel coil machine can be seen in Figure 5. The
3-phase voltage of the main power supply passes through the MCB to feed the control board. VFD and power
contactor are fed via the MCB directly. The SMPS received 220 Vr.m.s via the transformer and step-down
and rectified it to the 24 Vdc which represents the input to the PLC, limit switch, and the encoder. The
operation principle can be illustrated as:
Figure 5. Block diagram of control system
At the beginning of the operation, the initial parameters of the system must be specified by the
system operator using HMI to control and monitor the work of the machine. These parameters include length
of each plate and the number of the plate to be cutting. The system operation is started when the push button
is pressed ON. VFD will be received a signal from the PLC to control the speed of the induction motor
(levelling motor). The encoder starts to rotate and sends pulses to the PLC to define the length of the steel
plate continuously. Before the plate reaches to the required length (90% of length), PLC sends a signal to the
VFD. The levelling motor received the control signal from VFD and then it reduces its speed gradually and
finally stopped when the plate reached to the required length. After that, PLC sends a signal to the relay,
which is in turn sending it to the cutting device to cut the steel plate. When the cutting process complete, the
control process is repeated for the next plate until reach to the required number of the steel plates.
5. SOFTWARE DESCRIPTION
The program was implemented for Delta PLC Table 3 gives its specifications based on logical
instruction where it works on two states (ON and OFF) [23], [24]. The programming method used is the
ladder diagram (LAD) method. The designing LAD can be running and verifying by a personal computer
[25]. PLC takes the sensors signal and processed them by the program then gives the signal to the VFD
which again processes this input signals and finally controlling the motor speed. In this project, programming
of PLC was performed employing WPLSoft 2.5.0 version. This software integrates all the modules connected
to the PLC and the devices connected to its HMI, VFD, induction motor and hydraulic motor. Also, the
monitor and control are achieved through HMI and its screens are developed using DOPSoft version 1.00.11.
The flowchart of the automatic cutting steel plate machine given in Figure 6, while Figure 7 shows the screen
shot of part of ladder logic program for the control system.
Table 3. Delta PLC specifications
Model Operating voltage Max. frequency Input/Output ports Comm ports
DVP12SE11R 24 VDC 100 kHz 8 input/4 output digital 1 Ethernet, 2 RS-485, 1 RS-232
Int J Elec & Comp Eng ISSN: 2088-8708 
Design and implementation of a control system for a steel plate cutting … (Basheer Najemaldeen Shaheed)
3973
Figure 6. Flowchart of the control system of the cutting steel plate machine
Figure 7. Screen shot of the ladder program for the control system
 ISSN: 2088-8708
Int J Elec & Comp Eng, Vol. 13, No. 4, August 2023: 3969-3976
3974
6. EXPERIMENT RESULTS
The testing of the design system is done practically to determine how the control system used to cut
the steel plate with satisfactory accuracy. Figure 8 shows a picture to the main control board. Figure 9
illustrates the control panel that used by operator of the system to enter the required implementation.
Figure 10 gives the HMI that used to input and display the following data: i) input length: the required length
of the steel plate; ii) number of plates: represents the required number of the steel plate; iii) instant distance:
represents the instant length of the steel plate moving through the cutting press. This distance is important to
give indication to the operator before the plate reaches the cutting point; iv) number of completed plate: gives
the completed steel plate that were cutting; v) cleared (CLR): pushbutton for clearing the system; vi) run and
stop; and vii) forward (FWD) and reverse (REV) rotation of levelling motor respectively.
Figure 8. Main control board Figure 9. Control desk panel
Figure 10. HMI that used to input and display data
Figure 11 shows the increase in productivity before and after system renewal. One can notice that
the increase in the number of production plates is inversely proportional to the length of the plate (the
increase in productivity was from 150 plate/hour to 190 plate/hour when the length of the plate was 1 meter,
while the increase was from 20 plate/hour to 32 plate/hour when the length of the plate 9 meter). The reason
for the difference in increasing rate of the productivity is the stopping that occurs after the production of each
plate. Figure 12 gives the relation between the length of the plate and the pulses of the encoded. Table 4
illustrates the total production cost per day before and after development ($90/day and $28/day respectively).
This means that the total cost decreases significantly (less than one third).
Int J Elec & Comp Eng ISSN: 2088-8708 
Design and implementation of a control system for a steel plate cutting … (Basheer Najemaldeen Shaheed)
3975
Figure 11. Increase in productivity before and after
system development
Figure 12. Relation between the length of the plate
and the pulses of the Encoded
Table 4. Average production cost
Cost type Before development After development
Product deterioration 40$ 10$
salaries of operators 45$, for three operators 15$ for one operator
other costs 5$ 3$
Total/day 90$ 28$
7. CONCLUSION
In this paper, an automatic control system based on PLC and HMI was designed. The system is used
to develop the work of the steel plate cutting machine that has been installed early in one of the production
factories. This update is saving the capital of buying a new entire new product. The operator enters the plate
length and plate number through the HMI which represents important part of the updating system. The
position of the length of the plate that was driven by the motor can be sensed by the encoder. The signal of
the encoder is sending to the PLC, which in turn sends a signal to the motor. The motor slow down gradually
until it reaches the desired length, then it stops. After that, PLC sends a signal to the cutting motor to cut the
plate, then the process is repeated again. In order to confirm the usefulness of the developed system, it was
verified experimentally in real-time production line. The output production capacity of the updated system
was increased due to the reducing in stopping time that occurs after each cutting of plate by system operator.
Also, there is an increase in the safety of the system and a saving in labor from 3 persons to one.
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BIOGRAPHIES OF AUTHORS
Basheer Najemaldeen Shaheed received the B.Eng. degree in electrical and
communication engineering from Al-Furat Al-Awsat Technical University, Iraq, in 2018.
Currently, working as an engineer in a private sector company. His research interests include
communication networks, internet of thing, automation control, wireless sensor networks,
renewable energy, power electronics, solar energy, power generation, electric vehicles, store
energy, and artificial intelligence. He can be contacted at email: basheernajem7@gmail.com.
Nasir Hussein Selman received the Bsc. Eng. degree in electrical engineering
from university of technology, Iraq, in 1992 and Msc in 2004. Ph.D. degrees in electric power
and machine engineering from Basrah University, Iraq, in 2016. Currently, he is a Lecturereat
the Al-Najaf Technical Engineering College/Najaf, Al-Furat Al-Awsat Technical University
ATU, Iraq. His research interests include renewable energy, power electronics,
microcontroller, programming, power generation, smart grids, load flow control. He can be
contacted at email: nhsm1969@yahoo.com.coj.nas@atu.edu.iq.

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Design and implementation of a control system for a steel plate cutting production line using programmable logic controller

  • 1. International Journal of Electrical and Computer Engineering (IJECE) Vol. 13, No. 4, August 2023, pp. 3969~3976 ISSN: 2088-8708, DOI: 10.11591/ijece.v13i4.pp3969-3976  3969 Journal homepage: http://ijece.iaescore.com Design and implementation of a control system for a steel plate cutting production line using programmable logic controller Basheer Najemaldeen Shaheed, Nasir Hussein Selman Al-Najaf Technical Engineering College/Najaf, Al-Furat Al-Awsat Technical University ATU, Najaf, Iraq Article Info ABSTRACT Article history: Received Nov 12, 2022 Revised Dec 21, 2022 Accepted Dec 27, 2022 Most of the old machines installed in different industries are managed manually by system operators. This action makes their productivity low and not suitable to cover the needs in other sectors. In addition, these machines are not without risks due to the proximity of the operators to them. The installing a new full system instead of the old one on the same site requires very high costs. So, modernizing the same old system by making its operation automatic has become necessary to reduce the economic cost significantly. In this paper, an automatic control system based on programmable logic controller (PLC) for the cutting steel plate machine that had been managed manually in a factory is designed. The system includes an Encoder that is used to specify the length of the steel plate to be cut by sending a signal to the PLC. The system operation is completed by using human machine interface (HMI) unit to monitor and control the system performance by the system operator. A practical test for the developed system offered more productivity (more than 30%), more safety, reduces human efforts and the total daily production cost (less than one third). Keywords: Encoder Human machine interface Ladder diagram Programmable logic controller Variable frequency drive This is an open access article under the CC BY-SA license. Corresponding Author: Basheer Najemaldeen Shaheed Al-Najaf Technical Engineering College/Najaf, Al-Furat Al-Awsat Technical University ATU Najaf, Iraq Email: basheernajem7@gmail.com 1. INTRODUCTION Nowadays, developers are searching for numerous methods to minimize labor efforts, cost and time [1], [2]. The idea of freshening conventional machines that managed manually is a popular rule in many factories. Developing the same longstanding systems by adding automation to them has become vital to increase the productivity and profits [3], [4]. Programmable logic controller (PLCs) are commonly employed in manufacturing automation, and are characterized by high flexibility, accuracy, reliability and strong real-time performance [5], [6]. Steel plate cutting machines are important machines that are installed in many factories and used in many applications such as water tanks, cars bodywork, roof works for garages, and buildings. To increase productivity and safety, PLC systems are used to control these machines. Also, a display tool such as a computer or human machine interface (HMI) is used to monitor the progress operation of such systems [7]. In this paper, a control system for a conventional steel plate cutting machine located in a factory using PLC and HMI is built. PLC system helps control the speed of the induction motor that responsible for the movement of the steel plate by the variable frequency drive (VFD) and the encoder. The operator enters the panel length and number of panels through the HMI to obtain the desired product. The organization sections of this paper as: in section 2, literature review is given. In section 3 the hardware tools that include mechanical and electrical parts are described. In section 4, architecture of control
  • 2.  ISSN: 2088-8708 Int J Elec & Comp Eng, Vol. 13, No. 4, August 2023: 3969-3976 3970 strategy is illustrated. In section 5, software description is specified. In section 6 experiment results are offered. Finally, the conclusions are given in section 7. 2. RELATED WORK PLC and HMI are widely used to control many industrial processes. Therefore, many researchers have addressed the use of PLC to control production lines in factories. Kumar and Prasad [5] presented a case study of modifying automation system of a filament coiling machine to increase its activity and accuracy. The developed machine was reducing the human labor and increasing the robustness of the system using Delta PLC. The speed feedback control is designed by digital encoder for constant speed operation. VFD is used to control the speed of an induction motor which drive the required load. The PLC monitors and controls all the input and output apparatuses through HMI. Gafar and Said [7] discussed modifying a control system using a PLC for a wire cutting machine used in an air cooler refrigerators plant. The paper was focused on how the control system is able to increase production, safety, and benefits as well as decrease workers, stopping time, failures, and waste. Kamau [8] proposed a case study to modify and control the machine by using PLC. The electrical board that controls the machine was an old PCB board and the faults were frequent and it was very expensive to repair. The new design with the help of Siemens PLC provides more efficiency and higher production. Han et al. [9] introduced an automatic control system using PLC for “cutting metal plates in the flame cutting machine”. The developed system is able to perform fixed lengths of plates with high accuracy. The system has many operation modes and meets the requirements of many types of products. Syufrijal et al. [10] designed a system that controls a “pipe cutting machine” using PLC and HMI with high accuracy. The system employed an “servo motor”. PLC received a signal from proximity and Encoder. Proximity is used to detect the existence of pipe whereas the Encoder detects servo motor speed and hence the pipe Length. The machine cuts pipes automatically depending on the number and length of the pipes required. Bhatlawande et al. [11] proposed an automated system using a PLC to control on “Velcro cutting machine” with the help of stepper motor and the encoder. The roller is controlled by stepper motor rotations. The encoder is used for giving a pulse per each movement of the roller. Heater’s temperature is sensed by temperature sensor that fed the feedback signal to the PLC to control the heat of the cutter which cuts the product properly. Gadale et al. [12] presented a study on the importance of automation in the traditional cutting machines used in industrialization. The cutting machine has lower execution time, greater productivity, and less damage to the workers when using a PLC control system. Kumar et al. [13] designed a control system for a “powder press machine” using PLC, servo motor and linear displacement Encoder. Servo motor operation is controlled by VFD. LVDT device is used to send the servo motor positioning to the PLC. The outputs terminals of PLC are connected to valves, VFD and HMI. PLC helps reduce the cost, increase production, and save on energy. 3. DESCRIPTIONOF HARDWARE TOOLS 3.1. Mechanical parts The mechanical parts of the cutting steel plate machine have been presented in Figure 1. The first part is a steel coil that is rotated by a three-phase induction motor. The leveling parts pull the steel plate due to the force of friction and make it flat and balanced. The plate passes through a cutting press that cuts the plate to the desired length. The cutting section includes a three-phase induction motor and a saw blade. The encoder, which is tangent to the steel plate, starts to rotate and sends pulses to the PLC to determine the length of the steel plate continuously. Figure 2 shows a screenshot of the mechanical parts of the system. Figure 1. Mechanical parts of the cutting steel plate machine Figure 2. Photograph of the mechanical parts of the system
  • 3. Int J Elec & Comp Eng ISSN: 2088-8708  Design and implementation of a control system for a steel plate cutting … (Basheer Najemaldeen Shaheed) 3971 3.2. Electrical parts The electrical parts of the system include several elements. The important part of the system is the PLC unit, which is the main control for the rest of the parts. The VFD has the function of controlling induction motors in the system. The system also contains an encoder whose function is to sense the movement of the steel plate and to present its signal as input to the PLC. The HMI is an important part of the integration of the system's work as it is used to monitor and enter all the required data. The system contains secondary accessories that include motor protection circuit breaker (MPCB), oil pump system, A 3-Pole miniature circuit breaker (MCB), switched-mode power supply (SMPS), transformer and relays. The following sections describe the main electric parts. 3.2.1. Variable frequency drive Variable frequency drive (VFD) is an electrical device that converts input AC power into AC with adjustable voltage and frequency [14]. The VFD is used for speed control of a three-phase asynchronous motor [15], [16]. The VFD has many advantages such as reliable energy saving, accurate speed control, and easily realize automatic control [17], [18]. Figure 3 shows the block diagram of the VFD circuit [19]. In this work, VFD used to control the speed of leveling motor. At the beginning, the leveling motor rotates at full speed and before the plate reaches the specified length, the motor slows down its speed and finally break. Table 1 shows the VFD specifications. Figure 3. Block diagram of the VFD Table 1. VFD specifications Rated power (KW) Rated voltage (V) Rated current (A) Frequency (Hz) 5.5 380 13 0-400 3.2.2. Encoder An incremental rotary encoder is a device that converts mechanical movement into an electrical signal. It is employed vastly in industrial automation systems like speed estimation of motors [20], [21]. It is used in measuring lengths, angular position, and speed. The pulses generated by the encoder are proportional to the variable to be measured [22]. Figure 4 gives a pictorial image of the encoder used in this work. Specification of the encoder is given in Table 2. Figure 4. Incremental rotary encoder Table 2. Specification of the rotary encoder Model Shaft external diameter Pulse number per revolution Phase type Voltage E50S8 8 mm 500 3: A, B, Z 12-24 V DC
  • 4.  ISSN: 2088-8708 Int J Elec & Comp Eng, Vol. 13, No. 4, August 2023: 3969-3976 3972 4. ARCHITECTURE OF THE CONTROL SYSTEM The architecture of the whole system of cutting steel coil machine can be seen in Figure 5. The 3-phase voltage of the main power supply passes through the MCB to feed the control board. VFD and power contactor are fed via the MCB directly. The SMPS received 220 Vr.m.s via the transformer and step-down and rectified it to the 24 Vdc which represents the input to the PLC, limit switch, and the encoder. The operation principle can be illustrated as: Figure 5. Block diagram of control system At the beginning of the operation, the initial parameters of the system must be specified by the system operator using HMI to control and monitor the work of the machine. These parameters include length of each plate and the number of the plate to be cutting. The system operation is started when the push button is pressed ON. VFD will be received a signal from the PLC to control the speed of the induction motor (levelling motor). The encoder starts to rotate and sends pulses to the PLC to define the length of the steel plate continuously. Before the plate reaches to the required length (90% of length), PLC sends a signal to the VFD. The levelling motor received the control signal from VFD and then it reduces its speed gradually and finally stopped when the plate reached to the required length. After that, PLC sends a signal to the relay, which is in turn sending it to the cutting device to cut the steel plate. When the cutting process complete, the control process is repeated for the next plate until reach to the required number of the steel plates. 5. SOFTWARE DESCRIPTION The program was implemented for Delta PLC Table 3 gives its specifications based on logical instruction where it works on two states (ON and OFF) [23], [24]. The programming method used is the ladder diagram (LAD) method. The designing LAD can be running and verifying by a personal computer [25]. PLC takes the sensors signal and processed them by the program then gives the signal to the VFD which again processes this input signals and finally controlling the motor speed. In this project, programming of PLC was performed employing WPLSoft 2.5.0 version. This software integrates all the modules connected to the PLC and the devices connected to its HMI, VFD, induction motor and hydraulic motor. Also, the monitor and control are achieved through HMI and its screens are developed using DOPSoft version 1.00.11. The flowchart of the automatic cutting steel plate machine given in Figure 6, while Figure 7 shows the screen shot of part of ladder logic program for the control system. Table 3. Delta PLC specifications Model Operating voltage Max. frequency Input/Output ports Comm ports DVP12SE11R 24 VDC 100 kHz 8 input/4 output digital 1 Ethernet, 2 RS-485, 1 RS-232
  • 5. Int J Elec & Comp Eng ISSN: 2088-8708  Design and implementation of a control system for a steel plate cutting … (Basheer Najemaldeen Shaheed) 3973 Figure 6. Flowchart of the control system of the cutting steel plate machine Figure 7. Screen shot of the ladder program for the control system
  • 6.  ISSN: 2088-8708 Int J Elec & Comp Eng, Vol. 13, No. 4, August 2023: 3969-3976 3974 6. EXPERIMENT RESULTS The testing of the design system is done practically to determine how the control system used to cut the steel plate with satisfactory accuracy. Figure 8 shows a picture to the main control board. Figure 9 illustrates the control panel that used by operator of the system to enter the required implementation. Figure 10 gives the HMI that used to input and display the following data: i) input length: the required length of the steel plate; ii) number of plates: represents the required number of the steel plate; iii) instant distance: represents the instant length of the steel plate moving through the cutting press. This distance is important to give indication to the operator before the plate reaches the cutting point; iv) number of completed plate: gives the completed steel plate that were cutting; v) cleared (CLR): pushbutton for clearing the system; vi) run and stop; and vii) forward (FWD) and reverse (REV) rotation of levelling motor respectively. Figure 8. Main control board Figure 9. Control desk panel Figure 10. HMI that used to input and display data Figure 11 shows the increase in productivity before and after system renewal. One can notice that the increase in the number of production plates is inversely proportional to the length of the plate (the increase in productivity was from 150 plate/hour to 190 plate/hour when the length of the plate was 1 meter, while the increase was from 20 plate/hour to 32 plate/hour when the length of the plate 9 meter). The reason for the difference in increasing rate of the productivity is the stopping that occurs after the production of each plate. Figure 12 gives the relation between the length of the plate and the pulses of the encoded. Table 4 illustrates the total production cost per day before and after development ($90/day and $28/day respectively). This means that the total cost decreases significantly (less than one third).
  • 7. Int J Elec & Comp Eng ISSN: 2088-8708  Design and implementation of a control system for a steel plate cutting … (Basheer Najemaldeen Shaheed) 3975 Figure 11. Increase in productivity before and after system development Figure 12. Relation between the length of the plate and the pulses of the Encoded Table 4. Average production cost Cost type Before development After development Product deterioration 40$ 10$ salaries of operators 45$, for three operators 15$ for one operator other costs 5$ 3$ Total/day 90$ 28$ 7. CONCLUSION In this paper, an automatic control system based on PLC and HMI was designed. The system is used to develop the work of the steel plate cutting machine that has been installed early in one of the production factories. This update is saving the capital of buying a new entire new product. The operator enters the plate length and plate number through the HMI which represents important part of the updating system. The position of the length of the plate that was driven by the motor can be sensed by the encoder. The signal of the encoder is sending to the PLC, which in turn sends a signal to the motor. The motor slow down gradually until it reaches the desired length, then it stops. After that, PLC sends a signal to the cutting motor to cut the plate, then the process is repeated again. In order to confirm the usefulness of the developed system, it was verified experimentally in real-time production line. The output production capacity of the updated system was increased due to the reducing in stopping time that occurs after each cutting of plate by system operator. Also, there is an increase in the safety of the system and a saving in labor from 3 persons to one. REFERENCES [1] D. G. Gahane, P. Katole, P. Naidu, R. Dhoke, and S. Kore, “Automatic pipe-wire cutting machine,” International Journal of Engineering Applied Sciences and Technology, vol. 5, no. 1, pp. 454–456, May 2020, doi: 10.33564/IJEAST.2020.v05i01.078. [2] M. Chattal, V. Bhan, H. Madiha, and S. A. Shaikh, “Industrial automation and control trough plc and labview,” in 2019 2nd International Conference on Computing, Mathematics and Engineering Technologies (iCoMET), Jan. 2019, pp. 1–5, doi: 10.1109/ICOMET.2019.8673448. [3] H. H. Hadi and M. Y. Sallom, “Pneumatic control system of automatic production line using SCADA implement PLC,” in 2019 4th Scientific International Conference Najaf (SICN), Apr. 2019, pp. 37–42, doi: 10.1109/SICN47020.2019.9019356. [4] R. Pawar and N. Bhasme, “Application of PLC’s for automation of processes in industries,” International Journal of Engineering Research and Applications, vol. 6, no. 6, pp. 53–59, 2016. [5] K. K. Kumar and S. N. Prasad, “A heuristic approach to retrofit and automation of machines using PLC,” International Journal of Advances in Engineering and Technology, vol. 7, no. 4, 2014. [6] A. D. Meshram, B. A. Godbole, T. P. Jaminkar, T. G. Lohambare, M. A. Kande, and D. R. A. Keswani, “PLC based control for induction motor,” International Journal of Advanced Research in Computer and Communication Engineering, vol. 9, no. 4, pp. 96–99, 2020. [7] A. E. Gafar and K. M. A. Said, “Intelligent PLC system to control wire cutting machine,” International Journal of Engineering Applied Sciences and Technology, vol. 03, no. 11, pp. 35–38, Mar. 2019, doi: 10.33564/IJEAST.2019.v03i11.007. [8] J. N. Kamau, “A step-by-step approach to retrofit and automation of PCB machines using PLC,” in Proceedings of the Sustainable Research and Innovation Conference, 2022, pp. 25–33.
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Diaz-Choque, “Supervision and control by SCADA of an automated fire system,” Indonesian Journal of Electrical Engineering and Computer Science (IJEECS), vol. 21, no. 1, pp. 92–100, Jan. 2021, doi: 10.11591/ijeecs.v21.i1.pp92-100. [24] M. K. Gupta, P. K. Gupta, R. K. Giri, and A. Gupta, “Smart electric control system using PLC and HMI,” International Journal of Mechanical Engineering and Technology, vol. 9, no. 4, pp. 548–555, 2018. [25] I. D. Pranowo and D. Artanto, “Improved control and monitor two different PLC using LabVIEW and NI-OPC server,” International Journal of Electrical and Computer Engineering (IJECE), vol. 11, no. 4, pp. 3003–3012, Aug. 2021, doi: 10.11591/ijece.v11i4.pp3003-3012. BIOGRAPHIES OF AUTHORS Basheer Najemaldeen Shaheed received the B.Eng. degree in electrical and communication engineering from Al-Furat Al-Awsat Technical University, Iraq, in 2018. Currently, working as an engineer in a private sector company. His research interests include communication networks, internet of thing, automation control, wireless sensor networks, renewable energy, power electronics, solar energy, power generation, electric vehicles, store energy, and artificial intelligence. He can be contacted at email: basheernajem7@gmail.com. Nasir Hussein Selman received the Bsc. Eng. degree in electrical engineering from university of technology, Iraq, in 1992 and Msc in 2004. Ph.D. degrees in electric power and machine engineering from Basrah University, Iraq, in 2016. Currently, he is a Lecturereat the Al-Najaf Technical Engineering College/Najaf, Al-Furat Al-Awsat Technical University ATU, Iraq. His research interests include renewable energy, power electronics, microcontroller, programming, power generation, smart grids, load flow control. He can be contacted at email: nhsm1969@yahoo.com.coj.nas@atu.edu.iq.