This document describes a microcontroller-based gas flow alert system for an industrial furnace. The system monitors the furnace's gas flow mode (manual vs automatic) and uses a GSM modem to send alert messages if the mode is not changed on schedule. This helps reduce wasted nitrogen gas flow and lower production costs by ensuring the optimal gas flow level is maintained based on whether items are actively being loaded into the furnace. The system was designed and assembled with a microcontroller board connected to a GSM modem. It provides alerts if the operator fails to change the furnace mode between shifts, allowing nitrogen usage and costs to be reduced by an estimated Rs. 10,407.93 per month.
PID-based temperature control device for electric kettleIJECEIAES
A normal electric kettle usually is intended to boil water until boiling point and cannot be controlled. Most of the kettle does not provide the temperature display for user to track the current temperature reading. Thus, this project is inspired from the shortcoming of most kettles that are sold at the market. By using Arduino microcontroller, a device is developed to control water temperature inside electric kettle. To provide automated temperature control, PID controller is chosen since it can provides precise water temperature control with less fluctuation. The device is also equipped with the display of the current water temperature and desired temperature. The device is tested to an electric kettle and the performance of PID controller in controlling water temperature is compared to on-off controller. An analysis is performed based on the amount of fluctuation with respect to desired temperature to verify the efficacy of the designed circuit and controller. It is found that the developed device and PID controller are capable to control the water temperature inside kettle based on the desired temperature set by user with less amount of fluctuation
Temperature based fan speed control & monitoring usingJagannath Dutta
Our object of making this project is for reducing the power consumption. And also to assist people who are disabled and are unable to control the speed of fan.
The aim of the project is to design a wireless helmet for coal miners using ZigBee wireless mine supervising machines. Nowadays coal miners are facial various problems. Workers safety in underground coal mines has always remained a challenging task. Several fatal and non-fatal accidents take place worldwide resulting in causalities and injuries of coal miners. Study aims to develop a wearable safety device comprising of gas sensor, temperature sensor, oxygen sensor, opguard, ultrasonic sensor, ultraviolet sensor. The values of different sensors are continuously transmitted by wireless transmitter to the remote monitoring unit which is placed outside the mine and received by the receiver module (PC).
PID-based temperature control device for electric kettleIJECEIAES
A normal electric kettle usually is intended to boil water until boiling point and cannot be controlled. Most of the kettle does not provide the temperature display for user to track the current temperature reading. Thus, this project is inspired from the shortcoming of most kettles that are sold at the market. By using Arduino microcontroller, a device is developed to control water temperature inside electric kettle. To provide automated temperature control, PID controller is chosen since it can provides precise water temperature control with less fluctuation. The device is also equipped with the display of the current water temperature and desired temperature. The device is tested to an electric kettle and the performance of PID controller in controlling water temperature is compared to on-off controller. An analysis is performed based on the amount of fluctuation with respect to desired temperature to verify the efficacy of the designed circuit and controller. It is found that the developed device and PID controller are capable to control the water temperature inside kettle based on the desired temperature set by user with less amount of fluctuation
Temperature based fan speed control & monitoring usingJagannath Dutta
Our object of making this project is for reducing the power consumption. And also to assist people who are disabled and are unable to control the speed of fan.
The aim of the project is to design a wireless helmet for coal miners using ZigBee wireless mine supervising machines. Nowadays coal miners are facial various problems. Workers safety in underground coal mines has always remained a challenging task. Several fatal and non-fatal accidents take place worldwide resulting in causalities and injuries of coal miners. Study aims to develop a wearable safety device comprising of gas sensor, temperature sensor, oxygen sensor, opguard, ultrasonic sensor, ultraviolet sensor. The values of different sensors are continuously transmitted by wireless transmitter to the remote monitoring unit which is placed outside the mine and received by the receiver module (PC).
The aim of the project is to design a wireless helmet for coal miners using ZigBee wireless mine supervising machines. Nowadays coal miners are facial various problems. Workers safety in underground coal mines has always remained a challenging task. Several fatal and non-fatal accidents take place worldwide resulting in causalities and injuries of coal miners. Study aims to develop a wearable safety device comprising of gas sensor, temperature sensor, oxygen sensor, opguard, ultrasonic sensor, ultraviolet sensor. The values of different sensors are continuously transmitted by wireless transmitter to the remote monitoring unit which is placed outside the mine and received by the receiver module (PC).
I have create slides which lists examples of oops programming concepts including looping,enums,structures,linq,threading,delegates,generics,inheritenc..so on.
The aim of the project is to design a wireless helmet for coal miners using ZigBee wireless mine supervising machines. Nowadays coal miners are facial various problems. Workers safety in underground coal mines has always remained a challenging task. Several fatal and non-fatal accidents take place worldwide resulting in causalities and injuries of coal miners. Study aims to develop a wearable safety device comprising of gas sensor, temperature sensor, oxygen sensor, opguard, ultrasonic sensor, ultraviolet sensor. The values of different sensors are continuously transmitted by wireless transmitter to the remote monitoring unit which is placed outside the mine and received by the receiver module (PC).
I have create slides which lists examples of oops programming concepts including looping,enums,structures,linq,threading,delegates,generics,inheritenc..so on.
BTech ECE project final report using ArduinoBhuvi85107
This is my original work. The notes I have made on some pages were learnt over time, you can incorporate them in your electronics hobbying (although this site is mostly used for copying projects and not learning haha). Feel free to use any part of the project.
IJRET : International Journal of Research in Engineering and Technology is an international peer reviewed, online journal published by eSAT Publishing House for the enhancement of research in various disciplines of Engineering and Technology. The aim and scope of the journal is to provide an academic medium and an important reference for the advancement and dissemination of research results that support high-level learning, teaching and research in the fields of Engineering and Technology. We bring together Scientists, Academician, Field Engineers, Scholars and Students of related fields of Engineering and Technology.
In this project an automated greenhouse robot was built with the purpose of controlling the greenhouse
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sensor and a temperature sensor. The 2sensors are controlling the two Relays which are a fan (for cooling) and
a bulb (for heating). The fan is used to change the temperature and the bulb is used to heat the plants. The
humidity control system and the temperature control system were tested both separately and together. The
result showed that the temperature and humidity could be maintained in the desired range.
Implementation of Industrial Boiler Monitoring System with GSMSivasankarK11
The working of the boiler is monitored by means of their parameters. The parameters are the key of the proper functioning of the boiler. The steam produced in the boiler is used for various industrial applications. The application vary from the industrial purposes which may be for the power generation. Here the steam ids used for the testing of valves. The parameters of the boiler like temperature, pressure, pH and flow level are monitored. The parameters thus monitored are sent through the GSM (Global system for mobile Communication) to the control room of the industry.
1. International Journal of Research in Advent Technology, Vol.2, No.2, April 2014
E-ISSN: 2321-9637
155
Micro Controller Based Alert System for Gas Flow
In an Industrial Furnace
ARULARASAN.R1, PREMKUMAR.M2, SARATHKUMAR.M2, JAGATHEESAN.G2,
MUBARAK.B2.
1, Faculty, 2, UG Students,
Department of Mechanical Engineering, University College of Engineering Arni
Thatchur, Thiruvannamalai (DT) - 632326, India
Email: mpkr163@gmail.com2, sarath.ucea@gmail.com2, vrarasan@gmail.com1
Abstract: In a NOCOLOK brazing furnace Nitrogen is passed through the different zones. Usage of Nitrogen is
to reduce the amount of the Oxygen level. This Nitrogen is injected in five different pipes. Each pipe has one
gate valve and one solenoid system for flowing. Generally, Furnace has two modes. One is Manual mode and
second is Auto mode. If auto mode is on, the flow is passed in both Solenoid system and gate valve. If Manual
mode is on, the flow is passed in the Gate Valve only. At end of the first shift, the mode will change by operator.
Because the cores are not loading into the furnace. So the operator will change into Manual mode. In the Manual
mode, Nitrogen flow is reduced. Similarly, at the starting of the next shift, the operator changed into Auto mode.
But the drawback is, if operator does not change the mode at particular time. So Nitrogen flow is wasted. Our
scope is to reduce the usage of Nitrogen flow by using GSM Modem. The output signal from the Auto or
Manual mode Switch connected with Micro controller Board. The output from this board is connected with
GSM modem input. So, the changed mode is detected and it gives alarm and message output to the operator and
top level group.
Index Terms- BRAZING, FURNACE, NITROGEN, GSM FLOW ALERT, MICRO CONTROLLER
1. BRAZING PROCESS:
In a special type of NOCOLOK Furnace
brazing process can be carried out for fabricating
purposes. Brazing is a process for joining similar or
dissimilar metals using a filler metal. Brazing covers a
temperature range of 900ºF - 2200ºF (470ºC -
1190ºC). Brazing differs from welding in that brazing
does not melt the base metals; therefore brazing
temperatures are lower than the melting points of the
base metals.
Fig.1 NOCOLOK Brazing Furnace layout
2. International Journal of Research in Advent Technology, Vol.2, No.2, April 2014
E-ISSN: 2321-9637
156
2. BLOCK DIAGRAM OF FLOW ALERT SYSTEM:
.
Fig.2. Block diagram of flow alert
system
3. ASSEMBLED DIAGRAM OF MICRO CONTROLLER WITH
GSM
Fig.3. Assembled diagram of Micro controller with GSM
3. International Journal of Research in Advent Technology, Vol.2, No.2, April 2014
E-ISSN: 2321-9637
157
4. FLOW ALERT SYSTEM - METHOD
DESCRIPTION:
In a NOCOLOK BRAZING furnace
Nitrogen is passed through the different zones. Usage
of Nitrogen is to reduce the amount of the Oxygen
level. This Nitrogen is injected in five different pipes.
Each pipe has one gate valve and one solenoid system
for flowing. Generally, Furnace has two modes. One
is Manual mode and second is Auto mode. If auto
mode is on, the flow is passed in both Solenoid
system and gate valve. If Manual mode is on, the flow
is passed in the Gate Valve only.
At the end of the first shift, the operator will
change the mode into Manual. Because the cores are
not loaded into the furnace. In this mode, flow of
Nitrogen is partially reduced. Similarly, at the starting
of the next shift, the operator changed into Auto
mode. But the drawback is, if operator does not
change the mode at particular time. So Nitrogen flow
is wasted. So we change the system initially, output
from the Manual or Auto mode in the furnace, is
connected into level shifter.
Level shifter is used for prevent high voltage
from affecting the system receiving the signal. Then
the output signal is connected with Micro Controller.
The Micro Controller is connected with LCD, GSM
Modem and Hooter. If the operator changes the mode,
output from the mode is sending to the Micro
Controller. Then GSM modem gives the SMS based
alert to the operator and the top level group.
5. PROCUCTIVITY IMPROVEMENT:
S.N
O.
DESCRI
PTION
BEFORE AFTER
1. PEOPLE
Operator cannot
change the
mode at correct
time.
This system
alerts the
operator to
change the
mode at
correct time.
2. MAN
POWER
Additional
operators
required.
Addition-al
operators are
not required.
3. QUALIT
Y
Mode is not
changed at a
correct time.
The quality of
product is poor.
Here, the
mode is
changed at
correct time.
So, the
quality of
product is
good.
4. PRODUC
T
More no. of
rejected parts.
Less no. of
rejected
parts.
5. COST
Usage of
Nitrogen is
high. So total
cost high.
Usage of
Nitrogen is
reduced. So
total cost is
reduced.
6. COST REDUCTION:
• In Auto mode Nitrogen flow is = 120m3/hr =
2m3/min
• In Manual mode Nitrogen flow is = 80m3/hr
= 1.33m3/min
• Therefore, we reduce the Nitrogen flow is
0.67m3/min
1 kg of Nitrogen = Rs. 8.63
0.67 of Nitrogen = Rs. 5.782 (per min)
If we change the mode on after 5 min = Rs. 28.9
If we change the mode on after 1 hour = Rs. 346
If we change the mode on after (every day1 hour
delay)1 month = Rs.10407.93
7. CONCLUSION:
With the proper usage of this GSM based
flow alert system, alerts and messages to the
operator to change the mode in correct time
can be sent.
Due to change of mode in correct time,
Flow of nitrogen usage can be reduced. So
cost of brazing can be reduced.
So productions cost can be reduced
significantly.
So the quality of the product is improved.
Improved safety and smooth operation of
process and provide proper working
environment.
Our total cost of the components is Rs.7149.
Reduced Nitrogen cost for one month (every
day 1hour delay) is Rs.10407.93. So we get
back the amount within one month. So this
economical.
4. International Journal of Research in Advent Technology, Vol.2, No.2, April 2014
E-ISSN: 2321-9637
158
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1. Vandana Pandya, Deepali Shukla, Medicaps
Institute of Technology and Management, Indore
(M.P). India- International Journal of
Computational Engineering Research.
2. www.nxp.com
3. www.atmel.com
4. Dale H.Besterfiled, “Total Quality Management”,
Pearson Education Asia.
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International Journal of smart Home.
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