The document summarizes an improvement project to increase productivity in bulk operations at a noodle manufacturing plant. It provides data showing current productivity levels are 14 kg/man hour on average across manual and machine bulk filling. A project charter was developed with the goal of increasing productivity by 30% through analyzing processes, collecting data on output and stoppages, and identifying causes of low productivity such as the bulk machine running slow and lack of training. The document outlines the project team, timeline, and plan to measure improvements through increased daily production and optimized manpower utilization.
A student organization called JMC is hosting a Dead Week event called The Waking Dead from 8-10am and 8-10pm where $2 coffee will be available. The event is taking place at Gaylord College and credit cards will be accepted for payment.
Normal waking consciousness is characterized by:
1) Different levels of awareness including controlled processes that require conscious effort and automatic processes that require little effort.
2) Content is generally organized and logical but may be limited through selective attention.
3) Awareness of time as moving at a normal rate and the ability to focus on the past, present and future.
The document summarizes the goals, technical constraints, and solutions for rendering wounds in Left 4 Dead 2. It aimed to accurately locate wounds, match weapon strength by removing body parts, and allow multiple active wounds per model. Constraints included memory and CPU limits. The initial prototype used ellipsoids to cull pixels and fill holes with wound models, but had issues. The final solution combined ellipsoids with projected textures to create natural-looking wounds, blood effects, and up to 54 unique wounds per model with minimal performance impact.
The Walking Dead comic book volume 2, Miles Behind Us
The Walking Dead centers around Rick Grimes, a former police officer who was shot in the line of duty and wakes up from a coma after the world has succumbed to the zombie plague. Dazed from months in the hospital, and confused as to why he can't find anyone alive, he makes his way home only to find his wife and son missing. He packs up supplies from his station and travels to Atlanta in search of his family after hearing the cities would be safe (heard from Morgan and Duane Jones, his previous neighbors). Arriving in the city on horseback, Rick is overcome by a horde of zombies and narrowly escapes death with the aid of another survivor named Glenn, who has been scavenging the city for supplies. Glenn takes Rick back to his camp just outside of town where Rick's wife Lori and son Carl happen to be living, alive and well. His partner and best friend Shane had taken Lori and Carl to the outskirts of Atlanta to wait for rescue by the US Government. There they found a small group of survivors.
Paul state, "And you were dead in the trespasses and sins in which you once walked, following the course of this world, following the prince of the power of the air, the spirit that is now at work in the sons of disobedience..." Free PowerPoint Download at http://BibleGuy.org
It was really excited to run my First Lean Six Sigma Black Belt Project in my factory . And during the project im really great full to my honorable management . Now im posting this project for the audience of this site .
The document discusses effective inventory planning and control strategies for a corrugated box manufacturing plant. It provides an overview of the company profile and facilities. It then defines the current problems with raw material procurement and storage capacity. The objectives are to forecast demand, revise the replenishment policy and create a new master production schedule. The methodology involves data collection, forecasting analysis using Holt's, seasonal and moving average models, and comparing the existing versus proposed replenishment policies and schedules. The results show implementing a revised policy with domestic materials procured twice monthly improves inventory management.
1. The document summarizes productivity improvement efforts for a production line at WABCO. A team analyzed data on cycle times, outputs, WIP levels, and identified causes for low productivity such as imbalanced cycle times and unnecessary movements.
2. The team conducted experiments to optimize cycle times on critical machines like CNC machines through Design of Experiments. They also combined operations, improved fixtures, implemented a cell layout, and modified material handling.
3. These countermeasures helped reduce cycle times and WIP, increase output to meet rising demand, and boost productivity and efficiency on the production line.
A student organization called JMC is hosting a Dead Week event called The Waking Dead from 8-10am and 8-10pm where $2 coffee will be available. The event is taking place at Gaylord College and credit cards will be accepted for payment.
Normal waking consciousness is characterized by:
1) Different levels of awareness including controlled processes that require conscious effort and automatic processes that require little effort.
2) Content is generally organized and logical but may be limited through selective attention.
3) Awareness of time as moving at a normal rate and the ability to focus on the past, present and future.
The document summarizes the goals, technical constraints, and solutions for rendering wounds in Left 4 Dead 2. It aimed to accurately locate wounds, match weapon strength by removing body parts, and allow multiple active wounds per model. Constraints included memory and CPU limits. The initial prototype used ellipsoids to cull pixels and fill holes with wound models, but had issues. The final solution combined ellipsoids with projected textures to create natural-looking wounds, blood effects, and up to 54 unique wounds per model with minimal performance impact.
The Walking Dead comic book volume 2, Miles Behind Us
The Walking Dead centers around Rick Grimes, a former police officer who was shot in the line of duty and wakes up from a coma after the world has succumbed to the zombie plague. Dazed from months in the hospital, and confused as to why he can't find anyone alive, he makes his way home only to find his wife and son missing. He packs up supplies from his station and travels to Atlanta in search of his family after hearing the cities would be safe (heard from Morgan and Duane Jones, his previous neighbors). Arriving in the city on horseback, Rick is overcome by a horde of zombies and narrowly escapes death with the aid of another survivor named Glenn, who has been scavenging the city for supplies. Glenn takes Rick back to his camp just outside of town where Rick's wife Lori and son Carl happen to be living, alive and well. His partner and best friend Shane had taken Lori and Carl to the outskirts of Atlanta to wait for rescue by the US Government. There they found a small group of survivors.
Paul state, "And you were dead in the trespasses and sins in which you once walked, following the course of this world, following the prince of the power of the air, the spirit that is now at work in the sons of disobedience..." Free PowerPoint Download at http://BibleGuy.org
It was really excited to run my First Lean Six Sigma Black Belt Project in my factory . And during the project im really great full to my honorable management . Now im posting this project for the audience of this site .
The document discusses effective inventory planning and control strategies for a corrugated box manufacturing plant. It provides an overview of the company profile and facilities. It then defines the current problems with raw material procurement and storage capacity. The objectives are to forecast demand, revise the replenishment policy and create a new master production schedule. The methodology involves data collection, forecasting analysis using Holt's, seasonal and moving average models, and comparing the existing versus proposed replenishment policies and schedules. The results show implementing a revised policy with domestic materials procured twice monthly improves inventory management.
1. The document summarizes productivity improvement efforts for a production line at WABCO. A team analyzed data on cycle times, outputs, WIP levels, and identified causes for low productivity such as imbalanced cycle times and unnecessary movements.
2. The team conducted experiments to optimize cycle times on critical machines like CNC machines through Design of Experiments. They also combined operations, improved fixtures, implemented a cell layout, and modified material handling.
3. These countermeasures helped reduce cycle times and WIP, increase output to meet rising demand, and boost productivity and efficiency on the production line.
This document analyzes safety stock levels at a roll manufacturing company in India called TAYO ROLLS LTD. The author collected sales data for A-class inventory items and used Monte Carlo simulation to determine the optimal safety stock level that minimizes total inventory costs. The simulation considered holding costs when supply exceeds demand and lost contribution margin when demand exceeds supply. Based on a simulated sales dataset and calculation of monthly costs, the analysis found that maintaining a safety stock level of 7 units minimized total costs of Rs. 42960. Therefore, the author's conclusion is that the company should keep a safety stock of 7 units for each item each month to balance inventory costs.
Production Planning Industrial Engineering Management E-BookLuis Cabrera
This document discusses production planning and factors that affect demand and production planning. It provides an example showing material quantities over time, including material in, processed, wasted, leftover, and available. Plant facilities production process, maintenance, and supply chain management impact production yields and performance. Finished goods demand seasonality and market factors are also important to consider in production and demand planning. The document emphasizes understanding the full production process cycle and related operational areas.
Integrating New Products and the Sales Funnel in Demand Planningfreighthunter
This document provides information on how to integrate new products and sales forecasts into demand planning discussions to improve sales and operations planning (S&OP). It discusses reviewing product pipelines and new product launches, incorporating assumptions and risks into forecasts, and comparing forecasts to past performance by customer to improve accuracy. The goal is to align sales, supply, and financial plans through collaborative demand meetings.
Optimization of Capacity Utilization in a Manufacturing Industry – A Case StudyIJMER
In today’s competitive market, every organization is striving hard to excel to utilize capacities effectively which determines the position of the organization in the Market. To achieve effective utilization a lot of planning is required with respect to capacity utilization. Capacity Planning and Capacity Management are today’s modern organization requirement. The capacity plans needs to be executed flawlessly without unpleasant surprises .To match the capacity with the plans, an attempt has been made to evaluate capacity utilization index in a cement manufacturing industry. Overall equipment effectiveness is calculated with three separate but measurable components availability, performance and quality. Many manufacturing companies benchmark their industry to set challenging target at 85% capacity utilization, even though 100% OEE is possible
This document summarizes a project to reduce production lead time at a automotive parts manufacturing company using value stream mapping. It describes collecting data on current processes, creating a current state map showing a 12.6 hour lead time, identifying wastes like transportation delays, and proposing a future state map with a reduced 2.25 hour lead time through improvements like relocating machines, improved material handling, and adding a new welding machine. The project aimed to improve productivity, understand waste, and provide a plan for a more efficient lean production line.
PRODUCTIVITY IMPROVEMENT OF PRE-TREATMENTS & POWDER COATING PROCESS.Raheem Arif
This document summarizes a project to improve the productivity of pre-treatment and powder coating processes at a manufacturing plant. The objectives were to increase the capacity of two bottleneck workstations: pre-treatment and powder coating. The project modified the hanger design to hold more jobs simultaneously. Testing showed the improved design increased monthly production from 328,000 to 342,000 springs while increasing resource consumption as expected. Operator training ensured proper handling of the new process. Overall the project helped address capacity shortfalls and better fulfill production demands.
Subrat Kumar Pradhan has over 5 years of experience in plastics manufacturing operations, maintenance, quality assurance and control, and team management. He is currently working as a Shift In Charge at Genoa Plastic Industries in Kuwait City, where he is responsible for daily production planning, machine maintenance, quality monitoring, and ensuring 5S standards. Previously he has worked as a Shift Engineer at Oasis Flower Plant in Saudi Arabia and as a Technical Engineer Trainee at Elringklinger Automotive in Pune, India. He holds a B-Tech degree in Production and Industrial Engineering and a diploma in Plastic Engineering.
What is the Circular Economy and How can Data and AI drive Outcomes.pptxpaul young cpa, cga
This document discusses the circular economy and how data and AI can help drive better outcomes. It begins with an introduction of the speaker, Paul Young, and his background. It then defines the circular economy and discusses challenges it faces. Data and AI can help with metrics, reporting, forecasting costs and risk mitigation. Key metrics for circularity are identified. Solutions for ESG reporting from IBM, like Planning Analytics and Cognos Analytics, are demonstrated. Overall, circular policies and the right technology are needed to capture and analyze data to improve business outcomes and progress towards sustainability goals.
This document summarizes a webinar on enhancing performance using a programme dashboard. It provides information on the Programme Management SIG, including its vision and workstreams. It also lists upcoming events like the Programme Management Conference in March 2016 in London. The document outlines the speaker programme for the webinar. Finally, it introduces the presentation topic of enhancing performance using a programme dashboard and provides a brief biography of the speaker, Simon Springate.
Effectiveness of preventive maintenance in critical equip at Apollo tyresJustine Thomachan
This document analyzes the effectiveness of preventative maintenance for two critical pieces of equipment, a calendar and dual extruder, at Apollo Tyres over a 10 month period. It calculates the overall equipment effectiveness (OEE) using metrics like availability, performance, and quality. Pareto analysis identified the top 5 breakdown causes for each machine. Eliminating these primary issues could reduce breakdowns by 72-80%, and increase availability by 3-7% and OEE by 3-6%, saving over Rs. 90,000-120,000 in labor costs. The study aims to improve equipment uptime and identify opportunities to enhance availability.
Harish Kumar Shahi completed a summer internship at Axalta Coating Systems where he worked on three projects: optimization of extruders, analysis of product wheel sequencing, and development of a planning software tool. He analyzed the constraints and throughput of eight extruders, identifying issues like cooling problems. This led to an average 10% increase in throughput. He also analyzed moving from bucket to product wheel sequencing, finding potential inventory and cost savings. Finally, he developed a software tool to optimize production planning and inventory levels.
IMPROVING OSH & PRODUCTIVITY OF RMG INDUSTRIES BY IMPLEMENTING LEAN TOOLS AN...Karina Islam
The garment industry has played a pioneering role in the development of industrial sector of Bangladesh. The RMG sector is expected to grow despite the global financial crisis of 2009.As China is finding it challenging to make textile and foot wear items at cheap price, due to rising labor costs, many foreign investors, are coming to Bangladesh to take advantage of the low labor cost. Though Bangladesh produces garment with lowest cost but poor productivity. To survive and prosper in today's economic times, companies can no longer manage using financial measures alone, they have to track non-financial measures also such as customer satisfaction, brand preference, speed of response, employee satisfaction etc.Productivity can improve by applying lean tools like- 5s, JIT, Muda, Root Cause analysis, KPIs, VSM. For improving the ultimate productivity OHS of RMG sector of Bangladesh should be improved. In Ready Made Garments (RMG) sector of Bangladesh, the employees represent an organization's biggest and its most valuable asset. The company's productivity, and ultimately, its profitability depend on making sure all of its workers perform up to their full potential. This paper summarizes that how KPIs analysis improve productivity and OHS of RMG sectors. Appropriate indicators are first selected for KPI scoring then simulate the scores with the help of Adaptive Network-based Fuzzy Inference System (ANFIS) and finally illustrated how KPIs impacts on overall productivity.
IRJET- Design Development and Automation of Roasting SystemIRJET Journal
The document describes the design and development of an automated groundnut roasting system. The goals of the project were to redesign an existing roasting system to be more automated, efficient, and cost-effective. The team analyzed customer needs and existing products to generate design concepts. They developed a roasting system with an automated feeding mechanism, detachable components for easy fabrication, and temperature control. Design calculations and structural analysis using ANSYS software were conducted to validate the design. The automated system provides continuous output, zero pollution roasting with uniform heating and temperature control.
The document provides details about Tayo Rolls Ltd, including its production planning process. It discusses [1] the company's various departments involved in production planning, [2] factors that affect machine shop production planning such as product mix and cycle times, and [3] the objectives and key elements of an effective production planning and control system.
IRJET - Invistigation and Implement of Six Sigma and Reduce Labour Cost a...IRJET Journal
This document discusses an investigation into implementing Six Sigma methods to reduce rejection rates and labor costs in a plastic injection molding process. It begins with an introduction to injection molding and Six Sigma. A case study of an Indian plastic parts manufacturer is presented, where the process was experiencing high rejection rates of 10%. Six Sigma methods were used to identify causes of defects like missing inserts. Solutions included adding a timer to the process logic controller to stop the process if inserts were missing. This reduced rejection rates to only 5% and saved an estimated Rs. 172,800 per year in labor costs by reducing downtime. In conclusion, Six Sigma implementation improved quality, productivity and profits for the company by minimizing variations and defects.
080324 Miller Opportunity Matrix Asq Presentationrwmill9716
The document describes a methodology called the "Opportunity Matrix" used by Six Sigma teams at Solutia to systematically identify and address root causes impacting manufacturing process performance. The method involves brainstorming by process experts to develop a list of potential issues, ranking them to create the matrix, and having team members champion high-priority causes. Examples are given of four teams that successfully applied this approach to improve yields and reduce costs, including identifying issues like head pressure variations on winders. In conclusion, the approach continues to generate over $10 million in annual savings for Solutia.
This document analyzes safety stock levels at a roll manufacturing company in India called TAYO ROLLS LTD. The author collected sales data for A-class inventory items and used Monte Carlo simulation to determine the optimal safety stock level that minimizes total inventory costs. The simulation considered holding costs when supply exceeds demand and lost contribution margin when demand exceeds supply. Based on a simulated sales dataset and calculation of monthly costs, the analysis found that maintaining a safety stock level of 7 units minimized total costs of Rs. 42960. Therefore, the author's conclusion is that the company should keep a safety stock of 7 units for each item each month to balance inventory costs.
Production Planning Industrial Engineering Management E-BookLuis Cabrera
This document discusses production planning and factors that affect demand and production planning. It provides an example showing material quantities over time, including material in, processed, wasted, leftover, and available. Plant facilities production process, maintenance, and supply chain management impact production yields and performance. Finished goods demand seasonality and market factors are also important to consider in production and demand planning. The document emphasizes understanding the full production process cycle and related operational areas.
Integrating New Products and the Sales Funnel in Demand Planningfreighthunter
This document provides information on how to integrate new products and sales forecasts into demand planning discussions to improve sales and operations planning (S&OP). It discusses reviewing product pipelines and new product launches, incorporating assumptions and risks into forecasts, and comparing forecasts to past performance by customer to improve accuracy. The goal is to align sales, supply, and financial plans through collaborative demand meetings.
Optimization of Capacity Utilization in a Manufacturing Industry – A Case StudyIJMER
In today’s competitive market, every organization is striving hard to excel to utilize capacities effectively which determines the position of the organization in the Market. To achieve effective utilization a lot of planning is required with respect to capacity utilization. Capacity Planning and Capacity Management are today’s modern organization requirement. The capacity plans needs to be executed flawlessly without unpleasant surprises .To match the capacity with the plans, an attempt has been made to evaluate capacity utilization index in a cement manufacturing industry. Overall equipment effectiveness is calculated with three separate but measurable components availability, performance and quality. Many manufacturing companies benchmark their industry to set challenging target at 85% capacity utilization, even though 100% OEE is possible
This document summarizes a project to reduce production lead time at a automotive parts manufacturing company using value stream mapping. It describes collecting data on current processes, creating a current state map showing a 12.6 hour lead time, identifying wastes like transportation delays, and proposing a future state map with a reduced 2.25 hour lead time through improvements like relocating machines, improved material handling, and adding a new welding machine. The project aimed to improve productivity, understand waste, and provide a plan for a more efficient lean production line.
PRODUCTIVITY IMPROVEMENT OF PRE-TREATMENTS & POWDER COATING PROCESS.Raheem Arif
This document summarizes a project to improve the productivity of pre-treatment and powder coating processes at a manufacturing plant. The objectives were to increase the capacity of two bottleneck workstations: pre-treatment and powder coating. The project modified the hanger design to hold more jobs simultaneously. Testing showed the improved design increased monthly production from 328,000 to 342,000 springs while increasing resource consumption as expected. Operator training ensured proper handling of the new process. Overall the project helped address capacity shortfalls and better fulfill production demands.
Subrat Kumar Pradhan has over 5 years of experience in plastics manufacturing operations, maintenance, quality assurance and control, and team management. He is currently working as a Shift In Charge at Genoa Plastic Industries in Kuwait City, where he is responsible for daily production planning, machine maintenance, quality monitoring, and ensuring 5S standards. Previously he has worked as a Shift Engineer at Oasis Flower Plant in Saudi Arabia and as a Technical Engineer Trainee at Elringklinger Automotive in Pune, India. He holds a B-Tech degree in Production and Industrial Engineering and a diploma in Plastic Engineering.
What is the Circular Economy and How can Data and AI drive Outcomes.pptxpaul young cpa, cga
This document discusses the circular economy and how data and AI can help drive better outcomes. It begins with an introduction of the speaker, Paul Young, and his background. It then defines the circular economy and discusses challenges it faces. Data and AI can help with metrics, reporting, forecasting costs and risk mitigation. Key metrics for circularity are identified. Solutions for ESG reporting from IBM, like Planning Analytics and Cognos Analytics, are demonstrated. Overall, circular policies and the right technology are needed to capture and analyze data to improve business outcomes and progress towards sustainability goals.
This document summarizes a webinar on enhancing performance using a programme dashboard. It provides information on the Programme Management SIG, including its vision and workstreams. It also lists upcoming events like the Programme Management Conference in March 2016 in London. The document outlines the speaker programme for the webinar. Finally, it introduces the presentation topic of enhancing performance using a programme dashboard and provides a brief biography of the speaker, Simon Springate.
Effectiveness of preventive maintenance in critical equip at Apollo tyresJustine Thomachan
This document analyzes the effectiveness of preventative maintenance for two critical pieces of equipment, a calendar and dual extruder, at Apollo Tyres over a 10 month period. It calculates the overall equipment effectiveness (OEE) using metrics like availability, performance, and quality. Pareto analysis identified the top 5 breakdown causes for each machine. Eliminating these primary issues could reduce breakdowns by 72-80%, and increase availability by 3-7% and OEE by 3-6%, saving over Rs. 90,000-120,000 in labor costs. The study aims to improve equipment uptime and identify opportunities to enhance availability.
Harish Kumar Shahi completed a summer internship at Axalta Coating Systems where he worked on three projects: optimization of extruders, analysis of product wheel sequencing, and development of a planning software tool. He analyzed the constraints and throughput of eight extruders, identifying issues like cooling problems. This led to an average 10% increase in throughput. He also analyzed moving from bucket to product wheel sequencing, finding potential inventory and cost savings. Finally, he developed a software tool to optimize production planning and inventory levels.
IMPROVING OSH & PRODUCTIVITY OF RMG INDUSTRIES BY IMPLEMENTING LEAN TOOLS AN...Karina Islam
The garment industry has played a pioneering role in the development of industrial sector of Bangladesh. The RMG sector is expected to grow despite the global financial crisis of 2009.As China is finding it challenging to make textile and foot wear items at cheap price, due to rising labor costs, many foreign investors, are coming to Bangladesh to take advantage of the low labor cost. Though Bangladesh produces garment with lowest cost but poor productivity. To survive and prosper in today's economic times, companies can no longer manage using financial measures alone, they have to track non-financial measures also such as customer satisfaction, brand preference, speed of response, employee satisfaction etc.Productivity can improve by applying lean tools like- 5s, JIT, Muda, Root Cause analysis, KPIs, VSM. For improving the ultimate productivity OHS of RMG sector of Bangladesh should be improved. In Ready Made Garments (RMG) sector of Bangladesh, the employees represent an organization's biggest and its most valuable asset. The company's productivity, and ultimately, its profitability depend on making sure all of its workers perform up to their full potential. This paper summarizes that how KPIs analysis improve productivity and OHS of RMG sectors. Appropriate indicators are first selected for KPI scoring then simulate the scores with the help of Adaptive Network-based Fuzzy Inference System (ANFIS) and finally illustrated how KPIs impacts on overall productivity.
IRJET- Design Development and Automation of Roasting SystemIRJET Journal
The document describes the design and development of an automated groundnut roasting system. The goals of the project were to redesign an existing roasting system to be more automated, efficient, and cost-effective. The team analyzed customer needs and existing products to generate design concepts. They developed a roasting system with an automated feeding mechanism, detachable components for easy fabrication, and temperature control. Design calculations and structural analysis using ANSYS software were conducted to validate the design. The automated system provides continuous output, zero pollution roasting with uniform heating and temperature control.
The document provides details about Tayo Rolls Ltd, including its production planning process. It discusses [1] the company's various departments involved in production planning, [2] factors that affect machine shop production planning such as product mix and cycle times, and [3] the objectives and key elements of an effective production planning and control system.
IRJET - Invistigation and Implement of Six Sigma and Reduce Labour Cost a...IRJET Journal
This document discusses an investigation into implementing Six Sigma methods to reduce rejection rates and labor costs in a plastic injection molding process. It begins with an introduction to injection molding and Six Sigma. A case study of an Indian plastic parts manufacturer is presented, where the process was experiencing high rejection rates of 10%. Six Sigma methods were used to identify causes of defects like missing inserts. Solutions included adding a timer to the process logic controller to stop the process if inserts were missing. This reduced rejection rates to only 5% and saved an estimated Rs. 172,800 per year in labor costs by reducing downtime. In conclusion, Six Sigma implementation improved quality, productivity and profits for the company by minimizing variations and defects.
080324 Miller Opportunity Matrix Asq Presentationrwmill9716
The document describes a methodology called the "Opportunity Matrix" used by Six Sigma teams at Solutia to systematically identify and address root causes impacting manufacturing process performance. The method involves brainstorming by process experts to develop a list of potential issues, ranking them to create the matrix, and having team members champion high-priority causes. Examples are given of four teams that successfully applied this approach to improve yields and reduce costs, including identifying issues like head pressure variations on winders. In conclusion, the approach continues to generate over $10 million in annual savings for Solutia.
Identifying, Mitigating and Eliminating Risk with an Asset Management Strategy
Gurnoor Technical Trainee Review 2011-2012 Final
1.
2. • Days without Lost Time Injury * - 121
• IP Man hours without LT Injury * - 3135
• Last Lost Time Injury - None
* From 1st Jan 2012 to 30th April 2012
Safe by Choice
4. Noodle Mfg and Filling Process
TM Mfg and Filling Process
Vending Mix Manufacturing and Filling Process
GMP, CCP, OPRPs, PRPs, KLOs
Net Weight Control (RCPs)
Overview of Consumer Complaint Handling
Food Safety and Compliances
Factor’s Key Quality Indicators( FTQ, FTR, OTR,
ER , Consumer Complaints etc) , their trend and impact.
Supplier Audits for strengthening internal controls
COP of Noodles
MIS – understanding & interpretation
Variances on Budget
Production
Quality
Finance
&
Control
Overview of Learning's from Other Departments
5. Basics
• GI 23.010-2
• Role of IP in Industry
• SCB Line Standards
Systems
•SAP ( Master Recipe, Production Version, Resource)
•SAM ( Updation of Standards, Stoppage Classification, Troubleshooting )
•Manufacturing Standards Sheet
•Capacity Summary Tool
•Minitab
•I-nexus
NCE
• Problem Solving –GSTD & DMAIC
• Goal Alignment
Productivity
• Definition and Meaning
• Calculation , Reporting , Impact & Scope of Improvement
• Contract Labor – Tracking and Variance Calculations
Other Key
Learning's
• Loss Tree Analysis-Overview
• Piece Rate
• Workload Study
• Noodle Benchmarking Exercise
• Understanding of Key Performance Indicators of All Departments
Learning's from Industrial Performance
6. Improvement in Bulk operation productivity
Project Leader: Gurnoor Singh Kakkar
Market/Org: Nestle Pantnagar
Sponsor: IJS Kahlon
Coach: VPS Tyagi
Process Owner : Amit Kumar
Project Period: January,2012 to April, 2012
i-nexus ID: 55877
DMAIC level: Basic
7. Historical Data & Trends of Productivity
NCE / DMAIC program
14.0
13.5
10.9
13.0
16.0
13.5
8.0
9.0
10.0
11.0
12.0
13.0
14.0
15.0
16.0
17.0
18.0
August September October November December YTD
Productivity Average
Kg/Man Hr
ProblemProblem
Define Phase
8. “Specific but Stretching Measurable Agreed, aligned, achievable & attractive Realistic & Relevant Time bound”
Objective: Improvement in Bulk Operation Productivity by April by 30%
Project Charter
Project Title: Improvement in Bulk Operation Productivity by 30 %
Problem Statement:
Low productivity of Noodle Bulk Filling & Packing
Operation (equal to 14 kg/ man hour)
1 SCOPE (What is the start/end of the process? Escalation decision?
Budget limits? Use the IS/IS NOT tool to define the scope)
Noodle Bulk Filling and Packing Operation in Phase 1 &
Phase 2
TOLLGATES (Review with the team and sponsor):
Deliverables (Process changes, training, documentation that ensure sustainability)
Increase in Daily Bulk Production
New Layout of Bulk Operation
New Manpower Standards for Bulk including less manpower requirements.
Fixed Contractual Crew for Bulk Machine
Problem
Measures that will be used to judge success. Include baseline and
target:
Increase in Productivity by 30 % (i.e. 18.2 kg/ manhr)
Business Case (Why is it important for the customer?)
Improvement in productivity of Bulk Operation will lead to optimization of
resources and getting closer to our goal of ZERO WASTE resulting in potential
savings 2 Mio. It will also help to cater increased market demand of bulk pack to
fulfill business needs.
Potential Benefits:
• Better management of manpower in bulk operations
• Improvement in Productivity i.e. more output for the same input of manhours
• Rework Reduction
•Optimization of manpower
2
3
4 5
20/01/2012
15/02/201201/03/2012
31/03/2012
It’s 20% the tools & 80% how you use them! Use only the tools that are relevant to stimulate and guide your thinking so the objective can be reached.
Document Owner:- Project Sponsor
30/04/2012
9. NCE / DMAIC program
Team Leader
Coachgives expert guidance
and coaching to the team on the
DMAIC tools and cycle.
VPS Tyagi
(IP Manager)
Team Leaderleads
the team, manages team dynamics &
team’s progress against schedule.
Serves as a liaison with Sponsor,
Coach and Process Owner. Maintains
records & documentation.
Gurnoor
Singh
(IP)
Sponsor Approves project
and scope. Accountable for the
project result. Reviews progress
(tollgates). Removes roadblocks for
the team. Celebrates the project’s
conclusion.
Inder Mohan
Singh Kahlon
(Factory
Manager)
Process Owner
is the customer of the project who the
team needs to delight.
Amit Kumar
Production
Manger
(Green Belt)Team Member
Team Member
Team Member
Jitendra Singh
(Engineering)
Team Member
6 Team Charter
Resource might be
called upon by the team for additional
information & expertise.
It’s 20% the tools & 80% how you use them! Use only the tools that are relevant to stimulate and guide your thinking so the
Document Owner:- Project Sponsor
ProblemProblem
Chander Deep
(Engineering)
Bhupesh
Chandel
(Process
Specialist)
Abhishek
Shukla
Gaurav Katheriya
IP
Team Member
Amit Kumar
(Technician)
Shanti Ballabh
(Technician)
Team Member
Ravi Sharma
(Quality
Assurance)
10. NCE/FI 10Project Title – Open the Master Slide
ProblemProblem
Phase 2 Manual Bulk Operation
Phase 1 Manual Bulk Operation Phase 1
Bulk
machine
Packing
Process Layout – December 2011
Measure Phase
11. NCE/FI 11
Process Layout (Snapshot – January 2012)
Project Title – Open the Master Slide
ProblemProblem
Phase 2
Manual Bulk
Packing
Phase 1 Bulk
Machine
Packing
Cont Manpower Allocated =15/shift (45/day)
Permanent Manpower = 1/shift (3/day)
Average Output = 1200 cases/day
Cont Manpower Allocated =10/shift (30/day)
Permanent Manpower = 2/shift (6/day)
Average Output = 450 cases/day
Cont. Manpower Allocated =15/shift (45/day)
Permanent Manpower = 1/shift (3/day)
Average Output = 1000 cases/day
Phase 1
Manual Bulk
Packing
12. NCE/FI 12Project Title – Open the Master Slide
New Process Map
Noodle
Cake Filling
Noodle
Cake Filling
Noodle
Cake Filling
Taping
Machine
Shipper
Filling
Weighing TM Placing
on Cakes
Transfer of
Cakes to
bulk
machine
ProblemProblem
Packing
TM Cutting
and Chipping
Addition
Noodle Bulk Filling & Packing Layout
TM Placing on
Cakes
PackingWeighingShipper
Filling
Noodle
Cake
Filling
Noodle
Cake
Filling
TM
Sachet
Cutting
Filling of
TM
Sachet
in pouch
Stamping
TM Cutting
and Chipping
Addition
Cake Transfer From Crates to Conveyor
Transfer of
Cakes to
bulk
machine
Shipper
Filling
Noodle
Cake Filling
Chipping
addition &
Weighment
Transferring of Packs
Transferring of Packs
Finished Goods Movement
13. NCE/FI 13Project Title – Open the Master Slide
Data Collection Plan(5W1H)
What questions do you want to answer with this data?
ProblemProblem
What
Measuring
unit
When How Which Where Who Recording
Productivity Kg/Manhr January Output/Manhours
Manpower
&
Production
Bulk
Machine
GSK
Data
Collection
Sheet
Productivity Kg/Manhr January Output/Manhours
Manpower
&
Production
Manual Bulk BC
Data
Collection
Sheet
Stoppages Minutes
January-
February
Manually Duration
Bulk
Machines
Rahul
Data
Collection
Sheet
14. NCE/FI 14
Data Collection
Project Title – Open the Master Slide
ProblemProblem
Phase 1 Bulk m/c Phase 1 Manual Bulk Phase 2 Manual Bulk
Date SKU Plan Actual Manpower SKU Plan Actual Manpower SKU Plan Actual Manpower Machine Productivity Manual Productivity
2-Jan 640 g 300 534 36 640 g 900 550 45 640 g 900 0 0 14.2 11.7
3-Jan 640 g 300 571 36 640 g 900 768 45 640 g 900 0 0 15.2 16.4
4-Jan 640 g 300 50 36 640 g 900 1027 45 640 g 900 434 45 1.3 15.6
5-Jan 640 g 300 209 36 640 g 900 350 45 1.92 kg 900 409 30 5.6 9.7
6-Jan 640 g 300 246 36 640 g 900 1070 45 1.92 kg 600 715 30 6.6 22.8
7-Jan 640 g 300 671 36 640 g 1000 735 45 1.92 kg 600 739 30 17.9 18.9
8-Jan 640 g 300 322 36 640 g 900 673 45 1.92 kg 600 673 30 8.6 17.2
9-Jan 640 g 900 562 36 640 g 1200 500 45 1.92 kg 0 527 30 15.0 13.1
10-Jan 640 g 900 484 36 640 g 1200 670 45 1.92 kg 0 748 30 12.9 18.2
11-Jan 640 g 900 562 36 640 g 1200 633 45 1.92 kg 0 634 30 15.0 16.2
12-Jan 640 g 900 542 36 640 g 1200 608 45 1.92 kg 0 593 30 14.5 15.4
13-Jan 640 g 900 423 36 640 g 1200 0 0
Entire Bulk Operation Shifted to Phase 1
11.3 -
14-Jan 640 g 900 262 36 640 g 1500 0 0 7.0 -
15-Jan 640 g 900 383 36 640 g 1500 200 10 10.2 19.2
16-Jan 640 g 900 249 36 640 g 0 21 1 6.6 20.2
17-Jan 640 g 900 154 36 640 g 0 296 48 4.1 5.9
18-Jan 640 g 900 513 36 640 g 0 425 48 13.7 8.5
19-Jan 640 g 900 591 36 640 g 0 450 48 15.8 9.0
20-Jan 640 g 900 225 36 640 g 1200 710 48 6.0 14.2
21-Jan 640 g 900 664 36 640 g 1200 515 48 17.7 10.3
22-Jan 640 g 900 347 36 640 g 1200 555 48 9.3 11.1
23-Jan 640 g 900 598 36 640 g 1200 788 48 15.9 15.8
24-Jan 640 g 900 617 36 640 g 1200 820 48 16.5 16.4
25-Jan 640 g 900 568 36 640 g 1200 876 48 15.1 17.5
26-Jan 640 g 900 608 36 640 g 1200 919 48 16.2 18.4
27-Jan 640 g 900 540 36 640 g 1200 835 48 14.4 16.7
28-Jan 640 g 900 705 36 640 g 1200 736 48 18.8 14.7
29-Jan 640 g 600 594 36 640 g 800 560 48 15.8 11.2
30-Jan 0 0 0 0 0 0 - -
31-Jan 640 g 600 638 36 640 g 800 0 0 17.0 -
17. NCE/FI 17Project Title – Open the Master Slide
Focused Problem(s) StatementProblemProblem
Y = f {Low Productivity of Bulk Machine}
18. NCE/FI 18Project Title – Open the Master Slide
Cause & Effect
ProblemProblem
Effect /
Problem Y
Man X2Materials X1
Machine X3 Method X4
Rejection method
of check weigher
Lack of
training/awareness
Low
Productivity of
Bulk Machine
No fixed crew
No relievers available during lunch /tea breaks
and for cut open
Machine not running at nominal Speed
Non Availability of good cakes
No fixed position of reel holding
shaft Non Continuous Infeed
system
No key-lock in Long Sealer
shaft
High rejection due to
underweight
Gusetting System not working
properlySealing Issues
No Dispensing
System
Continuous misalignment
of laminate in long sealing
y1
y2
y1
y2
y3
y1
y5 y4
y3
y2
y3
y2
y1
y6
y7Low MTBF No Check Weigher
Analyze Phase
19. NCE/FI 21Project Title – Open the Master Slide
Identify Root Causes – 5 Why Analysis
Rate Loss
2nd Why 3rd Why 4th Why 5th Why1st Why
Cause Checked True on Gemba
Cause Checked False on Gemba
Observation CauseObservation Cause
Observation CauseObservation Cause Observation CauseObservation Cause
Observation CauseObservation Cause Observation CauseObservation Cause Observation CauseObservation Cause
ProblemProblem
Bulk Machine
not Running at
Nominal Speed
Rate of In feed
Insufficient for
Machine to Run
at Nominal Speed
Manual Stacking
& Feeding of
Cakes into Bulk
Machine
Unskilled
Contractual
Manpower
Lack of
Training/
Awareness
Observation CauseObservation Cause
No Fixed
Contractual
Crew for Bulk
Machine
Feeding System
is not Continuous
Reason
ReasonReasonReason
ReasonReasonReason
20. NCE/FI 22Project Title – Open the Master Slide
Identify Root Causes – 5 Why Analysis
High
Rejection
due to
underweight
2nd Why 3rd Why 4th Why 5th Why1st Why
Cause Checked True on Gemba
Cause Checked False on Gemba
Observation CauseObservation Cause
Observation CauseObservation Cause Observation CauseObservation Cause
Observation CauseObservation Cause
Observation CauseObservation Cause Observation CauseObservation Cause
ProblemProblem
High Batch
Variation
Mishandling of
Check weigher
Rejected
Under weight
Cakes
Observation CauseObservation Cause
No Holding
Support for
Laminate Roll
Check Weigher
Rejected
Underweight
Cakes are
Repacked
High Process
Variability
Observation CauseObservation Cause
High Chipping
Loss during
transfer of Check
weigher rejected
Cakes
Misalignment
of I-mark
resulting in
high rejection
Frequent Shifting
of Laminate Roll
Position of
Laminate Roll Not
Fixed
Observation CauseObservation Cause
Unskilled
Manpower
Observation CauseObservation Cause
Lack of
Awareness
on Cake
Handling
Reason Reason Reason
ReasonReason
ReasonReason
Reason Reason Reason
21. NCE/FI 23Project Title – Open the Master Slide
Identify Root Causes – 5 Why Analysis
Continuous
misalignment
of Laminate
in Long
Sealing
2nd Why 3rd Why 4th Why 5th Why1st Why
Cause Checked True on Gemba
Cause Checked False on Gemba
Observation CauseObservation Cause Observation CauseObservation Cause
Observation CauseObservation Cause
Observation CauseObservation Cause Observation CauseObservation Cause
ProblemProblem
Observation CauseObservation Cause
No Holding
Support for
Laminate Roll
Centre Sealer
Misalignment
High vibrations in
Long Sealer
Assembly.
Slipping of
Laminate in Long
Seal Rollers
Misalignment
of I-mark
resulting in
high rejection
Frequent Shifting
of Laminate Roll
Position of
Laminate Roll Not
Fixed
Observation CauseObservation Cause
Design of
Long Seal
Rollers not
proper
Observation CauseObservation Cause
One of the
Bearings on
the Shaft not
fixed
Observation CauseObservation Cause
No key-lock in
Long Sealer
Shaft
Reason ReasonReason
ReasonReason
ReasonReasonReason
Reason
22. NCE/FI 24Project Title – Open the Master Slide
Identify Root Causes – 5 Why Analysis
Mean Time
Between
Failures is Low
2nd Why 3rd Why 4th Why 5th Why1st Why
Cause Checked True on Gemba
Cause Checked False on Gemba
Observation CauseObservation Cause Observation CauseObservation Cause
Observation CauseObservation Cause
Observation CauseObservation Cause Observation CauseObservation Cause
ProblemProblem
Maintenance of
the Machine not
Proper
No Maintenance
Schedule of Bulk
Machine
No CDM
Checklist for
Machine
High Rejection
due to improper
Gusseting
System
Sealing
Defects due
to improper
Gusset
formation
Design of
Gusseting System
not Proper
Reason Reason
Reason
ReasonReason
23. NCE/FI 25Project Title – Open the Master Slide
List of Verified Causes
Non Continuous Infeed System
No holding Support for Laminate Roll
High Rejection due to underweight.
Misalignment of Laminate due to design of Long Sealer Assembly
No fixed Crew/Lack of Training
Machine not Running at Nominal Speed.
No key-lock in Long Sealer shaft.
No M&I schedule
No CDM Checklist for Bulk Machine
Gusseting System not proper resulting in High Rejecton
ProblemProblem
24. NCE/FI 26Project Title – Open the Master Slide
16. Implementation Plan (5W2H)
Root causes
Xs
Description Action Plan Responsibility Timeline Status
X3y1 Non Continuous Infeed System Infeed System to be changed VPST July 2012 In Progress
X3y6
Misalignment of Laminate due to
design of Long Sealer Assembly
Roller Assembly of Long Sealer to
be changed
CD/JS 16/4/2012 Done
X1y1
High Rejection due to
underweight cakes
Trial of 8.5 cakes in one pack to be
done
GSK/RS/BC 23/4/2012 In Progress
X4y4
No CDM Checklist & M&I
schedule
CDM checklist to be made, M&I
schedule to be established
JS/CD/JS 23/4/2012 In Progress
X3y4 Gusseting System not proper Gusseting System to be changed CD 31/3/2012 Done
X2y2
No fixed Crew in Bulk Machine
Packing
To be discussed with Contractor and
Crew to be fixed , Training to be
given
GSK/BC 16/4/2012 Done
X3y3
No Holding Support for Laminate
Roll
New Roller Shaft to be fixed for
Laminate Support, Laminate Roll
Specification to be changed
CD/Multipack 16/4/2012 Done
X3y2 No Key-Lock in Long Sealer Shaft Long Sealer Shaft to be Replaced CD/JS 31/3/2012 Done
X3y8 Manual Weighing of Packs Checkweigher to be installed ST/MS
August
2012
In Progress
X4y1 No Dispensing System Spare Dispenser to be used BC 23/4/2012 In Progress
ProblemProblem
Improve Phase
25. NCE/FI 27Project Title – Open the Master Slide
ProblemProblem
Implementation
Gusseting System Changed New Gusseting System
Old Gusseting System
26. NCE/FI 28Project Title – Open the Master Slide
ProblemProblem
Implementation
Long Sealer Shaft replaced
Old Shaft without key lock New Shaft with key lock
27. NCE/FI 29Project Title – Open the Master Slide
ProblemProblem
Implementation
Design of Roller Assembly changed
Old Roller Assembly New Roller Assembly
Before After
28. NCE/FI 30Project Title – Open the Master Slide
Results - Before & AfterProblemProblem
13.5
20
24
18.2 18.2 18.2
10
12
14
16
18
20
22
24
26
Before After Way Forward
Actual Productivity
Target
29. Innovation
Savings = 8 x 250 x 352 = INR 0.7 Mio annually
Number Optimized : 8 FTE
Method Followed : Work Load Study and Job Combining.
1. Productivity Improvement by Optimizing House Keeping Manpower
Savings = 6 x 250 x 352 = INR 0.53 Mio annually
Number Optimized : 6FTE
Method Followed : GSTD, Work Load Study and Job Combining
2. Productivity Improvement by Optimizing Phase 2 Contractual Manpower