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HIGH PRESSURE VESSEL LEAKAGE IN UREA PLANTS
ArticleĀ Ā inĀ Ā Global Science and Technology Ā· January 2021
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GSJ: Volume 9, Issue 1, January 2021
ISSN 2320-9186
GSJĀ© 2021
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GSJ: Volume 9, Issue 1, January 2021, Online: ISSN 2320-9186
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HIGH PRESSURE VESSEL LEAKAGE IN UREA PLANTS
(A case study)
Prem Baboo,
DGM (Production & Process), Dangote Fertilizer Limited) Ex. Sr. Manager, National Fertilizers Ltd, India
ARTICLE DETAILS ABSTRACT
__________________________ _____________________________________________________________________
Article History
Published Online: publisher use only
_____________________________
Keywords
Ammonium Carbamate
Carbamate Condenser
Liner, Leakage,
Reactor,
Stripper,
Urea,
*
Corresponding Author
atharva.dangre1@gmail.com
_______________________________________________________________________________________________
_______________________________________________________________________________________________
Introduction
National Fertilizers Ltd, (NFL) operates a fertilizer complex at Vijaipur, Distt. Guna (Madhya Pradesh) consisting of
two units Vijaipur-I and Vijaipur-II, plants were commissioned in December 1987 and March 1997 respectively.
In urea plant ammonium carbamate solution is very corrosive; all metals
have corrosion problems with ammonium carbamate and the corrosion
problems increase with temperature, a ten degree Celsius rise in temperature
doubles the corrosion rate to the point where the duplex steel is no longer
acceptable. The material plays a very important role in Urea plants. The
space between the reactor liner and the shell is most often empty and
employs various methods of detecting a leak ranging from conductivity
measurements. Vacuum leak detection system, pressure leak detection
system etc. Titanium, SS316L (urea grade), 2 RE-69 etc.) Over the years
that can resist ammonium carbamate corrosion. Materials plays very
important role in any industry. Selection of material is vital at design stage
itself ,Wrong selection of material may lead to catastrophic failures and
outage of plants & even loss of Human lives, Right selection of material
leads to long life of plant. In the latest plants specialty duplex materials are
used for liner. The actual reactor has been constructed using a variety of
materials, e.g. Zirconium, Vessel inside a protective liner. This paper
intended study of number of leakage in the HP loop vessels, e.g. Zirconium,
Vessel inside a protective liner. This paper intended study of number of
leakage in the HP loop vessels, e.g. Reactor, Stripper, Carbamate condenser
etc. How to detect leakage and troubleshooting during detection and
attending the leakages.
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Ammonia Plants are based on M/s. HTASā€™s Steam Reforming of Natural Gas and Urea plants are based on M/S.
Saipem Ammonia Stripping technology. The Vijaipur unit, which is an ISO 9001:2000 & 14001 certified, comprises
of two streams. The Vijaipur have two ammonia plant M/S. Haldor Topsoe Technology, Denmark capacity 1750 &
1864 TPD for Line-I & line-II respectively and urea plant capacity 3030 and 3231 TPD for line-1& Line-II
respectively.
Brief Description of Urea process
The urea process is characterized by a urea synthesis loop with a reactor operating at about 158 kg/cm2 (g) (for
stripping process) with ammonia to carbon dioxide molar ratio at urea reactor inlet of 3.3 - 3.6. This allows a CO2
conversion into urea of 64 - 66% in the reactor itself, also perforated trays which prevent back-flow maintained plug
flow and favour gas absorption by the liquid. Different type of HET is used now a day to increase the conversion
rather than vessel size and pressure. Different types of HET are developed like super cup etc. The urea process vessels
are High Pressure Decomposition in H.P. stripper; Medium Pressure Decomposition in M.P. Decomposer and, finally,
Low Pressure Decomposition in L.P. Decomposer. The decomposition reaction is the reverse reaction of the first one
above showed, viz.: NH2-COO-NH4 ā†” 2NH3 + CO2 (- Heat) and, as can be inferred from the equation, it is promoted
by reducing pressure and adding heat. The urea reactor effluent solution enters the stripper, under slightly lower
pressure than the urea reactor, where a fair part of the unconverted carbamate is decomposed, due to the stripping
action of either NH3 or CO2, so that the overall yield of the H.P. synthesis loop referred to CO2 is as high as 80-85%
(on molar basis). Ammonia and carbon dioxide vapours from the stripper top, after mixing with the carbamate recycle
solution from M.P. section, are condensed at the same pressure of the stripper, in the H.P. carbamate condenser; thus
producing the LS steam which is used in downstream sections. After separating the inert gases which are passed to
M.P. section, the carbamate solution is finally recycled to the reactor bottom by means of a liquid/liquid ejector, which
exploits H.P. ammonia feed to reactor as motive fluid. This ejector and the kettle-type carbamate condenser above
mentioned, allow a horizontal layout, which is one of the main features of Stripping process. Downstream of the
stripper residual carbamate and ammonia are recovered in two recycle stages operating at about 17.5 kg/cm2
(g) (M.P.
section) and 3.7 kg/cm2 (g) (L.P. section) respectively. Ammonia and carbon dioxide vapours coming from carbamate
decomposition are condensed and recycled to H.P. section. The solution leaving the L.P. section arrives to the
concentration section where process condensate is removed in order to reach a concentration of about 99.7 % which is
required to feed prilling tower bucket. The weep holes are provided for the following Equipmentā€™s:
1. Urea reactor
2. Stripper
3. Carbamate condenser and
4. Carbamate separator
Weep holes are safe installation for protecting the above equipment in case of leakages from the lining welds,
avoiding that process fluids could come in contact to the carbon steel material of equipment body. We had checked
prior to start-up of the plant.
(A) CASE STUDY OF REACTOR LEAKAGES
The all four reactors(R-1) of Urea line 1 & 2 plants are 40 meters Height (Tan to tan). The liner of all reactors has SS
316 L (mod) while shell of line 1 & line 2 are differing. The line -1 both reactors are coil layered vessel while 31 unit
has multi layered and that of 41 is mono block reactor. Detail as following table N0-1. The all four Urea reactor have
15 number of sieve trays. These have been provided to prevent the escape of gaseous CO2, which must react with NH3
in the lower portion of the reactor. These trays also help in preventing the internal recycling of the reaction products
with higher specific gravity products formed in the upper part of the reactor. Reactor shell is made of CS with a 7 mm
liner of SS316L (mod) on the liner surface.
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Liner of the reactor is cladded to the CS shell and longitudinal seams and circumferential seams are differing in line-1
and line-2 urea reactors .For detecting any leakage in the liner a weep hole monitoring system has been provided. The
line-1 urea reactors have 95 numbers weep holes. And Urea line-2 of 31-Urea reactors has 77 numbers weep holes and
41 reactors has 98 numbers weep holes. In the weep hole monitoring system there are two loops of weep holes
covering the entire reactor. All four Urea reactor (R-1) have 15 number of sieve trays. These have been provided to
prevent the escape of gaseous CO2, which must react with NH3 in the lower portion of the reactor. These trays also
help in preventing the internal recycling of the reaction products with higher specific gravity products .Reactor shell is
made of CS with a 7 mm liner of SS-316L (mod) on the inner surface. Liner of the reactor is cladded to the CS shell
and longitudinal seams and circumferential seams are differing in line-1 and line-2 urea reactors.
Reactors leakage detection and repairing ,Reactor Liner Leakage on 28/01/2006.
Reactors Specifications
Sr. No. Parameters units Value
1 Working Pressure Kg/cm2
159
2 Design Pressure
Kg/cm2
169 at top
Kg/cm2
169 +full of liq at Bottom
3 Hydro Test Pressure
Kg/cm2
219.7 (Vertical)
Kg/cm2
224 (Horizontal)
4 working Temperature 0
C 188
5 Design temperature 0
C 200
Table-1
In Urea Line-I and 2 plants all the weep holes are connected to conductivity meter based monitoring system. On dated
28/01/2006 the leakage alarm appeared in weep hole number 23 of 11 stream. The weep hole was checked physically
and vapour analysed in laboratory fond ammonia vapour and CO2.Immedially shut down was taken and leakage found
with instrument air and soap solution the leakage easily detected. For find out the leakage the liner plate behind the
weep hole was pressurized with instrument air at the pressure of 0.5 kg/cm2
and other three interconnected weep holes
were plugged. Soap solution applied on opposite side of liner. The pin hole leakage easily detected. The pin hole
repaired by welding. The repaired portion was passivated with 10 % HNO3 solution and rinse with Demineralised
water.The repaired portion was further checked with instrument air and soap solution no leakage was found. The
shutdown duration was only 69 hrs Feed cut to feed in.
Reactor Liner Leakage on 28/11/2017.
On dated 28/11/2017, a weep hole leakage alarm from Weep Hole No. 34 was appeared on lectrotek system.
Immediately checked the weep hole No.-34 and vapour analysed in laboratory found ammonia & CO2 vapour and
leakage was confirmed. Immediately shut down was taken at 11.15 hrs on dated 28/11/2017.draining of the H.P loop
started at 11.15 hrs. For air purging 11 PT-05 A/B cover open for air purging. Man entry permitted at 18.15 hrs on
dated 29/11/2017 after confirming ammonia contents less than 25 ppm and Oxygen contents more than 20 %. Four
Numbers man ways were opened for detecting leakage the leakage above 5th
tray. So the 4 man ways opened. First of
all, leakage detection tried with instrument air & soap solution. For detecting the leakage, the instrument air
introduced at the pressure of 0.5 kg/cm2
and other three interconnected weep hole plugged that the pressure retains
inside the liner and shell. Soap solution applied on liner for detecting the leakage. Four hour tried to leakage but
success did not get. After that our further step to detect the leakage with ammonia and phenolphthalein indicator. But
leakage could not have detected. As the weep hole leakage was not clear, the exact location the leak could not be fund
out with Soap solution and ammonia test. Finally the DP check and number of the spot found. Finally, all the
circumferential Seam and longitudinal seam opposite of weep hole No. 34 between 4th
& 5th
trays welding done. After
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that ammonia is introduced at the pressure of 0.4 kg/cm2
n weep hole No. 34 and hold up for 10 hrs. and liner and all
welding seal checked by phenolphthalein indicator. No leakage was found and man hole cover boxed up. Start-up
activities started and feed in done on dated 01/12/2017 at 11.1 hrs. Total time taken for this shut down was 72 hrs (3
days) feed cut to feed in.
Weep hole Monitoring
Urea line-1 weep hole monitoring with lectrotek system (Pune). In Urea line-2 Masibus weep hole monitoring system
is incorporated. The Micro genie scan is a microprocessor based scanner which has been specially designed for
resistance input to monitor reactor leakage easy and very simple in installation low pricing equipmentā€™s and easy in
maintenance. This programme containing non-volatile memory for setup data, 4 duals and 4 digit display and LED bar
for information RS -232 ā€“C serial port.The instrument is housed in a Ā½ DIN extruded Aluminum rack suitable for
control room mounting. A small but highly functional Keyboard consisting of 4 membrane keys is provided as the as
the instrument operator interface electrical and I/O temperature are instruments rear Via Screw type terminals. As
shown in the figure-2. The electronics is located on modularly designed board for easy field trouble shooting and
maintenance. All cards are plug in type and segregated by their function Viz ā€“including power supply CPU, A/D
display. All the weep holes have to be checked by passing instrument air every week/fortnight for any leakage and
blockage & the pressure of the testing medium should not be more than 0.5 kg/cm2
Fig-2
REACTOR (11-R-1) LEAKAGE JULY-19
The Leakage observed on dated 04/07/2019, during the hydraulic pressurization of the reactor. It was observed that
HP loop pressure was not increasing beyond 65 kgcm2
, rather started decreasing (Figure 4). It was noticed that
condensate was coming outside from 1st segment (L-seam) of the reactor from inside the insulation. Immediately
insulation was removed and it was noticed that the outer shell plate of 08 mm got ruptured from its vertical weld joint
(400 mm in length) at 1st segment (L-seam) (Figure 3). Hence, HP loop was depressurized and draining was carried
out and top manhole cover was removed for internal inspection. Simultaneously, tray man ways were opened from 1st
to 5th tray. To detect the leaky portion inside the reactor, DM water was supplied through flexible hose from outer
ruptured portion of the shell course and thorough physical (visual) inspection was carried out inside the reactor. It was
found that water was coming out through 1st trayā€™s TSRā€™s newly welded cleat. After insulation removal, it was also
noticed that there was bulging on outer (8 mm) layer at the first and fifth segment from the top of the reactor Vertical
joint of 1st
segment outer shell 8 mm layer welding was found in ruptured condition and bulging of longitudinal pad
plate of 5th segment was also noticed.
Reason for Failure of Vertical
Welding Joint of 1st
Segment System hydro-test water entered through the damaged portion of newly welded TSR
cleat of the first tray into the coiled layers and reached up to the last layer of 8 mm.
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Fig-3
As the vent holes and vent tube of the segment were in plugged condition, this resulted in pressurization of the outer
shell course, causing rupturing of the 8 mm outer layer vertical joint. The coiled layer welding remained intact;
otherwise it could have un winded. Repair and Maintenance After thorough inspection of internal and external
damage as well as consent and repair procedure approved from M/s. Saipem, rupture repairing company was
contacted for rectification/repair of the reactor within minimum possible time at NFL Vijaipur site itself repair
Procedure.
Fig -4
Temporary scaffolding was erected from ground floor to top of the reactor for approaching all vent..Tubes and vent
holes as well as to carry out the job. Subsequently, whole Insulation was removed from reactor. All the vent holes and
vent tubes plugs were de-plugged. All vent tubesā€™ depth was measured, which was found in the range 62 mm and
depth of vent holes was found as 40-42 mm. Further cleanliness of the vent tubes and connected vent holes of each
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segment was checked with instrument air pressure at 0.3 kg cm2
g and found at clear condition. Maintenance jobs
executed to rectify the damaged portion of reactor are as follows:
Fig-5
The outer shells (8 mm) of first and fifth segment were removed and replaced with new semi-circular shells made of
16 mm CS plate (SA516 Gr70) in NFL Vijaipur workshop.
The TSR leaky point was removed in rectangular shape of size 300 x 200 mm to ensure that the internal layers of the
reactor is not damaged and replaced with new patch plate, with separate weep hole for monitoring patch plate liner
and welding.
The first to fifth TSR as well as its all cleats was replaced with new one.
The longitudinal pad plate of the fifth segment was replaced. test, dye penetrate test, magnetic particle test and
ultrasonic test of all pressure seams (L, C and nozzle welds) were carried out on the external surface. Visual test, dye
penetrate test, ferrite content test of all the internal attachment welds were carried out followed by air and ammonia
leak test for weep holes as well as vent holes/vent tubes system of all segments inside the reactor. To facilitate air and
ammonia leak test, small loops connecting weep and vent system of 2/3 segments each were made to cover up the
whole reactor .Reactor feed in was carried out on 08-07-2019 at 03.00 hours and prilling lined up at 07.30 hours.
Again shut down taken on 08/07/2019.
Thorough physical inspection of reactor fresh urea deposition was observed at the exit of 70Ā° top vent hole of 3rd
segment. It was noticed that fresh urea melt was accumulating at the exit of the said vent hole . Again plant shutdown
was taken. After draining/depressurization and flushing of HP loop, reactor manhole cover was removed. Man ways
up to 4th
tray were opened for inspection and repairing the internal defect. Repairs at 3rd
Segment and Inspection
Grinding of longitudinal and circumferential seam weld joints was carried out keeping weep holes system and vent
tubes/vent holes system pressurized with instrument air at 0.3 kg cm2
g. One pinhole was found on C- seam weld joint
of 3rd
segment. Patch plate was welded over pinhole point. NDT test was done and clearance received from
mechanical team & M/s. L&T for leak test by air and ammonia on 12-07-2019 at 02.00 hours. This time air &
ammonia tests were performed at 0.4 kg cm-2g for 2nd
and 3rd
segment and 0.3 kg cm-2g for 4th segment which was
completed on 12-07-2019 at 21.20 hours. No leakage was found with air and ammonia leak test. Further, hydro test of
reactor was carried out but water started coming out through 70Ā° vent tube and 250Ā° vent hole (bottom) of 3rd
segment
at HP loop pressure of 90 kg cm2
g.The leak observed again. Finally system was depressurized and drained. Air leak
test as well as Helium test was carried for 2nd
, 3rd
and 4th
segment on 19th
and 20th
July(Figure-6) The same instrument
tapings that were used for the air and ammonia test were used for the helium test. First the system was purged with
Nitrogen and then helium was charged from helium cylinder through the vent hole/tube and weep hole system, the
system was kept at hold for 4.0 hours at a pressure of 0.3 kg cm2
g, to ensure the
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Fig-6
permeation of helium through leakage and cracks. Inside the reactor the segments were divided into smaller isolated
portion using sheets and tapes for leak detection . After the hold duration was complete, the leak test was carried out
by puncturing the sheet and inserting the analyzer in it. No leakages were detected in the test. Plant Start-up and
Monitoring.
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Fig--7
(B) LEAKAGE FROM STRIPPER
Detail of Stripper
The Urea HP Stripper is the equipment where there are the most severe process operating conditions in the Urea Plant.
This equipment, that basically is a falling film evaporator, must work under high pressure, temperature and very
aggressive process media .Urea Stripper is considered as the backbone of Urea Plant performance and efficiency. Its
performance determines production and profitability of end product which is Urea Fertilizer. The equipment design
takes into account a trade off between cost and corrosion resistance against the aggressive process media. The result is
a carbon steel body sized to withstand the stresses coming from the pressure and temperature loads, while it is
protected by a corrosion resistant material barrier in all the parts in contact with the process media including the heat
exchange tubes.
Reaction products leaving the reactor are sent into bimetallic stripper tubes sides for carbamate decomposition. The
medium pressure steam (23 bar) is used for this purpose. The stripper is the high pressure vessel of H.P loop.
Operating at 147 bar in tube side pressure and that of shell side is 24 bar. The top temperature of stripper is 190 0
C and
that of bottom is 2050
C.at this temperature approximate 80 % of carbamate presents in solution is decomposed and
rest are decomposed in MP & LP section. The water is separated in pre-concentrator and two stages of vacuum
evaporation sections. The decomposition reaction is a reverse reaction of urea formation.
NH4COONH2=NH3 +CO2- HEAT
As can be inferred from the equation, decomposition is promoted by reducing pressure and /or adding heat. In M/S.
Saipem process decomposition is carried out in three steps. Decomposition is promoted by heating and stripping CO2
by vaporized excess ammonia, according to Henryā€™s Law of partial pressure under the same pressure level as urea
reactor. The plant commissioned in 1997 till date stripper is running. During pre-commissioning 55 no of tubes
plugged in presence of Saipem representative. Tubes were plugged as Zirconium lining of these tubes was found
damaged. In present shut down one damaged old plug replaced with new one and others eight numbers minor
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Fig-8
Leakage. Stripper used is falling film type heat exchanger decomposed and vaporized gases and liquid effluent are
therefore in counter current contact and CO2 concentration in liquid is gradually reduced from top to bottom of the
stripper tubes.
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Fig-9
Besides the above, general corrosion has been observed on the bottom tube sheet, tube to tube sheet welding and
bottom part of tubes (20 mm). Stripper has rendered service for around 21 years. Two types of stripping process are
there; Viz: CO2 stripping and NH3 stripping. Both process work according to shift in partial pressure. This process is
the most modern and energy efficient and therefore, widely used now a day. Decomposition at high pressure requires
higher temperature, which means that much biuret has formed and the liquid becomes corrosive, but in the M/S.
Saipem process the excess of ammonia and the use of Zirconium in the stripper permits minimizing these problems.
The off gases generated in stripper are condensed in the high Pressure carbamate condenser where low pressure steam
is generated. The NH3 to CO2 mole ratio of 3.5:1 is used and the reactor is operated at a pressure by which the
carbamate solution is pumped to the reactor by ejector but not using Carbamate pumps.
For passivation of bottom parts of stripper, a passivation compressor also installed to give air in bottom dome. About
42 Nm3
/hr air is feed to stripper bottom.CO2 fed to Reactor normally contains a small percentage of H2, CH4 & CO in
addition to inerts like N2& Ar. The passivation air also given to CO2 in 1st
stage suction of CO2 compressor. We
maintained 0.35 to 0.4% O2in 3rd
suction of CO2 compressor. Together with O2 contained in passivation air could give
rise to explosiveness problem when sent to CPP for HRU fuel to avoid explosive mixture natural gas also fed to MP
condenser so that explosive mixture in inerts gas could not be made. Passivation air presents a major issue for urea
process. Designed to prevent the corrosion of stainless steel, passivation air constantly coats the inner surface of
stripper tubes with an oxygenated process solution.An ammonia rich gas (CO2 lean gas) rises from lower parts of the
tube, then the gas at the upper parts of the tube becomes an ammonia richer gas as compared with equilibrium
composition and the decomposition reaction in liquid phase correct the deviation from the equilibrium (the stripping
effect). Carbamate is decomposed at reactor pressure with the help of one of the reactants. First thing that comes into
mind while going to look for leakage in such high pressure vessel is that, what are the potential points that can lead to
leakage in such thick metal walls. There are three surfaces in contact with highly corrosive Carbamate solution.
1. Tube sheet.
2. Tube itself.
3. Tube to tube sheet joint.
The tube sheet thickness is 255 mm including 10 mm overlay. The leakage develops when overlay eaten with
corrosion/erosion, less passivation. The condensate outlet of stripper collects to steam condensate drum. The rest
energy of this steam condensate uses in MP decomposer. In this line conductivity meter also installed for quick
indication of leakage ranging 0-500 Āµ mho. Also if there is any leakage in Stripper tubes or tube sheet, it shall be
picked up in steam condensate leaving Stripper shell side. This will appear in the form of high conductivity.
Monitoring of fresh steam entering into steam drum and condensate leaving the steam drum is very important and its
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delta (increase in conductivity of condensate leaving steam drum with respect to incoming steam) will determine the
extent of leakage.
Reason of leakage
The main reason of plug failure is old age of equipment i.e. 21 years old vessel. The old 55 numbers tube plugs failure
one by one due to layers of welding gradually deteriorated. Corrosion and exposure of hidden defect in tube-to-tube
sheet joint.
Fig 10
Detection of the leakage
Lack of passivation air. Leakage was so heavy that steam to stripper turned to zero immediately and stripper shell
immediately pressurized up to PSV set value i.e. 26 bar, as shown in the Arrangement as shown in the figure- 12, was
done for getting tube leakage detection. Blind are provided to following equipment lines.
1. Steam to shell side inlet line
2. Outlet line i.e. V-29 vessel
The Shell side pressurized with instrument air at the pressure 7.0 bar and leakage detects with soap solution in top &
bottom dome (Channel). Air & soap solution test is the most effective and safe for detection of leakage. Although it is
the time consuming test and finding the defects but increasing the inspectors during the test serves the purpose. The
test was carried out by pressurizing the shell side with air at 6.5-7.0 bar. After pressurization, inspectors can readily
enter into both the channel sides with soap solution and can start finding the leaking points. It requires much of
attention and skill of inspector to look for all the defects. Full scanning is must and a cumbersome job. The salient
features of this test are:
1. Reliable and effective but time consuming.
2. Good for all small and large leakages.
3. Safe and less risky than ammonia leak test.
After the confirmation of leakage in both the channel itā€™s the responsibility of Inspection and welding by expert
welder to arrest the leakage in Urea Stripper. Major culprit plug leakage detects easily without applying soap solution
air was coming from the damaged plug. For further minor leakage detection, a team was deputed for top & bottom
channel.
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Fig-11
Old plug removing is very risky
When old plug removing the tubes filled with ammonium carbamate & urea solution. So the B.A set and protection
apparatus are used to remove the old plugs. Preparation and Installation work can be done by experts of fitting &
welding persons. In case of a leak one can easily check if there is any damage of tube sheet as corrosion would start
from the inside the tube sheet hole. Replacing a new plug with 2 RE-69(25/22/2) takes max 15 minutes and can be
done with a protection mask when ammonia is present.
Rectification of defects
The rectification of defects was carried out very carefully as it involves welding adjacent to the healthy tubes and
tube-to-tube sheet joints. Following guidelines was follow listed below:
1. Grinding was done effectively in order to flush the pin hole completely. Ineffective grinding would never
rectify the leaking point.
2. Welding was made after dye-penetrate testing of ground off area.
3. TIG welding with lower heat input was used for rectification.
4. Adjacent tubes and tube sheet weld joints avoided. Certain jigs used for the same in order to concentrate the
welding heat where required.
5. Qualification of welder was made before welding in this sensitive area. High heat input will cause burn thru /
HAZ area which would eventually be a potential point of leakage.
6. The 2 RE 69 (25/22/2) material plugs were applied on defected tubes. Each and every time leakage was
detected with DPT and air/soap solution.
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Fig-12
(C ) HP Carbamate Condenser Leakage
The gases leaving the top of the stripper are mixed with carbonate coming from the bottom of column medium
pressure absorber where they are condensed. Low pressure steam is produced on the shell side of condenser and is fed
to the steam network. Temperature of carbamate condensation is determined by shell side steam pressure which is
kept constant by pressure controller on L.P. steam network. The vessel having ā€˜Uā€™ tube bundle inside the carbamate.
The solution after mixing goes to Carbamate separator then feed to reactor along with ammonia ejector.
Schedule for 41-HP loop shut down
HP loop draining -5 hours.
Depressurization -2 hours.
LS purging -4 hours.
Water filling -4 hours
Over flow -4 hours
Draining -10 hours
PT-05(HP loop pressure) drop & air purging -
10-12 hours and contd. During shut down.
Detection of Leakage
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For detection of leakage the tube(process side) manhole cover open and Partion plate removed after that preparation of
leakages and inspection like NDT etc.
For leakage detection the blind provided at following lines
1. Both PSV Line
2. Condensate export line.
3. Steam cond import lines
After providing blinds the entry done in tube side for detecting of leakages with soap solution with instrument air
pressurization. The shell side pressurized up to 3.5 kg/cm2
g as shown in the figure-13
Fig-13
After that NDT was done for tube thickness as prier planed.
Report:
Health assessment of carbamate condenser tubes had been studied by the eddy current testing. A total 3230 tubes were
tested in 04 working days with one machine and one technician. The study yielded 34 tubes which is >50 % and above
in ID & OD , which need to be plugged to continue to take the unit for further service. The thickness reduction which
is <50% will be given in the final report later for your reference.
Layout:
Condenser has named as 41-Carbamate condenser Top Portion Inlets has been identified top inlet starting from Top to
Bottom (rows) left side(columns), and 41-E-5 Bottom portion outlets starting from Bottom to Top(rows) left
side(columns). This will be the nomenclature followed throughout our report.
SUMMARY: Total Number of tubes to be Plugged
Top portion (Inlet) ā€“ 17Tubes
Total Tubes - 34 Tubes
Bottom Portion (outlet) ā€“ 17 Tubes
Conclusion
In HP vessels whenever the leakage started shut down must be taken after confirmation.In any leakage development of
a specific welding/repair sequence taking into account item complexity, double lining construction and heat treatment
requirements. Welders training to maintain a high and homogeneous High pressure welder quality.
724
GSJ: Volume 9, Issue 1, January 2021
ISSN 2320-9186
GSJĀ© 2021
www.globalscientificjournal.com
Fig-14
It is clear that this is an approach that takes into account only the direct cost of the equipment without any
consideration on business losses that as in many cases like ours exceed by far the equipment cost. This option has the
overall lowest life cycle cost of all the alternatives evaluated. Corrosion also observed in the stainless steel bimetallic
tube next to the tube to tube sheet weld overlay. Corrosion in the 25-22-2 tube underneath the Zirconium tube caused
by stagnant zone due to poor bonding.
References
1. Urea Reactor Liner Leakage (A Case Study) by Prem Baboo, Published by International Journal of
Engineering Research & Technology (Vol. 6 Issue 12, December ā€“ 2017
2. Urea stripper Tube leakage by Prem Baboo, Published by International Journal of Engineering Research &
Technology (Vol. 7 Issue 03, March ā€“ 2018
3. New Urea High Pressure Zr Stripper Development by Jorge Versace ( Profertil S.A., Argentina). New Urea
HP Zr Stripper Development, 2004.
4. Urea Reactor Liner Leakage - A Case Study by Jagdeep Shah Singh published in Indian Journal of Fertilisers
16 (6) : 608-615, June 2020.
725
View publication stats
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High pressure vessel leakage in urea plants

  • 1. See discussions, stats, and author profiles for this publication at: https://www.researchgate.net/publication/348619816 HIGH PRESSURE VESSEL LEAKAGE IN UREA PLANTS ArticleĀ Ā inĀ Ā Global Science and Technology Ā· January 2021 CITATIONS 0 1 author: Some of the authors of this publication are also working on these related projects: Silo (UREA) level measurement View project Industrial Process View project Prem Baboo Dangote Fertilizer Ltd 65 PUBLICATIONSĀ Ā Ā 11 CITATIONSĀ Ā Ā  SEE PROFILE All content following this page was uploaded by Prem Baboo on 20 January 2021. The user has requested enhancement of the downloaded file.
  • 2. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com GSJ: Volume 9, Issue 1, January 2021, Online: ISSN 2320-9186 www.globalscientificjournal.com HIGH PRESSURE VESSEL LEAKAGE IN UREA PLANTS (A case study) Prem Baboo, DGM (Production & Process), Dangote Fertilizer Limited) Ex. Sr. Manager, National Fertilizers Ltd, India ARTICLE DETAILS ABSTRACT __________________________ _____________________________________________________________________ Article History Published Online: publisher use only _____________________________ Keywords Ammonium Carbamate Carbamate Condenser Liner, Leakage, Reactor, Stripper, Urea, * Corresponding Author atharva.dangre1@gmail.com _______________________________________________________________________________________________ _______________________________________________________________________________________________ Introduction National Fertilizers Ltd, (NFL) operates a fertilizer complex at Vijaipur, Distt. Guna (Madhya Pradesh) consisting of two units Vijaipur-I and Vijaipur-II, plants were commissioned in December 1987 and March 1997 respectively. In urea plant ammonium carbamate solution is very corrosive; all metals have corrosion problems with ammonium carbamate and the corrosion problems increase with temperature, a ten degree Celsius rise in temperature doubles the corrosion rate to the point where the duplex steel is no longer acceptable. The material plays a very important role in Urea plants. The space between the reactor liner and the shell is most often empty and employs various methods of detecting a leak ranging from conductivity measurements. Vacuum leak detection system, pressure leak detection system etc. Titanium, SS316L (urea grade), 2 RE-69 etc.) Over the years that can resist ammonium carbamate corrosion. Materials plays very important role in any industry. Selection of material is vital at design stage itself ,Wrong selection of material may lead to catastrophic failures and outage of plants & even loss of Human lives, Right selection of material leads to long life of plant. In the latest plants specialty duplex materials are used for liner. The actual reactor has been constructed using a variety of materials, e.g. Zirconium, Vessel inside a protective liner. This paper intended study of number of leakage in the HP loop vessels, e.g. Zirconium, Vessel inside a protective liner. This paper intended study of number of leakage in the HP loop vessels, e.g. Reactor, Stripper, Carbamate condenser etc. How to detect leakage and troubleshooting during detection and attending the leakages. 710
  • 3. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Ammonia Plants are based on M/s. HTASā€™s Steam Reforming of Natural Gas and Urea plants are based on M/S. Saipem Ammonia Stripping technology. The Vijaipur unit, which is an ISO 9001:2000 & 14001 certified, comprises of two streams. The Vijaipur have two ammonia plant M/S. Haldor Topsoe Technology, Denmark capacity 1750 & 1864 TPD for Line-I & line-II respectively and urea plant capacity 3030 and 3231 TPD for line-1& Line-II respectively. Brief Description of Urea process The urea process is characterized by a urea synthesis loop with a reactor operating at about 158 kg/cm2 (g) (for stripping process) with ammonia to carbon dioxide molar ratio at urea reactor inlet of 3.3 - 3.6. This allows a CO2 conversion into urea of 64 - 66% in the reactor itself, also perforated trays which prevent back-flow maintained plug flow and favour gas absorption by the liquid. Different type of HET is used now a day to increase the conversion rather than vessel size and pressure. Different types of HET are developed like super cup etc. The urea process vessels are High Pressure Decomposition in H.P. stripper; Medium Pressure Decomposition in M.P. Decomposer and, finally, Low Pressure Decomposition in L.P. Decomposer. The decomposition reaction is the reverse reaction of the first one above showed, viz.: NH2-COO-NH4 ā†” 2NH3 + CO2 (- Heat) and, as can be inferred from the equation, it is promoted by reducing pressure and adding heat. The urea reactor effluent solution enters the stripper, under slightly lower pressure than the urea reactor, where a fair part of the unconverted carbamate is decomposed, due to the stripping action of either NH3 or CO2, so that the overall yield of the H.P. synthesis loop referred to CO2 is as high as 80-85% (on molar basis). Ammonia and carbon dioxide vapours from the stripper top, after mixing with the carbamate recycle solution from M.P. section, are condensed at the same pressure of the stripper, in the H.P. carbamate condenser; thus producing the LS steam which is used in downstream sections. After separating the inert gases which are passed to M.P. section, the carbamate solution is finally recycled to the reactor bottom by means of a liquid/liquid ejector, which exploits H.P. ammonia feed to reactor as motive fluid. This ejector and the kettle-type carbamate condenser above mentioned, allow a horizontal layout, which is one of the main features of Stripping process. Downstream of the stripper residual carbamate and ammonia are recovered in two recycle stages operating at about 17.5 kg/cm2 (g) (M.P. section) and 3.7 kg/cm2 (g) (L.P. section) respectively. Ammonia and carbon dioxide vapours coming from carbamate decomposition are condensed and recycled to H.P. section. The solution leaving the L.P. section arrives to the concentration section where process condensate is removed in order to reach a concentration of about 99.7 % which is required to feed prilling tower bucket. The weep holes are provided for the following Equipmentā€™s: 1. Urea reactor 2. Stripper 3. Carbamate condenser and 4. Carbamate separator Weep holes are safe installation for protecting the above equipment in case of leakages from the lining welds, avoiding that process fluids could come in contact to the carbon steel material of equipment body. We had checked prior to start-up of the plant. (A) CASE STUDY OF REACTOR LEAKAGES The all four reactors(R-1) of Urea line 1 & 2 plants are 40 meters Height (Tan to tan). The liner of all reactors has SS 316 L (mod) while shell of line 1 & line 2 are differing. The line -1 both reactors are coil layered vessel while 31 unit has multi layered and that of 41 is mono block reactor. Detail as following table N0-1. The all four Urea reactor have 15 number of sieve trays. These have been provided to prevent the escape of gaseous CO2, which must react with NH3 in the lower portion of the reactor. These trays also help in preventing the internal recycling of the reaction products with higher specific gravity products formed in the upper part of the reactor. Reactor shell is made of CS with a 7 mm liner of SS316L (mod) on the liner surface. 711
  • 4. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 Fig-1 GSJ: Volume 9, Issue 1, January 2021 GSJĀ© 2021 www.globalscientificjournal.com 712
  • 5. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Liner of the reactor is cladded to the CS shell and longitudinal seams and circumferential seams are differing in line-1 and line-2 urea reactors .For detecting any leakage in the liner a weep hole monitoring system has been provided. The line-1 urea reactors have 95 numbers weep holes. And Urea line-2 of 31-Urea reactors has 77 numbers weep holes and 41 reactors has 98 numbers weep holes. In the weep hole monitoring system there are two loops of weep holes covering the entire reactor. All four Urea reactor (R-1) have 15 number of sieve trays. These have been provided to prevent the escape of gaseous CO2, which must react with NH3 in the lower portion of the reactor. These trays also help in preventing the internal recycling of the reaction products with higher specific gravity products .Reactor shell is made of CS with a 7 mm liner of SS-316L (mod) on the inner surface. Liner of the reactor is cladded to the CS shell and longitudinal seams and circumferential seams are differing in line-1 and line-2 urea reactors. Reactors leakage detection and repairing ,Reactor Liner Leakage on 28/01/2006. Reactors Specifications Sr. No. Parameters units Value 1 Working Pressure Kg/cm2 159 2 Design Pressure Kg/cm2 169 at top Kg/cm2 169 +full of liq at Bottom 3 Hydro Test Pressure Kg/cm2 219.7 (Vertical) Kg/cm2 224 (Horizontal) 4 working Temperature 0 C 188 5 Design temperature 0 C 200 Table-1 In Urea Line-I and 2 plants all the weep holes are connected to conductivity meter based monitoring system. On dated 28/01/2006 the leakage alarm appeared in weep hole number 23 of 11 stream. The weep hole was checked physically and vapour analysed in laboratory fond ammonia vapour and CO2.Immedially shut down was taken and leakage found with instrument air and soap solution the leakage easily detected. For find out the leakage the liner plate behind the weep hole was pressurized with instrument air at the pressure of 0.5 kg/cm2 and other three interconnected weep holes were plugged. Soap solution applied on opposite side of liner. The pin hole leakage easily detected. The pin hole repaired by welding. The repaired portion was passivated with 10 % HNO3 solution and rinse with Demineralised water.The repaired portion was further checked with instrument air and soap solution no leakage was found. The shutdown duration was only 69 hrs Feed cut to feed in. Reactor Liner Leakage on 28/11/2017. On dated 28/11/2017, a weep hole leakage alarm from Weep Hole No. 34 was appeared on lectrotek system. Immediately checked the weep hole No.-34 and vapour analysed in laboratory found ammonia & CO2 vapour and leakage was confirmed. Immediately shut down was taken at 11.15 hrs on dated 28/11/2017.draining of the H.P loop started at 11.15 hrs. For air purging 11 PT-05 A/B cover open for air purging. Man entry permitted at 18.15 hrs on dated 29/11/2017 after confirming ammonia contents less than 25 ppm and Oxygen contents more than 20 %. Four Numbers man ways were opened for detecting leakage the leakage above 5th tray. So the 4 man ways opened. First of all, leakage detection tried with instrument air & soap solution. For detecting the leakage, the instrument air introduced at the pressure of 0.5 kg/cm2 and other three interconnected weep hole plugged that the pressure retains inside the liner and shell. Soap solution applied on liner for detecting the leakage. Four hour tried to leakage but success did not get. After that our further step to detect the leakage with ammonia and phenolphthalein indicator. But leakage could not have detected. As the weep hole leakage was not clear, the exact location the leak could not be fund out with Soap solution and ammonia test. Finally the DP check and number of the spot found. Finally, all the circumferential Seam and longitudinal seam opposite of weep hole No. 34 between 4th & 5th trays welding done. After 713
  • 6. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com that ammonia is introduced at the pressure of 0.4 kg/cm2 n weep hole No. 34 and hold up for 10 hrs. and liner and all welding seal checked by phenolphthalein indicator. No leakage was found and man hole cover boxed up. Start-up activities started and feed in done on dated 01/12/2017 at 11.1 hrs. Total time taken for this shut down was 72 hrs (3 days) feed cut to feed in. Weep hole Monitoring Urea line-1 weep hole monitoring with lectrotek system (Pune). In Urea line-2 Masibus weep hole monitoring system is incorporated. The Micro genie scan is a microprocessor based scanner which has been specially designed for resistance input to monitor reactor leakage easy and very simple in installation low pricing equipmentā€™s and easy in maintenance. This programme containing non-volatile memory for setup data, 4 duals and 4 digit display and LED bar for information RS -232 ā€“C serial port.The instrument is housed in a Ā½ DIN extruded Aluminum rack suitable for control room mounting. A small but highly functional Keyboard consisting of 4 membrane keys is provided as the as the instrument operator interface electrical and I/O temperature are instruments rear Via Screw type terminals. As shown in the figure-2. The electronics is located on modularly designed board for easy field trouble shooting and maintenance. All cards are plug in type and segregated by their function Viz ā€“including power supply CPU, A/D display. All the weep holes have to be checked by passing instrument air every week/fortnight for any leakage and blockage & the pressure of the testing medium should not be more than 0.5 kg/cm2 Fig-2 REACTOR (11-R-1) LEAKAGE JULY-19 The Leakage observed on dated 04/07/2019, during the hydraulic pressurization of the reactor. It was observed that HP loop pressure was not increasing beyond 65 kgcm2 , rather started decreasing (Figure 4). It was noticed that condensate was coming outside from 1st segment (L-seam) of the reactor from inside the insulation. Immediately insulation was removed and it was noticed that the outer shell plate of 08 mm got ruptured from its vertical weld joint (400 mm in length) at 1st segment (L-seam) (Figure 3). Hence, HP loop was depressurized and draining was carried out and top manhole cover was removed for internal inspection. Simultaneously, tray man ways were opened from 1st to 5th tray. To detect the leaky portion inside the reactor, DM water was supplied through flexible hose from outer ruptured portion of the shell course and thorough physical (visual) inspection was carried out inside the reactor. It was found that water was coming out through 1st trayā€™s TSRā€™s newly welded cleat. After insulation removal, it was also noticed that there was bulging on outer (8 mm) layer at the first and fifth segment from the top of the reactor Vertical joint of 1st segment outer shell 8 mm layer welding was found in ruptured condition and bulging of longitudinal pad plate of 5th segment was also noticed. Reason for Failure of Vertical Welding Joint of 1st Segment System hydro-test water entered through the damaged portion of newly welded TSR cleat of the first tray into the coiled layers and reached up to the last layer of 8 mm. 714 714
  • 7. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig-3 As the vent holes and vent tube of the segment were in plugged condition, this resulted in pressurization of the outer shell course, causing rupturing of the 8 mm outer layer vertical joint. The coiled layer welding remained intact; otherwise it could have un winded. Repair and Maintenance After thorough inspection of internal and external damage as well as consent and repair procedure approved from M/s. Saipem, rupture repairing company was contacted for rectification/repair of the reactor within minimum possible time at NFL Vijaipur site itself repair Procedure. Fig -4 Temporary scaffolding was erected from ground floor to top of the reactor for approaching all vent..Tubes and vent holes as well as to carry out the job. Subsequently, whole Insulation was removed from reactor. All the vent holes and vent tubes plugs were de-plugged. All vent tubesā€™ depth was measured, which was found in the range 62 mm and depth of vent holes was found as 40-42 mm. Further cleanliness of the vent tubes and connected vent holes of each 715
  • 8. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com segment was checked with instrument air pressure at 0.3 kg cm2 g and found at clear condition. Maintenance jobs executed to rectify the damaged portion of reactor are as follows: Fig-5 The outer shells (8 mm) of first and fifth segment were removed and replaced with new semi-circular shells made of 16 mm CS plate (SA516 Gr70) in NFL Vijaipur workshop. The TSR leaky point was removed in rectangular shape of size 300 x 200 mm to ensure that the internal layers of the reactor is not damaged and replaced with new patch plate, with separate weep hole for monitoring patch plate liner and welding. The first to fifth TSR as well as its all cleats was replaced with new one. The longitudinal pad plate of the fifth segment was replaced. test, dye penetrate test, magnetic particle test and ultrasonic test of all pressure seams (L, C and nozzle welds) were carried out on the external surface. Visual test, dye penetrate test, ferrite content test of all the internal attachment welds were carried out followed by air and ammonia leak test for weep holes as well as vent holes/vent tubes system of all segments inside the reactor. To facilitate air and ammonia leak test, small loops connecting weep and vent system of 2/3 segments each were made to cover up the whole reactor .Reactor feed in was carried out on 08-07-2019 at 03.00 hours and prilling lined up at 07.30 hours. Again shut down taken on 08/07/2019. Thorough physical inspection of reactor fresh urea deposition was observed at the exit of 70Ā° top vent hole of 3rd segment. It was noticed that fresh urea melt was accumulating at the exit of the said vent hole . Again plant shutdown was taken. After draining/depressurization and flushing of HP loop, reactor manhole cover was removed. Man ways up to 4th tray were opened for inspection and repairing the internal defect. Repairs at 3rd Segment and Inspection Grinding of longitudinal and circumferential seam weld joints was carried out keeping weep holes system and vent tubes/vent holes system pressurized with instrument air at 0.3 kg cm2 g. One pinhole was found on C- seam weld joint of 3rd segment. Patch plate was welded over pinhole point. NDT test was done and clearance received from mechanical team & M/s. L&T for leak test by air and ammonia on 12-07-2019 at 02.00 hours. This time air & ammonia tests were performed at 0.4 kg cm-2g for 2nd and 3rd segment and 0.3 kg cm-2g for 4th segment which was completed on 12-07-2019 at 21.20 hours. No leakage was found with air and ammonia leak test. Further, hydro test of reactor was carried out but water started coming out through 70Ā° vent tube and 250Ā° vent hole (bottom) of 3rd segment at HP loop pressure of 90 kg cm2 g.The leak observed again. Finally system was depressurized and drained. Air leak test as well as Helium test was carried for 2nd , 3rd and 4th segment on 19th and 20th July(Figure-6) The same instrument tapings that were used for the air and ammonia test were used for the helium test. First the system was purged with Nitrogen and then helium was charged from helium cylinder through the vent hole/tube and weep hole system, the system was kept at hold for 4.0 hours at a pressure of 0.3 kg cm2 g, to ensure the 716
  • 9. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig-6 permeation of helium through leakage and cracks. Inside the reactor the segments were divided into smaller isolated portion using sheets and tapes for leak detection . After the hold duration was complete, the leak test was carried out by puncturing the sheet and inserting the analyzer in it. No leakages were detected in the test. Plant Start-up and Monitoring. 717
  • 10. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig--7 (B) LEAKAGE FROM STRIPPER Detail of Stripper The Urea HP Stripper is the equipment where there are the most severe process operating conditions in the Urea Plant. This equipment, that basically is a falling film evaporator, must work under high pressure, temperature and very aggressive process media .Urea Stripper is considered as the backbone of Urea Plant performance and efficiency. Its performance determines production and profitability of end product which is Urea Fertilizer. The equipment design takes into account a trade off between cost and corrosion resistance against the aggressive process media. The result is a carbon steel body sized to withstand the stresses coming from the pressure and temperature loads, while it is protected by a corrosion resistant material barrier in all the parts in contact with the process media including the heat exchange tubes. Reaction products leaving the reactor are sent into bimetallic stripper tubes sides for carbamate decomposition. The medium pressure steam (23 bar) is used for this purpose. The stripper is the high pressure vessel of H.P loop. Operating at 147 bar in tube side pressure and that of shell side is 24 bar. The top temperature of stripper is 190 0 C and that of bottom is 2050 C.at this temperature approximate 80 % of carbamate presents in solution is decomposed and rest are decomposed in MP & LP section. The water is separated in pre-concentrator and two stages of vacuum evaporation sections. The decomposition reaction is a reverse reaction of urea formation. NH4COONH2=NH3 +CO2- HEAT As can be inferred from the equation, decomposition is promoted by reducing pressure and /or adding heat. In M/S. Saipem process decomposition is carried out in three steps. Decomposition is promoted by heating and stripping CO2 by vaporized excess ammonia, according to Henryā€™s Law of partial pressure under the same pressure level as urea reactor. The plant commissioned in 1997 till date stripper is running. During pre-commissioning 55 no of tubes plugged in presence of Saipem representative. Tubes were plugged as Zirconium lining of these tubes was found damaged. In present shut down one damaged old plug replaced with new one and others eight numbers minor 718
  • 11. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig-8 Leakage. Stripper used is falling film type heat exchanger decomposed and vaporized gases and liquid effluent are therefore in counter current contact and CO2 concentration in liquid is gradually reduced from top to bottom of the stripper tubes. 719
  • 12. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig-9 Besides the above, general corrosion has been observed on the bottom tube sheet, tube to tube sheet welding and bottom part of tubes (20 mm). Stripper has rendered service for around 21 years. Two types of stripping process are there; Viz: CO2 stripping and NH3 stripping. Both process work according to shift in partial pressure. This process is the most modern and energy efficient and therefore, widely used now a day. Decomposition at high pressure requires higher temperature, which means that much biuret has formed and the liquid becomes corrosive, but in the M/S. Saipem process the excess of ammonia and the use of Zirconium in the stripper permits minimizing these problems. The off gases generated in stripper are condensed in the high Pressure carbamate condenser where low pressure steam is generated. The NH3 to CO2 mole ratio of 3.5:1 is used and the reactor is operated at a pressure by which the carbamate solution is pumped to the reactor by ejector but not using Carbamate pumps. For passivation of bottom parts of stripper, a passivation compressor also installed to give air in bottom dome. About 42 Nm3 /hr air is feed to stripper bottom.CO2 fed to Reactor normally contains a small percentage of H2, CH4 & CO in addition to inerts like N2& Ar. The passivation air also given to CO2 in 1st stage suction of CO2 compressor. We maintained 0.35 to 0.4% O2in 3rd suction of CO2 compressor. Together with O2 contained in passivation air could give rise to explosiveness problem when sent to CPP for HRU fuel to avoid explosive mixture natural gas also fed to MP condenser so that explosive mixture in inerts gas could not be made. Passivation air presents a major issue for urea process. Designed to prevent the corrosion of stainless steel, passivation air constantly coats the inner surface of stripper tubes with an oxygenated process solution.An ammonia rich gas (CO2 lean gas) rises from lower parts of the tube, then the gas at the upper parts of the tube becomes an ammonia richer gas as compared with equilibrium composition and the decomposition reaction in liquid phase correct the deviation from the equilibrium (the stripping effect). Carbamate is decomposed at reactor pressure with the help of one of the reactants. First thing that comes into mind while going to look for leakage in such high pressure vessel is that, what are the potential points that can lead to leakage in such thick metal walls. There are three surfaces in contact with highly corrosive Carbamate solution. 1. Tube sheet. 2. Tube itself. 3. Tube to tube sheet joint. The tube sheet thickness is 255 mm including 10 mm overlay. The leakage develops when overlay eaten with corrosion/erosion, less passivation. The condensate outlet of stripper collects to steam condensate drum. The rest energy of this steam condensate uses in MP decomposer. In this line conductivity meter also installed for quick indication of leakage ranging 0-500 Āµ mho. Also if there is any leakage in Stripper tubes or tube sheet, it shall be picked up in steam condensate leaving Stripper shell side. This will appear in the form of high conductivity. Monitoring of fresh steam entering into steam drum and condensate leaving the steam drum is very important and its 720
  • 13. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com delta (increase in conductivity of condensate leaving steam drum with respect to incoming steam) will determine the extent of leakage. Reason of leakage The main reason of plug failure is old age of equipment i.e. 21 years old vessel. The old 55 numbers tube plugs failure one by one due to layers of welding gradually deteriorated. Corrosion and exposure of hidden defect in tube-to-tube sheet joint. Fig 10 Detection of the leakage Lack of passivation air. Leakage was so heavy that steam to stripper turned to zero immediately and stripper shell immediately pressurized up to PSV set value i.e. 26 bar, as shown in the Arrangement as shown in the figure- 12, was done for getting tube leakage detection. Blind are provided to following equipment lines. 1. Steam to shell side inlet line 2. Outlet line i.e. V-29 vessel The Shell side pressurized with instrument air at the pressure 7.0 bar and leakage detects with soap solution in top & bottom dome (Channel). Air & soap solution test is the most effective and safe for detection of leakage. Although it is the time consuming test and finding the defects but increasing the inspectors during the test serves the purpose. The test was carried out by pressurizing the shell side with air at 6.5-7.0 bar. After pressurization, inspectors can readily enter into both the channel sides with soap solution and can start finding the leaking points. It requires much of attention and skill of inspector to look for all the defects. Full scanning is must and a cumbersome job. The salient features of this test are: 1. Reliable and effective but time consuming. 2. Good for all small and large leakages. 3. Safe and less risky than ammonia leak test. After the confirmation of leakage in both the channel itā€™s the responsibility of Inspection and welding by expert welder to arrest the leakage in Urea Stripper. Major culprit plug leakage detects easily without applying soap solution air was coming from the damaged plug. For further minor leakage detection, a team was deputed for top & bottom channel. 721
  • 14. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig-11 Old plug removing is very risky When old plug removing the tubes filled with ammonium carbamate & urea solution. So the B.A set and protection apparatus are used to remove the old plugs. Preparation and Installation work can be done by experts of fitting & welding persons. In case of a leak one can easily check if there is any damage of tube sheet as corrosion would start from the inside the tube sheet hole. Replacing a new plug with 2 RE-69(25/22/2) takes max 15 minutes and can be done with a protection mask when ammonia is present. Rectification of defects The rectification of defects was carried out very carefully as it involves welding adjacent to the healthy tubes and tube-to-tube sheet joints. Following guidelines was follow listed below: 1. Grinding was done effectively in order to flush the pin hole completely. Ineffective grinding would never rectify the leaking point. 2. Welding was made after dye-penetrate testing of ground off area. 3. TIG welding with lower heat input was used for rectification. 4. Adjacent tubes and tube sheet weld joints avoided. Certain jigs used for the same in order to concentrate the welding heat where required. 5. Qualification of welder was made before welding in this sensitive area. High heat input will cause burn thru / HAZ area which would eventually be a potential point of leakage. 6. The 2 RE 69 (25/22/2) material plugs were applied on defected tubes. Each and every time leakage was detected with DPT and air/soap solution. 722
  • 15. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig-12 (C ) HP Carbamate Condenser Leakage The gases leaving the top of the stripper are mixed with carbonate coming from the bottom of column medium pressure absorber where they are condensed. Low pressure steam is produced on the shell side of condenser and is fed to the steam network. Temperature of carbamate condensation is determined by shell side steam pressure which is kept constant by pressure controller on L.P. steam network. The vessel having ā€˜Uā€™ tube bundle inside the carbamate. The solution after mixing goes to Carbamate separator then feed to reactor along with ammonia ejector. Schedule for 41-HP loop shut down HP loop draining -5 hours. Depressurization -2 hours. LS purging -4 hours. Water filling -4 hours Over flow -4 hours Draining -10 hours PT-05(HP loop pressure) drop & air purging - 10-12 hours and contd. During shut down. Detection of Leakage 723
  • 16. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com For detection of leakage the tube(process side) manhole cover open and Partion plate removed after that preparation of leakages and inspection like NDT etc. For leakage detection the blind provided at following lines 1. Both PSV Line 2. Condensate export line. 3. Steam cond import lines After providing blinds the entry done in tube side for detecting of leakages with soap solution with instrument air pressurization. The shell side pressurized up to 3.5 kg/cm2 g as shown in the figure-13 Fig-13 After that NDT was done for tube thickness as prier planed. Report: Health assessment of carbamate condenser tubes had been studied by the eddy current testing. A total 3230 tubes were tested in 04 working days with one machine and one technician. The study yielded 34 tubes which is >50 % and above in ID & OD , which need to be plugged to continue to take the unit for further service. The thickness reduction which is <50% will be given in the final report later for your reference. Layout: Condenser has named as 41-Carbamate condenser Top Portion Inlets has been identified top inlet starting from Top to Bottom (rows) left side(columns), and 41-E-5 Bottom portion outlets starting from Bottom to Top(rows) left side(columns). This will be the nomenclature followed throughout our report. SUMMARY: Total Number of tubes to be Plugged Top portion (Inlet) ā€“ 17Tubes Total Tubes - 34 Tubes Bottom Portion (outlet) ā€“ 17 Tubes Conclusion In HP vessels whenever the leakage started shut down must be taken after confirmation.In any leakage development of a specific welding/repair sequence taking into account item complexity, double lining construction and heat treatment requirements. Welders training to maintain a high and homogeneous High pressure welder quality. 724
  • 17. GSJ: Volume 9, Issue 1, January 2021 ISSN 2320-9186 GSJĀ© 2021 www.globalscientificjournal.com Fig-14 It is clear that this is an approach that takes into account only the direct cost of the equipment without any consideration on business losses that as in many cases like ours exceed by far the equipment cost. This option has the overall lowest life cycle cost of all the alternatives evaluated. Corrosion also observed in the stainless steel bimetallic tube next to the tube to tube sheet weld overlay. Corrosion in the 25-22-2 tube underneath the Zirconium tube caused by stagnant zone due to poor bonding. References 1. Urea Reactor Liner Leakage (A Case Study) by Prem Baboo, Published by International Journal of Engineering Research & Technology (Vol. 6 Issue 12, December ā€“ 2017 2. Urea stripper Tube leakage by Prem Baboo, Published by International Journal of Engineering Research & Technology (Vol. 7 Issue 03, March ā€“ 2018 3. New Urea High Pressure Zr Stripper Development by Jorge Versace ( Profertil S.A., Argentina). New Urea HP Zr Stripper Development, 2004. 4. Urea Reactor Liner Leakage - A Case Study by Jagdeep Shah Singh published in Indian Journal of Fertilisers 16 (6) : 608-615, June 2020. 725 View publication stats View publication stats