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Sona Koyo Steering Systems Ltd Dharuhera Team
Welcomes
1/49
Organization & Products
*
DELHI
GURGAON
MUMBAI
Chennai PlantChennai Plant
CHENNAI
Dharuhera Plant
DHARUHERA
PRODUCTS DHR PLANT
Column Electric
Power Steering
Assy. (CEPS)
Pinion Valve
Assy. (PV
Assy.)
Upper Shaft
Dharuhera Plant
Founded : Jul 2006
1st
. SOP started : Jul 2007
Annual Sales F-10 : 264Cr.
Hydraulic Power Steering Assy.
(HPS)
Gurgaon PlantGurgaon Plant
SKSSL Group(Gurgaon, Dharuhera & Chennai)
Products & Customers
Column Electric Power Steering (CEPS)
Hydraulic Power Steering
Customer: Maruti Suzuki India Ltd
Models
Assembly Assembly
Wagon R Alto
Zen Estilo
Customer: Mahindra & Mahindra
Models
Scorpio
Bolero
Productivity improvement on Valve Body Line
Project Selection
Valve Body
Pinion Valve
Assembly
Theme Selection
182,023
206,340
236,340
0
50000
100000
150000
200000
250000
F13 F14 F15
Customer Requirement for HPS
Customer
Requirement
Nos
For HPS Customer Requirement trend increasing
19695
12278
0
10000
20000
30000
CustomerRequirement line Capacity
Capacity VsRequirementpermonth
Gap :
7417
Nos
Problem Statement
Increase Line
capacity by
investing in
new machines
Increase Line
capacity by
doing kaizens
Option
chosen
HPS line capacity found 44 % less compared to customer requirement for F-15
Process Mapping : HPS Group
Understanding Situation
Receipt
store RQA
HPS Assembly
Dispatch
Input Shaft
PV Assembly
Valve Body
Pinion Shaft
Torsion Bar
HPS AssemblyBlockDiagram
21600 21207
12278
44862
0
5000
10000
15000
20000
25000
30000
35000
40000
45000
50000
I.S P.S V.B T.B
Customer requirement Vslinecapacity Customer
Requirement
per month
19695Nos&
Takt Time 56
Capacity
Require
ment
Bottleneck Line :
Gap of 7417 parts
Understanding Situation
ID
Grinding
Gangway
Crack
Detection
Pass Hole
Deburring
& pining
I D
Buffing
Washing
Spline &Slit
Broaching
Slit
GrindingHoning
Sleev
Pressing
I D
Deburring
Pass Hole
Drilling
ID & OD
Buffing
Line Layout & Process flow
Gangway
A-83 A-91 A-74 A-62 B-85
A-88
Induction
Hardening
A-70A-68A-84A-86
B-08For Assy.
Washing
B-10
A-76
Understanding Situation
46 45
35 39 36
90
35 40
52
35
47
36
45
35
0
10
20
30
40
50
60
70
80
90
100
M/c Cycle Time
Cycle Time
CycleTime(Sec)
Understanding Situation
Target
Cycle
Time 55
Sec
HPS line capacity found 44 % less compared to customer requirement for F-15
Target Setting
90
50
5
0
20
40
60
80
100
Current Target
Seconds
Target cycle time for Induction Hardening Process
Manual
Auto
We set target of achieving Induction Hardening process Cycle Time 55 sec
(50 sec Auto +5 sec Manual) by 30th
May-14 .
Action Plan
S.No Activities
Feb-14-Jun-14
Feb March April May Jun July
1 Understanding
Situation
2 Data Collection
3 Analysis
4 Countermeasure
implementation
5 Effectiveness
Monitoring of
Countermeasures
6 Standardization
Analysis
Operation Sequence at
Induction Hardening M/c.
Positioning
Tempering
Unloading
Loading
Cooling
Positioning
I.D Heating
Quenching
PositionIng
Slit Heating
Quenching
Sketch Diagram of Induction Hardening M/c
LoadingI.D. HardeningSlit HardeningTemperingUn-Loading
Three operation (ID Hardening, Slit Hardening & Tempering)
performed for each component
37%
63%
Effective Process Time
Non Effective Process
Time (Transfer Time)
Analysis cont..
Non-effective operation Time for Induction Hardening process
S.No operation Time(sec.)
1 Positioning for I.D Hardening 10
2 Positioning for Slit Hardening 27
3 Positioning for Tempering 10
4 Component Unloading 10
Total Non Effective Time 57
Hence brain storming
done to reduce None
Effective Process time
Effective operation Time for Induction Hardening process
S.No operation Time(sec.)
1 Heating at ID hardening station 8
2 Quenching at I.D hardening station 10
3 Heating at slit Hardening station 3
4 Quenching at slit Hardening 5
5 Heating at Tempering station 3
6 Cooling at tempering station 6
Total Effective Time 33
Cycle Time study done and found only 37 % time is Effective for Process but 63 % time is
not effective for hardening Process to achieve product parameter
Analysis cont..
Break-up of non effective time
Hardening machine
S.No Non Effective Time Time(sec.)
1 Positioning for I.D Hardening 10
2 Positioning for Slit Hardening 27
3 Positioning for Tempering 10
4 Unloading 10
Total Non Effective Time 57
1 Loader Reverse 2
2 Gripper Loading Station Clamp 1
3 Loader Up 1
4 Loader Forward 2
5 Loader Down 1
6 Gripper Loading Station Declamp 1
7 Job lift Up Id Hardening Station 2
8 Job Lift Down I.D hardening Station 1
9 Loader Reverse 2
10 Gripper I.D Station Clamp 1
11 Loader Up 1
12 Loader Forward 2
13 Loader Down 1
14 Gripper I.D Station Declamp 1
15 Job lift Up Slit Hardening Station 2
16 Rotate for Slit Detection 11
17 Job Lift Down Slit Hardening Station 1
18 Ratate for Heating Position 2
19 Job lift Up Slit Hardening Station 2
20 Job lift Down Slit Hardening Station 1
21 Loader Reverse 2
22 Gripper Clamp Slit Hardening Station 1
23 Loader Up 1
24 Loader Forward 2
25 Loader Down 1
26 Gripper Declamp Slit Hardening Station 1
27 Job lift Up Tempering Station 2
28 Job lift Down Tempering Station 1
29 Loader Reverse 2
30 Gripper Clamp Tempering Station 1
31 Loader Up 1
32 Loader Forward 2
33 Loader Down 1
34 Gripper Declamp Tempering Station 1
S.No. Operation Time
PositioningforI.D
Hardening
PositioningforSlitHardeningPositioningforTemperingComponrntUnloading
Analysis cont..
Is this Step Is
necessary ?
Can We
Eliminate ?
Can we
reduce ?
Can we
overlap with
other
activities ?
Conclusion
(Should We
Change it)
1 Loader Reverse 2 P   P Yes
2 Gripper Loading Station Clamp 1 P    No
3 Loader Up 1 P   P Yes
4 Loader Forward 2 P   P Yes
5 Loader Down 1 P   P Yes
6 Gripper Loading Station Declamp 1 P    No
7 Job lift Up Id Hardening Station 2 P    No
8 Job Lift Down I.D hardening Station 1 P    No
9 Loader Reverse 2 P   P Yes
10 Gripper I.D Station Clamp 1 P    No
11 Loader Up 1 P   P Yes
12 Loader Forward 2 P   P Yes
13 Loader Down 1 P   P Yes
14 Gripper I.D Station Declamp 1 P    No
15 Job lift Up Slit Hardening Station 2 P    No
16 Rotate for Slit Detection 11 P  P  Yes
17 Job Lift Down Slit Hardening Station 1 P    No
18 Ratate for Heating Position 2 P    No
19 Job lift Up Slit Hardening Station 2 P    No
20 Job lift Down Slit Hardening Station 1 P    No
21 Loader Reverse 2 P   P Yes
22 Gripper Clamp Slit Hardening Station 1 P    No
23 Loader Up 1 P   P Yes
24 Loader Forward 2 P   P Yes
25 Loader Down 1 P   P Yes
26 Gripper Declamp Slit Hardening Station 1 P    No
27 Job lift Up Tempering Station 2 P    No
28 Job lift Down Tempering Station 1 P    No
29 Loader Reverse 2 P   P Yes
30 Gripper Clamp Tempering Station 1 P    No
31 Loader Up 1 P   P Yes
32 Loader Forward 2 P   P Yes
33 Loader Down 1 P   P Yes
34 Gripper Declamp Tempering Station 1 P    No
ForTemperingForComponrntUnloading
S.No. Time
Questionnaire
Operation
ForI.DHardeningForSlitHardening
Analysis cont..
Problem
Non Effective time is more at Valve body Induction Hardening
M/c
Why-1 Why Non effective (non-Operation) time is more ?
Answer Component Transfer time for different operating is more
Why-2 Why Component Transfer time for different operating is more ?
Answer At a time only single component transfer for different operation.
Why-3 Why single component transfer for different operation?
Answer Process was not optimize for Three component transfer at a time.
Root-cause
At a time only single component transfer for different
operation
Counter measure
At a three component should be transfer for different
operation.
Implementation of Countermeasure
Kaizen-1: Cycle time reduction Induction Hardening machine
O0004(NC PROG) BEFORE
G98
M47(LOADER REVERSE)
M48 (GRIPPER 1 CLAMP)
M44 (LOADER UP)
M46(LOADER FORWARD)
M45 (LOADER DOWN)
M49 (GRIPPER 1 UNCLAMP)
M40
G04P1000
M08
G04P1000
M3S80
M12
G04P1400
M10
M13
G04P10000
M11
M09
G04P500
M41
M47(LOADER REVERSE)
M50(GRIPPER 2 CLAMP)
M44 (LOADER UP)
M46(LOADER FORWARD)
M45 (LOADER DOWN)
M51(GRIPPER 2 UNCLAMP)
G90G01F2000C0.0
G04P500
G90G01G31F2000C359.0
M69
G04P500
G01F2500C-90.0
G04P500
M68
B7500
M70
G04P3000
M19
M71
G04P6000
M20
M69
M47(LOADER REVERSE)
M52(GRIPPER 3 CLAMP)
M44 (LOADER UP)
M46(LOADER FORWARD)
M45 (LOADER DOWN)
M53(GRIPPER 3 UNCLAMP)
M42
M17
T4500
M60
G04P2000
M61
G04P3000
M18
M43
M47(LOADER REVERSE)
M66(GRIPPER 4 CLAMP)
M44 (LOADER UP)
M46(LOADER FORWARD)
M45 (LOADER DOWN)
M67(GRIPPER 4 UNCLAMP)
G04P3000
/M99
M30
N6000M40
M38
M36
M08
M3S27
M12
G04P5700(HARDENING TIME-3)
M10
M36
M13
M39
M83
IF[#1000EQ1]GOTO100
M68
N220IF[#1005EQ1]GOTO350
G90G01F5000C0.0
G90G01F5000C359.9
IF[#1004NE1]GOTO220
M42
M11
M69
M74
T1600(TEMP. POWER)
M17
M70
G04P1800(TEMP TIME)
M71
M75
G90G00F2500C-88.5
M68
IF[#1000EQ1]GOTO100
M11
M37
M17
M64
B5650
M60
G04P1600
M72
M19P1000
M61
M65
M41
M09
M20
M75
M43
M14
M20
M69
G04P1000
M15
M18
IF[#1000EQ1]GOTO100
M73
M20
M47(LOADER REVERSE)
M66 (GRIPPER 4 CLAMP)
M52(GRIPPER 3 CLAMP)
M50(GRIPPER 2 CLAMP)
M48 (GRIPPER 1 CLAMP)
M44 (LOADER UP)
M46(LOADER FORWARD)
M45 (LOADER DOWN)
M67(GRIPPER 4 CLAMP)
M53(GRIPPER 3 CLAMP)
M51(GRIPPER 2 CLAMP)
M49 (GRIPPER 1 UNCLAMP)
M85
G04P600
IF[#1006EQ1]GOTO500
M01
IF[#1001EQ1]GOTO200
GOTO6000
M47
M30
(PRG END)
N100M80
N200M81
N300M82
N350M98P9025
M99
M30
N500M98P2580
M30
4component
transfer at a
time
Only
one
Compo
nent
transfer
at time
Effectiveness of Countermeasure
50
90
72
0
20
40
60
80
100
Target cycle time Before After
Sec
Induction Hardening machine cycle time
Result after kaizen -1
Still
Gap is
22 Sec
Countermeasure-2
Video captured and analysis was done for operation on Induction
Hardening M/c
1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 32 33 34 35 36 37 38 39 40 41 42 43 44 45 46 47 48 49 50 51 52 53 54 55 56 57 58 59 60 61 62 63 64 65 66 67 68 69 70 71 72
1 Positioning
2 Heating
3 Quenching
4 PositionIng
5 Heating
6 Quenching
7 Positioning
8 Heating
9 Cooling
10
CycleTime afteraction(TotalCycleTime72sec.)
Time(Sec.)
Tempering
Unloading
S.No. Operation
IDHardening
Slit hardening
SomeOperation
shouldbe
simultaneously
Operation
timeismore
Countermeasure-2 cont..
After Kaizen Cycle Time 50 sec.
1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 32 33 34 35 36 37 38 39 40 41 42 43 44 45 46 47 48 49 50
1
Positioning
2
Heating
3
Quenching
4
PositionIng
5
Heating
6
Quenching
7
Positioning
8
Heating
9
Cooling
10
Tempering
Unloading
Cycle Time After Condition ( Total Cycle Time 50 sec.)
S.No. Operation
Time (Sec.)
ID Hardening
Slit hardening
LoadingI.D. HardeningSlit HardeningTemperingUn-Loading
Countermeasure-3
LoadingI.D. HardeningSlit HardeningTemperingUn-Loading
Before Condition
Cycle Time 50 sec
After Condition
Cycle Time 48 sec
Component
Loading
Component
Loading
Transfer Time
2 sec reduced
Check Result
50
72
48
0
20
40
60
80
Target cycle time Before After
Sec
Induction Hardening machine cycle time
Standardization
DATE(Origin) 1/7/2007 CHECKED By PREPARED BY
Rev. No : 0
Rev date : -
NEEDED
UNITS PER
SHIFT
A.K Singh Yogesh kumar
STANDARD IN
PROCESSSTOCK
QUALITY CHECK
SAFETY
Sona
Standard
in process
stock
5
Productionp
er hour
40
STANDARDIZEDWORK
CHART
Part No. D040-5911
Process Valve Body Machining
Takt Time
Cycle Time
90 min
1 2 3
DATE(Origin) 1/7/2007 CHECKED By PREPARED BY
Rev. No : 0
Revdate : -
NEEDED
UNITS PER
SHIFT
A.K Singh Yogesh kumar
STANDARD IN
PROCESS STOCK
QUALITY CHECK
SAFETY
Sona
Standard
in process
stock
5
Productionp
er hour
67.9
STANDARDIZEDWORK
CHART
Part No. D040-5911
Process Valve Body Machining
Takt Time
Cycle Time
53 min
1 2 3
SWC Before SWC AFTER
Tangible Benefits
40
67.9
0
10
20
30
40
50
60
70
80
Before After
Nos
Production
per Hour
36
0
0
5
10
15
20
25
30
35
40
Before After
Area(Meter2) Space Saving
9
11.8
0
2
4
6
8
10
12
14
Before After
Nos
Production per
Man Hour
90
0
0
10
20
30
40
50
60
70
80
90
100
Before After
Rupes(Lac)
Capital
Investment
Saving
Intangible benefits
1.Customer requirement fulfilled .
2.Capital investment can be deferred .
3.Highly motivated team
4.Motivated workmen force
5.Encouragement to other Teams
26/49
1. 2.
Future Plans
27/49
Thanks for Kind Attention

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Updated cycle time_reduction_on_valve_body_ih_

  • 1. Sona Koyo Steering Systems Ltd Dharuhera Team Welcomes 1/49
  • 2. Organization & Products * DELHI GURGAON MUMBAI Chennai PlantChennai Plant CHENNAI Dharuhera Plant DHARUHERA PRODUCTS DHR PLANT Column Electric Power Steering Assy. (CEPS) Pinion Valve Assy. (PV Assy.) Upper Shaft Dharuhera Plant Founded : Jul 2006 1st . SOP started : Jul 2007 Annual Sales F-10 : 264Cr. Hydraulic Power Steering Assy. (HPS) Gurgaon PlantGurgaon Plant SKSSL Group(Gurgaon, Dharuhera & Chennai)
  • 3. Products & Customers Column Electric Power Steering (CEPS) Hydraulic Power Steering Customer: Maruti Suzuki India Ltd Models Assembly Assembly Wagon R Alto Zen Estilo Customer: Mahindra & Mahindra Models Scorpio Bolero
  • 4. Productivity improvement on Valve Body Line Project Selection Valve Body Pinion Valve Assembly
  • 5. Theme Selection 182,023 206,340 236,340 0 50000 100000 150000 200000 250000 F13 F14 F15 Customer Requirement for HPS Customer Requirement Nos For HPS Customer Requirement trend increasing
  • 6. 19695 12278 0 10000 20000 30000 CustomerRequirement line Capacity Capacity VsRequirementpermonth Gap : 7417 Nos Problem Statement Increase Line capacity by investing in new machines Increase Line capacity by doing kaizens Option chosen HPS line capacity found 44 % less compared to customer requirement for F-15
  • 7. Process Mapping : HPS Group Understanding Situation Receipt store RQA HPS Assembly Dispatch Input Shaft PV Assembly Valve Body Pinion Shaft Torsion Bar HPS AssemblyBlockDiagram
  • 8. 21600 21207 12278 44862 0 5000 10000 15000 20000 25000 30000 35000 40000 45000 50000 I.S P.S V.B T.B Customer requirement Vslinecapacity Customer Requirement per month 19695Nos& Takt Time 56 Capacity Require ment Bottleneck Line : Gap of 7417 parts Understanding Situation
  • 9. ID Grinding Gangway Crack Detection Pass Hole Deburring & pining I D Buffing Washing Spline &Slit Broaching Slit GrindingHoning Sleev Pressing I D Deburring Pass Hole Drilling ID & OD Buffing Line Layout & Process flow Gangway A-83 A-91 A-74 A-62 B-85 A-88 Induction Hardening A-70A-68A-84A-86 B-08For Assy. Washing B-10 A-76 Understanding Situation
  • 10. 46 45 35 39 36 90 35 40 52 35 47 36 45 35 0 10 20 30 40 50 60 70 80 90 100 M/c Cycle Time Cycle Time CycleTime(Sec) Understanding Situation Target Cycle Time 55 Sec HPS line capacity found 44 % less compared to customer requirement for F-15
  • 11. Target Setting 90 50 5 0 20 40 60 80 100 Current Target Seconds Target cycle time for Induction Hardening Process Manual Auto We set target of achieving Induction Hardening process Cycle Time 55 sec (50 sec Auto +5 sec Manual) by 30th May-14 .
  • 12. Action Plan S.No Activities Feb-14-Jun-14 Feb March April May Jun July 1 Understanding Situation 2 Data Collection 3 Analysis 4 Countermeasure implementation 5 Effectiveness Monitoring of Countermeasures 6 Standardization
  • 13. Analysis Operation Sequence at Induction Hardening M/c. Positioning Tempering Unloading Loading Cooling Positioning I.D Heating Quenching PositionIng Slit Heating Quenching Sketch Diagram of Induction Hardening M/c LoadingI.D. HardeningSlit HardeningTemperingUn-Loading Three operation (ID Hardening, Slit Hardening & Tempering) performed for each component
  • 14. 37% 63% Effective Process Time Non Effective Process Time (Transfer Time) Analysis cont.. Non-effective operation Time for Induction Hardening process S.No operation Time(sec.) 1 Positioning for I.D Hardening 10 2 Positioning for Slit Hardening 27 3 Positioning for Tempering 10 4 Component Unloading 10 Total Non Effective Time 57 Hence brain storming done to reduce None Effective Process time Effective operation Time for Induction Hardening process S.No operation Time(sec.) 1 Heating at ID hardening station 8 2 Quenching at I.D hardening station 10 3 Heating at slit Hardening station 3 4 Quenching at slit Hardening 5 5 Heating at Tempering station 3 6 Cooling at tempering station 6 Total Effective Time 33 Cycle Time study done and found only 37 % time is Effective for Process but 63 % time is not effective for hardening Process to achieve product parameter
  • 15. Analysis cont.. Break-up of non effective time Hardening machine S.No Non Effective Time Time(sec.) 1 Positioning for I.D Hardening 10 2 Positioning for Slit Hardening 27 3 Positioning for Tempering 10 4 Unloading 10 Total Non Effective Time 57 1 Loader Reverse 2 2 Gripper Loading Station Clamp 1 3 Loader Up 1 4 Loader Forward 2 5 Loader Down 1 6 Gripper Loading Station Declamp 1 7 Job lift Up Id Hardening Station 2 8 Job Lift Down I.D hardening Station 1 9 Loader Reverse 2 10 Gripper I.D Station Clamp 1 11 Loader Up 1 12 Loader Forward 2 13 Loader Down 1 14 Gripper I.D Station Declamp 1 15 Job lift Up Slit Hardening Station 2 16 Rotate for Slit Detection 11 17 Job Lift Down Slit Hardening Station 1 18 Ratate for Heating Position 2 19 Job lift Up Slit Hardening Station 2 20 Job lift Down Slit Hardening Station 1 21 Loader Reverse 2 22 Gripper Clamp Slit Hardening Station 1 23 Loader Up 1 24 Loader Forward 2 25 Loader Down 1 26 Gripper Declamp Slit Hardening Station 1 27 Job lift Up Tempering Station 2 28 Job lift Down Tempering Station 1 29 Loader Reverse 2 30 Gripper Clamp Tempering Station 1 31 Loader Up 1 32 Loader Forward 2 33 Loader Down 1 34 Gripper Declamp Tempering Station 1 S.No. Operation Time PositioningforI.D Hardening PositioningforSlitHardeningPositioningforTemperingComponrntUnloading
  • 16. Analysis cont.. Is this Step Is necessary ? Can We Eliminate ? Can we reduce ? Can we overlap with other activities ? Conclusion (Should We Change it) 1 Loader Reverse 2 P   P Yes 2 Gripper Loading Station Clamp 1 P    No 3 Loader Up 1 P   P Yes 4 Loader Forward 2 P   P Yes 5 Loader Down 1 P   P Yes 6 Gripper Loading Station Declamp 1 P    No 7 Job lift Up Id Hardening Station 2 P    No 8 Job Lift Down I.D hardening Station 1 P    No 9 Loader Reverse 2 P   P Yes 10 Gripper I.D Station Clamp 1 P    No 11 Loader Up 1 P   P Yes 12 Loader Forward 2 P   P Yes 13 Loader Down 1 P   P Yes 14 Gripper I.D Station Declamp 1 P    No 15 Job lift Up Slit Hardening Station 2 P    No 16 Rotate for Slit Detection 11 P  P  Yes 17 Job Lift Down Slit Hardening Station 1 P    No 18 Ratate for Heating Position 2 P    No 19 Job lift Up Slit Hardening Station 2 P    No 20 Job lift Down Slit Hardening Station 1 P    No 21 Loader Reverse 2 P   P Yes 22 Gripper Clamp Slit Hardening Station 1 P    No 23 Loader Up 1 P   P Yes 24 Loader Forward 2 P   P Yes 25 Loader Down 1 P   P Yes 26 Gripper Declamp Slit Hardening Station 1 P    No 27 Job lift Up Tempering Station 2 P    No 28 Job lift Down Tempering Station 1 P    No 29 Loader Reverse 2 P   P Yes 30 Gripper Clamp Tempering Station 1 P    No 31 Loader Up 1 P   P Yes 32 Loader Forward 2 P   P Yes 33 Loader Down 1 P   P Yes 34 Gripper Declamp Tempering Station 1 P    No ForTemperingForComponrntUnloading S.No. Time Questionnaire Operation ForI.DHardeningForSlitHardening
  • 17. Analysis cont.. Problem Non Effective time is more at Valve body Induction Hardening M/c Why-1 Why Non effective (non-Operation) time is more ? Answer Component Transfer time for different operating is more Why-2 Why Component Transfer time for different operating is more ? Answer At a time only single component transfer for different operation. Why-3 Why single component transfer for different operation? Answer Process was not optimize for Three component transfer at a time. Root-cause At a time only single component transfer for different operation Counter measure At a three component should be transfer for different operation.
  • 18. Implementation of Countermeasure Kaizen-1: Cycle time reduction Induction Hardening machine O0004(NC PROG) BEFORE G98 M47(LOADER REVERSE) M48 (GRIPPER 1 CLAMP) M44 (LOADER UP) M46(LOADER FORWARD) M45 (LOADER DOWN) M49 (GRIPPER 1 UNCLAMP) M40 G04P1000 M08 G04P1000 M3S80 M12 G04P1400 M10 M13 G04P10000 M11 M09 G04P500 M41 M47(LOADER REVERSE) M50(GRIPPER 2 CLAMP) M44 (LOADER UP) M46(LOADER FORWARD) M45 (LOADER DOWN) M51(GRIPPER 2 UNCLAMP) G90G01F2000C0.0 G04P500 G90G01G31F2000C359.0 M69 G04P500 G01F2500C-90.0 G04P500 M68 B7500 M70 G04P3000 M19 M71 G04P6000 M20 M69 M47(LOADER REVERSE) M52(GRIPPER 3 CLAMP) M44 (LOADER UP) M46(LOADER FORWARD) M45 (LOADER DOWN) M53(GRIPPER 3 UNCLAMP) M42 M17 T4500 M60 G04P2000 M61 G04P3000 M18 M43 M47(LOADER REVERSE) M66(GRIPPER 4 CLAMP) M44 (LOADER UP) M46(LOADER FORWARD) M45 (LOADER DOWN) M67(GRIPPER 4 UNCLAMP) G04P3000 /M99 M30 N6000M40 M38 M36 M08 M3S27 M12 G04P5700(HARDENING TIME-3) M10 M36 M13 M39 M83 IF[#1000EQ1]GOTO100 M68 N220IF[#1005EQ1]GOTO350 G90G01F5000C0.0 G90G01F5000C359.9 IF[#1004NE1]GOTO220 M42 M11 M69 M74 T1600(TEMP. POWER) M17 M70 G04P1800(TEMP TIME) M71 M75 G90G00F2500C-88.5 M68 IF[#1000EQ1]GOTO100 M11 M37 M17 M64 B5650 M60 G04P1600 M72 M19P1000 M61 M65 M41 M09 M20 M75 M43 M14 M20 M69 G04P1000 M15 M18 IF[#1000EQ1]GOTO100 M73 M20 M47(LOADER REVERSE) M66 (GRIPPER 4 CLAMP) M52(GRIPPER 3 CLAMP) M50(GRIPPER 2 CLAMP) M48 (GRIPPER 1 CLAMP) M44 (LOADER UP) M46(LOADER FORWARD) M45 (LOADER DOWN) M67(GRIPPER 4 CLAMP) M53(GRIPPER 3 CLAMP) M51(GRIPPER 2 CLAMP) M49 (GRIPPER 1 UNCLAMP) M85 G04P600 IF[#1006EQ1]GOTO500 M01 IF[#1001EQ1]GOTO200 GOTO6000 M47 M30 (PRG END) N100M80 N200M81 N300M82 N350M98P9025 M99 M30 N500M98P2580 M30 4component transfer at a time Only one Compo nent transfer at time
  • 19. Effectiveness of Countermeasure 50 90 72 0 20 40 60 80 100 Target cycle time Before After Sec Induction Hardening machine cycle time Result after kaizen -1 Still Gap is 22 Sec
  • 20. Countermeasure-2 Video captured and analysis was done for operation on Induction Hardening M/c 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 32 33 34 35 36 37 38 39 40 41 42 43 44 45 46 47 48 49 50 51 52 53 54 55 56 57 58 59 60 61 62 63 64 65 66 67 68 69 70 71 72 1 Positioning 2 Heating 3 Quenching 4 PositionIng 5 Heating 6 Quenching 7 Positioning 8 Heating 9 Cooling 10 CycleTime afteraction(TotalCycleTime72sec.) Time(Sec.) Tempering Unloading S.No. Operation IDHardening Slit hardening SomeOperation shouldbe simultaneously Operation timeismore
  • 21. Countermeasure-2 cont.. After Kaizen Cycle Time 50 sec. 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 32 33 34 35 36 37 38 39 40 41 42 43 44 45 46 47 48 49 50 1 Positioning 2 Heating 3 Quenching 4 PositionIng 5 Heating 6 Quenching 7 Positioning 8 Heating 9 Cooling 10 Tempering Unloading Cycle Time After Condition ( Total Cycle Time 50 sec.) S.No. Operation Time (Sec.) ID Hardening Slit hardening
  • 22. LoadingI.D. HardeningSlit HardeningTemperingUn-Loading Countermeasure-3 LoadingI.D. HardeningSlit HardeningTemperingUn-Loading Before Condition Cycle Time 50 sec After Condition Cycle Time 48 sec Component Loading Component Loading Transfer Time 2 sec reduced
  • 23. Check Result 50 72 48 0 20 40 60 80 Target cycle time Before After Sec Induction Hardening machine cycle time
  • 24. Standardization DATE(Origin) 1/7/2007 CHECKED By PREPARED BY Rev. No : 0 Rev date : - NEEDED UNITS PER SHIFT A.K Singh Yogesh kumar STANDARD IN PROCESSSTOCK QUALITY CHECK SAFETY Sona Standard in process stock 5 Productionp er hour 40 STANDARDIZEDWORK CHART Part No. D040-5911 Process Valve Body Machining Takt Time Cycle Time 90 min 1 2 3 DATE(Origin) 1/7/2007 CHECKED By PREPARED BY Rev. No : 0 Revdate : - NEEDED UNITS PER SHIFT A.K Singh Yogesh kumar STANDARD IN PROCESS STOCK QUALITY CHECK SAFETY Sona Standard in process stock 5 Productionp er hour 67.9 STANDARDIZEDWORK CHART Part No. D040-5911 Process Valve Body Machining Takt Time Cycle Time 53 min 1 2 3 SWC Before SWC AFTER
  • 25. Tangible Benefits 40 67.9 0 10 20 30 40 50 60 70 80 Before After Nos Production per Hour 36 0 0 5 10 15 20 25 30 35 40 Before After Area(Meter2) Space Saving 9 11.8 0 2 4 6 8 10 12 14 Before After Nos Production per Man Hour 90 0 0 10 20 30 40 50 60 70 80 90 100 Before After Rupes(Lac) Capital Investment Saving
  • 26. Intangible benefits 1.Customer requirement fulfilled . 2.Capital investment can be deferred . 3.Highly motivated team 4.Motivated workmen force 5.Encouragement to other Teams 26/49
  • 28. Thanks for Kind Attention