17. Tuning our System Proportional Control First Attempt
Rise Time = 60s
Offset difference = 25 (g/L)
Control Effort saturates at at 40s
18. Tuning Our System Proportional Control Second
Attempt
Rise Time = 68s
Offset Differences = 11 g/L
Control Effort does not show any saturation
19. Tuning Our System Proportional Control Third
Attempt
Rise Time - N/A
Offset Difference - 75 g/L Control Effort immediately saturates and
the auger did not move
20. Tuning Our System PI Control First Attempt
Rise Time - 37s
Offset difference - 56 g/L
Control effort is stable at 0.045 until 8s and
then saturates at 13s and auger stops
working.
21. Tuning Our System PI Control Second Attempt
Rise time - 83s
Overshoot - 1.16
Control effort heads toward saturation at
7s but works its way back up around 80s
22. Tuning Our System PI Control Third Attempt
Rise Time - 183s
System stayed at setpoint for 30s
Control Effort does not saturate and
remains stable
23. Setpoint Change - Raising Setpoint
Time to reach new setpoint:
120 s
27. Challenges
1. Not able to directly measure sugar concentration
2. Building around the load cell
a. Placement of hot plate
b. How to build a platform on load cell
c. Determining our batch size
3. Flow meter
4. Pump start up
5. The ALBERT II
6. How to dissolve sugar
7. PID tuning
28. VI Improvements
-Add a sequence structure to the VI that will turn off the pump and load cell once
the PID system is turned off
-Find a way to tare the load cell at the beginning of each batch
-Program the system so that the auger and pump turn on simultaneously instead of
turning them both in separately
- Find a way to incorporate the flow meter
- Figure out why we couldn’t start with an integral time right away
29. Hardware Improvements
-Develop a way to more permanently attach the auger screw to the stepper motor
-Develop a method that allows for aggressive agitation of the brewing vessel in
order to increase the rate at which sugar dissolves into the unsweetened tea
-Stronger pump for faster addition of unsweetened tea
-Stop sugar from escaping out the back of the system and prevent it from getting
into the auger shaft
30. Conclusion
-We feel that our project performed in a satisfactory manner.
-We were able to complete all of our goals, namely we were able to control the
sugar concentration of a batch of sweet tea.
Editor's Notes
Sam
Michael
explain why the frame is the way it is
Michael
had to use the squarejoints becasue the drill piece that is used to thread the metal was broken
Noah
Pump- buildup time
Auger - 2 parts, screw and stepper motor, pump given constant voltage, stepper motor given pulses
Sam
Sam
Noah
Inverse time target - same as frequency, gives linear equation
Large tau value due in part to method of measuring flow rate - load cell has own tau value
Michael
Load cell gain around the 1180 range
Used a 200 ohm resistor to increase the sensitivity
Michael
Michael
Noah - block diagram, Sam - Front Panel
Michael
Sam
Noah
Difference due to limitations of stepper motor
Michael
Sam
Sam
Sam
Sam
Sam
Sam
Noah
Drop in control effort (period)
Noah
Rise in Control effort
Noah
Noah
Got around by subtraction, difference in masses
Brew location/single screw applying a moment/limitations of load cell
Couldn’t get the flow meter to work
fed into ln eqn
made sure all connections were good
heating/stirring
discuss strategy again