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ABSTRACT FOR USER CASE STUDY
                      17th International Pump Users Symposium

Title:

“SUCCESSFUL MODIFICATION OF VERTICAL-TURBINE PUMPS FOR CAPACITY
AND RELIABILITY IMPROVEMENT”

Abstract:

A modification of seven 560 hp vertical-turbine pumps was carried out with outstanding
results to improve their actual capacity. The installation was limited to 64% of its rated
capacity, which was never reached, and the operating demand required to maintain all
seven pumps in continuous service. Reliability of the pumps was additionaly impaired by
severe cavitation damage of impellers.

A plant revamp required increased and reliable cooling water flow, with a limited time
frame of seven months for full implementation. Original cast iron impellers were reverse
engineered and manufactured oversize in 18Cr-16Mn steel. Bowls were modified for the
larger impellers. Performance for all pumps was adjusted in a test stand and the efficiency
improved not to exceed the rated horsepower of installed electric motors.

As a result, the capacity of the installation reached its rated value. Operation was
optimized with six pumps in operation and one in standby feeding 33% more water. After
26 months in service, none of the pumps had shown capacity drop or required
maintenance beyond repacking. Significant savings were attained compared to the
installation of new pumps.



AUTHOR:

César A. Morales Casanova
Rotating Equipment Specialist
PDVSA – Pequiven
UNF Morón, Edo. Carabobo
Venezuela
®

        17th International Pump Users Symposium
        March 6-9, 2000. Houston, Texas




  SUCCESSFUL MODIFICATION
 OF VERTICAL-TURBINE PUMPS
       FOR CAPACITY
AND RELIABILITY IMPROVEMENT

                                          César A. Morales Casanova
                                          Rotating Equipment Specialist
                                          PDVSA-Pequiven
                                          Edo. Carabobo - Venezuela
SITUATION OVERVIEW

28 year old Cooling Tower servicing a 600 MTD
Ammonia Plant and a 750 MTD Urea Plant.
Seven 560 HP cooling water pumps installed (Four
turbine driven and three motor driven). European
OEM.
An additional pump kept as a spare.
SITUATION OVERVIEW (cont...)

Pump efficiency was reduced due to severe
cavitation damage of impellers, causing additional
limitations to cooling water feed.




     IMPELLER CONDITION AFTER 1 YR IN SERVICE
PROJECT SCOPE / OBJECTIVES-PREMISES

Ammonia plant revamp to 680 MTD to be implemented.
Reliable and increased cooling water flow up to 16,000
m3/hr (70,400 GPM) required.
Seven months available for full implementation:
   • Workscope analysis started by mid August 1996.
   • Equipment required in service by May 1997.
CAPACITY EVALUATION OF EXISTING PUMPS

One pump completely overhauled for testing.
A new impeller –as supplied by the OEM– installed.
TEST-STAND RESULTS – UNMODIFIED PUMP
        PUBLISHED VS. TEST PERFORMANCE
       OEM IMPELLER φ550/500 mm @1170 RPM
TEST RESULTS OF EXISTING PUMP
     PUBLISHED VS. TEST PERFORMANCE
    OEM IMPELLER φ550/500 mm @1170 RPM
TEST-STAND RESULTS – UNMODIFIED PUMP
 Actual capacity @ rated head found 33% below:
   Found:         2,000 m3/hr (8,800 GPM)
   Rated:         3,000 m3/hr (13,200 GPM)
 Pump could not reach rated flow:
   Max attainable: 2,970 m3/hr (13,068 GPM)
 TDH nearest rated flow was 75% below:
   Found:         9.5 m (30 ft)
   Rated:         38.0 m (125 ft)
 BEP was found at 79% of the expected flow and well
 below in efficiency:
   Found:          64% @ 2,200 m3/hr (9,680 GPM)
   Expected:       83% @ 2,800 m3/hr (12,320 GPM)
TEST-STAND RESULTS – UNMODIFIED PUMP
   CONCLUSIONS / RECOMMENDATIONS
 Considerable performance impairment compared
 to expected.
 Impeller subject to severe cavitation before
 reaching rated flow.
 Significant improvement not possible              by
 reworking of existing impellers (underfilling).
 Major modifications     required    to   accomplish
 project objectives.
 A prototype pump to be modified and re-tested.
PLANNED MODIFICATIONS - IMPELLER
Largest oversize impeller that could be fitted in
existing bowls locally manufactured.
Material improved from Cast Iron to cavitation
resistant Stainless Steel 18Cr-16Mn Alloy.
PLANNED MODIFICATIONS – BOWL
Suction Bell fit diameter
increased.
GAP “A” set to 2.5 mm
(0.10 in).
Diffuser vanes cut back.
Leading edges thinned &
rounded.
Even number of vanes for
both impeller and diffuser:
 •   6 vane impeller.
 •   8 vane diffuser.
Gap “B” set to 10% of new
impeller vane radius = 30
mm (1.18 in).
MODIFIED COMPONENTS - NEW IMPELLER




 FIRST IMPROVED IMPELLER “AS SUPPLIED”- DEC’96
MODIFIED COMPONENTS – BOWL REWORK




IMPELLER TEMPLATE INSERTED   VANE ROUGH CUT




    VANE CUT MARKING         FINISHED BOWL
TEST-STAND RESULTS – PROTOTYPE PUMP
          PUBLISHED VS. TEST PERFORMANCE
   AS RECEIVED NEW IMPELLER φ590/540 mm @1188 RPM
TEST-STAND RESULTS – PROTOTYPE PUMP
          PUBLISHED VS. TEST PERFORMANCE
   AS RECEIVED NEW IMPELLER φ590/540 mm @1188 RPM
TEST-STAND RESULTS – PROTOTYPE PUMP
Actual capacity @ rated head found 8% above:
  Found:           3,250 m3/hr (14,300 GPM)
  Rated:           3,000 m3/hr (13,200 GPM)
Pump exceeded rated flow:
  Max attainable: 3,400 m3/hr (14,960 GPM)
TDH @ rated flow/rpm was 10% above:
  Found:          42 m (138 ft)
  Rated:          38 m (125 ft)
BEP found @ rated flow and slightly below in efficiency:
  Found:         79% @ 3,000 m3/hr (13,200 GPM)
  OEM Published: 83% @ 2,800 m3/hr (12,320 GPM)
BEP found @ rated flow and slightly below in efficiency:
  Max HP:        620 @ 3,000 m3/hr (13,200 GPM)
  Motor HP:      562 (1.0 S.F.)
TEST-STAND RESULTS – PROTOTYPE PUMP
  CONCLUSIONS / RECOMMENDATIONS

 Performance significantly improved.
 Rated point easily reached and exceeded.
 BEP matched rated flow.
 Limitation in available power from installed
 electrical motors.
 Impeller rework required to adjust performance.
 Efficiency improvement required to reach rated
 point and limit power requirement.
PERFORMANCE ADJUSTMENT
    IMPELLER REWORK
          Vanes trimmed.
          Shrouds not machined to keep
          GAP “A” at 2.5 mm (0.10 in).
          Vane exit under/overfilled.
          Vane leading edge rounded &
          thinned to improve NPSHR.
          Vane surface finish improved to
          increase efficiency.
PERFORMANCE ADJUSTMENT
             IMPELLER REWORK




  “AS SUPPLIED” VANE EXIT     “AS SUPPLIED” ROUGH VANE SURFACE




ADJUSTED (UNDER/OVERFILLED)             VANES POLISHED
         VANE EXIT                   LEAD EDGE ROUND & THIN
TEST STAND RESULTS - FINAL
     PUBLISHED VS. TEST PERFORMANCE
REWORKED NEW IMPELLER φ577/527 mm @1188 RPM
TEST STAND RESULTS - FINAL
     PUBLISHED VS. TEST PERFORMANCE
REWORKED NEW IMPELLER φ577/527 mm @1188 RPM
TEST STAND RESULTS - FINAL

 Operating point closely adjusted:
      TDH @ rated flow within +5% of rated value.
 Efficiency at BEP improved by 3 points:
    Final:               82%
    Before adjustment: 79%
 Shaft horsepower adjusted:
      Max BHP within +1.5% of motor nameplate value (*)



* (Pump BHP based on electrical measurements, ηmec assumed 90%).
OVERALL RESULTS
Pump improvement completed on time, in May ’97.
Optimized operation:
   • Installed capacity fully recovered (155% increase).
   • 6 pump running / 1 stand-by.
   • 18,000 m3/hr (79,200 GPM) continuously delivered.
Increased reliability:
   •   Pump performance sustained after 2-1/2 years.
   •   Extended impeller service life.
   •   Maintenance costs significantly reduced
Savings of US$ 1.4 million compared to the alternative of
replacing existing pumps.
Eight pumps were modified at the cost of a single new
unit (approx. US$ 200 k)
RESULTS – IMPELLER SERVICE LIFE




     AGOSTO 1996 – 1 YEAR IN SERVICE




     MAY 1997 - FEB 2000 – 3 YEARS IN SERVICE
RESULTS – MAINTENANCE REDUCTION
CONCLUSIONS

Pumps successfully upgraded by simple impeller-
bowl modifications.
Better metallurgy in pump impellers, together with
smooth vane surface finish and operation close to the
BEP, provided significant service life improvement in
conditions where cavitation-corrosion damage can
develop.
Stand-testing of modified pumps allowed reliable
performance adjustment for trouble-free start-up at
the field .
Expected performance of original equipment should
have been overrated.
LESSONS LEARNED

Evaluate the possibilities for improvement of existing
equipment before considering their replacement .
Simple solutions to the root cause of problems may
provide good results and considerable savings .
Equipment to be delivered on turn-key projects must
have specifications for procurement, written by the
user or on a user basis, in order to ensure long-term,
trouble-free operation and reduced maintenance costs.
Choose a reliable supplier as “partner.”
REFERENCES

Mc. Caul, Colin. An Advanced Cavitation Resistant Austenitic Steel
for Pumps. Corrosion 96, The NACE International Annual Conference
and Exposition. Paper Nº 415, 1996.
Bloch, Heinz P., Geitner, Fred K. Machinery Failure Analysis and
Troubleshooting. 2nd Edition. 1993. Page 44-46. Gulf Publishing
Company
Bloch, Heinz P. Pump Reliability Improvement Program. Pump
Failure Reduction Programs. PRIME Seminar notes
Pfleiderer, Carl. Bombas Centrífugas y Turbocompresores. Editorial
Labor, 1960.
THANK YOU !

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Successful Modification of Vertical-Turbine Pumps for Capacity and Reliability Improvement

  • 1. ABSTRACT FOR USER CASE STUDY 17th International Pump Users Symposium Title: “SUCCESSFUL MODIFICATION OF VERTICAL-TURBINE PUMPS FOR CAPACITY AND RELIABILITY IMPROVEMENT” Abstract: A modification of seven 560 hp vertical-turbine pumps was carried out with outstanding results to improve their actual capacity. The installation was limited to 64% of its rated capacity, which was never reached, and the operating demand required to maintain all seven pumps in continuous service. Reliability of the pumps was additionaly impaired by severe cavitation damage of impellers. A plant revamp required increased and reliable cooling water flow, with a limited time frame of seven months for full implementation. Original cast iron impellers were reverse engineered and manufactured oversize in 18Cr-16Mn steel. Bowls were modified for the larger impellers. Performance for all pumps was adjusted in a test stand and the efficiency improved not to exceed the rated horsepower of installed electric motors. As a result, the capacity of the installation reached its rated value. Operation was optimized with six pumps in operation and one in standby feeding 33% more water. After 26 months in service, none of the pumps had shown capacity drop or required maintenance beyond repacking. Significant savings were attained compared to the installation of new pumps. AUTHOR: César A. Morales Casanova Rotating Equipment Specialist PDVSA – Pequiven UNF Morón, Edo. Carabobo Venezuela
  • 2. ® 17th International Pump Users Symposium March 6-9, 2000. Houston, Texas SUCCESSFUL MODIFICATION OF VERTICAL-TURBINE PUMPS FOR CAPACITY AND RELIABILITY IMPROVEMENT César A. Morales Casanova Rotating Equipment Specialist PDVSA-Pequiven Edo. Carabobo - Venezuela
  • 3. SITUATION OVERVIEW 28 year old Cooling Tower servicing a 600 MTD Ammonia Plant and a 750 MTD Urea Plant. Seven 560 HP cooling water pumps installed (Four turbine driven and three motor driven). European OEM. An additional pump kept as a spare.
  • 4. SITUATION OVERVIEW (cont...) Pump efficiency was reduced due to severe cavitation damage of impellers, causing additional limitations to cooling water feed. IMPELLER CONDITION AFTER 1 YR IN SERVICE
  • 5. PROJECT SCOPE / OBJECTIVES-PREMISES Ammonia plant revamp to 680 MTD to be implemented. Reliable and increased cooling water flow up to 16,000 m3/hr (70,400 GPM) required. Seven months available for full implementation: • Workscope analysis started by mid August 1996. • Equipment required in service by May 1997.
  • 6. CAPACITY EVALUATION OF EXISTING PUMPS One pump completely overhauled for testing. A new impeller –as supplied by the OEM– installed.
  • 7. TEST-STAND RESULTS – UNMODIFIED PUMP PUBLISHED VS. TEST PERFORMANCE OEM IMPELLER φ550/500 mm @1170 RPM
  • 8. TEST RESULTS OF EXISTING PUMP PUBLISHED VS. TEST PERFORMANCE OEM IMPELLER φ550/500 mm @1170 RPM
  • 9. TEST-STAND RESULTS – UNMODIFIED PUMP Actual capacity @ rated head found 33% below: Found: 2,000 m3/hr (8,800 GPM) Rated: 3,000 m3/hr (13,200 GPM) Pump could not reach rated flow: Max attainable: 2,970 m3/hr (13,068 GPM) TDH nearest rated flow was 75% below: Found: 9.5 m (30 ft) Rated: 38.0 m (125 ft) BEP was found at 79% of the expected flow and well below in efficiency: Found: 64% @ 2,200 m3/hr (9,680 GPM) Expected: 83% @ 2,800 m3/hr (12,320 GPM)
  • 10. TEST-STAND RESULTS – UNMODIFIED PUMP CONCLUSIONS / RECOMMENDATIONS Considerable performance impairment compared to expected. Impeller subject to severe cavitation before reaching rated flow. Significant improvement not possible by reworking of existing impellers (underfilling). Major modifications required to accomplish project objectives. A prototype pump to be modified and re-tested.
  • 11. PLANNED MODIFICATIONS - IMPELLER Largest oversize impeller that could be fitted in existing bowls locally manufactured. Material improved from Cast Iron to cavitation resistant Stainless Steel 18Cr-16Mn Alloy.
  • 12. PLANNED MODIFICATIONS – BOWL Suction Bell fit diameter increased. GAP “A” set to 2.5 mm (0.10 in). Diffuser vanes cut back. Leading edges thinned & rounded. Even number of vanes for both impeller and diffuser: • 6 vane impeller. • 8 vane diffuser. Gap “B” set to 10% of new impeller vane radius = 30 mm (1.18 in).
  • 13. MODIFIED COMPONENTS - NEW IMPELLER FIRST IMPROVED IMPELLER “AS SUPPLIED”- DEC’96
  • 14. MODIFIED COMPONENTS – BOWL REWORK IMPELLER TEMPLATE INSERTED VANE ROUGH CUT VANE CUT MARKING FINISHED BOWL
  • 15. TEST-STAND RESULTS – PROTOTYPE PUMP PUBLISHED VS. TEST PERFORMANCE AS RECEIVED NEW IMPELLER φ590/540 mm @1188 RPM
  • 16. TEST-STAND RESULTS – PROTOTYPE PUMP PUBLISHED VS. TEST PERFORMANCE AS RECEIVED NEW IMPELLER φ590/540 mm @1188 RPM
  • 17. TEST-STAND RESULTS – PROTOTYPE PUMP Actual capacity @ rated head found 8% above: Found: 3,250 m3/hr (14,300 GPM) Rated: 3,000 m3/hr (13,200 GPM) Pump exceeded rated flow: Max attainable: 3,400 m3/hr (14,960 GPM) TDH @ rated flow/rpm was 10% above: Found: 42 m (138 ft) Rated: 38 m (125 ft) BEP found @ rated flow and slightly below in efficiency: Found: 79% @ 3,000 m3/hr (13,200 GPM) OEM Published: 83% @ 2,800 m3/hr (12,320 GPM) BEP found @ rated flow and slightly below in efficiency: Max HP: 620 @ 3,000 m3/hr (13,200 GPM) Motor HP: 562 (1.0 S.F.)
  • 18. TEST-STAND RESULTS – PROTOTYPE PUMP CONCLUSIONS / RECOMMENDATIONS Performance significantly improved. Rated point easily reached and exceeded. BEP matched rated flow. Limitation in available power from installed electrical motors. Impeller rework required to adjust performance. Efficiency improvement required to reach rated point and limit power requirement.
  • 19. PERFORMANCE ADJUSTMENT IMPELLER REWORK Vanes trimmed. Shrouds not machined to keep GAP “A” at 2.5 mm (0.10 in). Vane exit under/overfilled. Vane leading edge rounded & thinned to improve NPSHR. Vane surface finish improved to increase efficiency.
  • 20. PERFORMANCE ADJUSTMENT IMPELLER REWORK “AS SUPPLIED” VANE EXIT “AS SUPPLIED” ROUGH VANE SURFACE ADJUSTED (UNDER/OVERFILLED) VANES POLISHED VANE EXIT LEAD EDGE ROUND & THIN
  • 21. TEST STAND RESULTS - FINAL PUBLISHED VS. TEST PERFORMANCE REWORKED NEW IMPELLER φ577/527 mm @1188 RPM
  • 22. TEST STAND RESULTS - FINAL PUBLISHED VS. TEST PERFORMANCE REWORKED NEW IMPELLER φ577/527 mm @1188 RPM
  • 23. TEST STAND RESULTS - FINAL Operating point closely adjusted: TDH @ rated flow within +5% of rated value. Efficiency at BEP improved by 3 points: Final: 82% Before adjustment: 79% Shaft horsepower adjusted: Max BHP within +1.5% of motor nameplate value (*) * (Pump BHP based on electrical measurements, ηmec assumed 90%).
  • 24. OVERALL RESULTS Pump improvement completed on time, in May ’97. Optimized operation: • Installed capacity fully recovered (155% increase). • 6 pump running / 1 stand-by. • 18,000 m3/hr (79,200 GPM) continuously delivered. Increased reliability: • Pump performance sustained after 2-1/2 years. • Extended impeller service life. • Maintenance costs significantly reduced Savings of US$ 1.4 million compared to the alternative of replacing existing pumps. Eight pumps were modified at the cost of a single new unit (approx. US$ 200 k)
  • 25. RESULTS – IMPELLER SERVICE LIFE AGOSTO 1996 – 1 YEAR IN SERVICE MAY 1997 - FEB 2000 – 3 YEARS IN SERVICE
  • 27. CONCLUSIONS Pumps successfully upgraded by simple impeller- bowl modifications. Better metallurgy in pump impellers, together with smooth vane surface finish and operation close to the BEP, provided significant service life improvement in conditions where cavitation-corrosion damage can develop. Stand-testing of modified pumps allowed reliable performance adjustment for trouble-free start-up at the field . Expected performance of original equipment should have been overrated.
  • 28. LESSONS LEARNED Evaluate the possibilities for improvement of existing equipment before considering their replacement . Simple solutions to the root cause of problems may provide good results and considerable savings . Equipment to be delivered on turn-key projects must have specifications for procurement, written by the user or on a user basis, in order to ensure long-term, trouble-free operation and reduced maintenance costs. Choose a reliable supplier as “partner.”
  • 29. REFERENCES Mc. Caul, Colin. An Advanced Cavitation Resistant Austenitic Steel for Pumps. Corrosion 96, The NACE International Annual Conference and Exposition. Paper Nº 415, 1996. Bloch, Heinz P., Geitner, Fred K. Machinery Failure Analysis and Troubleshooting. 2nd Edition. 1993. Page 44-46. Gulf Publishing Company Bloch, Heinz P. Pump Reliability Improvement Program. Pump Failure Reduction Programs. PRIME Seminar notes Pfleiderer, Carl. Bombas Centrífugas y Turbocompresores. Editorial Labor, 1960.