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D
unmurry Wastewater Treatment Works (WwTW) is located on the outskirts of Dunmurry Village, on the Lisburn
side of Belfast City. It is located on the banks of the River Lagan, approximately 8km south of Belfast City centre.
Previous upgrades were carried out in 1984 when modern inlet screening, grit plant, and storm storage were
added, and in 1999, when a tertiary filtration plant and sludge dewatering plant were added to help improve the
treatment and reduce the operational transport of sludges from the site. This was successfully operated for many
years, but in 2009 the works failed to comply with its discharge consents and an upgrade was urgently required
to meet the growing population in the area. NI Water invested £5.5 million to upgrade the Dunmurry treatment
process capacity to PE 62,500 and meet the required standards. Work commenced at the site in June 2010, and was
completed in June 2012.
Objectives/need
The old treatment works was in need of modernisation; nearly all
elements of the works operation were manual or required manual
intervention. The plant demanded two full time operators, with
support from M&E and additional reclamation staff in order to
maintain compliance. De-sludging, returning storm and general
site maintenance operations were manually carried out, which
resulted in significant overtime on weekends and very careful
sludgemanagementtodealwiththelackofcapacity.Frequentlythe
sludge export had to be carried out after hours in order to provide
sufficient space for holiday periods and planned maintenance.
www.WaterProjectsOnline.com	 Wastewater Treatment & Sewerage
UK Water Projects 2012	 Page 67
Dunmurry WwTW
£5.5m upgrade to an outdated works in South Belfast to serve an increasing
population and meet nitrogen and phosphorous consent conditions
by Derek Crabbe BSc (Hons)
Dunmurry WwTW – Aeration tank fine bubble membrane installation - Courtesy of NI Water
This upgrade was also designed to meet new total nitrogen and
total phosphorous discharge consent conditions. It will also ensure
the works can meet its future full flow to treatment capacity and
allow for further development in the catchments.
The works required modernisation to automate the treatment
process. It required modern control functionality such as historical
data recording to ensure it was compliant with the permits and
licensing agreements. The new control plant shall utilise SCADA
Wiscon and operator controls shall be via one of three touch screen
HMIs on the site.
Wastewater Treatment & Sewerage	 www.WaterProjectsOnline.com
Page 68	 UK Water Projects 2012
This software also allows the site manager to remote dial up to the
site, and provides them with full control of any plant connected
to the PLC network. This provides invaluable information for the
managers when alarms occur out of hours!
Operations required a robust plant that would deliver consistent
treatment for the lowest operating cost. The plant chosen was
based around an activated sludge process, which was similar to
the original plant and is familiar to the operators. It also provides
a flexible treatment process which will treat the current flows and
respond to the increased capacity demands for the area in the
future. The future consent standards to be achieved are:
Parameter 95 Percentile Upper tier limit
Biochemical
Oxygen Demand
10mg/l 50mg/l
Suspended Solids 25mg/l 65mg/l
Ammonia 2.5mg/l 10mg/l
Total Phosphorous
as P
n/a 2mg/l (annual average)
Total Nitrogen as N n/a 15mg/l (annual average)
The aim of the works upgrade is to provide a treatment facility that
complies with European Union legalisation, and it is designed to
meet these needs for South Belfast catchments up to the year 2030.
Considering the projected combined population growth in the
area, the works has been designed to 62,500 PE.
Solution
The existing site was selected as the obvious location to construct
theupgrade,asthesitebenefitedfromalltheplanningrequirements
to provide a WwTW. Space on the site was at a premium, and the
optimum location was chosen with the requirement to carry out
a substantial excavation. While this location for the main tank was
on an embankment, the location still allowed for a relatively easy
connection as a parallel process and negated the need for pumping
or affecting the existing plant hydraulics.
The existing tanks, which were previously surface aerated, now
presented the opportunity to fit fine bubble aeration, a more
efficient process and more economical to operate. Additional
controls were also possible and now the plant operates much more
efficiently where the aeration capacity is increased to match the
demand. The new aeration lane was designed in accordance with
the latest research into aeration lane design. The split structure is
approximately 80m long x 18m wide and 4.5m water depth. The
whole structure has a capacity of approximately 5,500m3
.
During the design phase, anti-floatation was identified as a
particular requirement given this size of the structure and its
location close to the River Lagan. Initial excavation identified
a natural water table level which was 3m above the proposed
finished floor. Rock tests were then carried out and rock anchoring
was the proposed solution.
To anchor the tank sufficiently it required 24 (No.) anchors each
14.5m in length into the rock beneath.
The additional final tank construction was a 31m diameter tank,
with a capacity of approximately 2,800m3
. Tank design was a
traditional conical shape, but due to the existing hydraulics and
requirement to maintain gravity feed and discharge as per the
existing tanks, it therefore required construction with a top water
level approximately 2m below the surrounding ground level. The
(Left) Aerial of original plant and (right) site layout drawing. Blue: existing plant - Green: redundant plant - Orange: new plant - Both images courtesy of NI Water
Tank excavation and rock anchors - Courtesy of NI Water Dunmurry WwTW – New aeration tank construction - Courtesy of NI Water
www.WaterProjectsOnline.com	 Wastewater Treatment & Sewerage
UK Water Projects 2012	 Page 69
centre floor level was 8.3m below the surrounding ground level.
The tank was also located only 80m from the River Lagan and the
floor level was well below the normal river dry water level. As was
the case with the aeration structure, the natural water table was
only 3-4 m below the finished ground level, with a high water table
and risk of floatation, the tank also required rock anchoring. This
tank required 72 (No.) rock anchors, which were all 9m deep.
Other new plant additions include:
•	 Increased sludge blending capacity, 600m3
glass lined
tank.
•	 Refurbishment of the existing final tank sludge scrapers
and structures.
•	 Storm tank separation and river abatement measures.
•	 Return activated sludge pumping station.
•	 New power standby generator.
•	 Inlet screening conditioning and new inlet flow control
and measurement.
•	 Final effluent recycling system, replace the potable water
supply.
Final effluent recycling system
Final effluent shall be reused on the site in a plan to reduce the
potable water consumption. Within the design the contractor has
included a separate final effluent ring main on the site to feed plant
requiring backwashing. This was specifically the inlet screenings,
conditioning units and sludge plant.
Inlet works screening is the largest consumer of water on a
treatment works. Backwashing demands a high pressure of clean
water to be delivered to the spray bars and allows the screen to
operate efficiently. At this site, similar to many NI Water sites, the
objective was to eliminate potable water consumption for the
process plant, so a final effluent recirculation pumping station with
automatic filtration was added to recycle final effluent and boost
to approximately 6 Bar pressure to backwash the inlet screens and
sludge screens as demanded.
River protection and improvements
NI Water in partnership with the Graham MWH JV has developed
robust Environmental Management Plans to meet Northern Ireland
Environmental Agency (NIEA) requirements. Deep excavations
within this proximity of a main river can incur obstacles, but with
assistance and agreement with NIEA, abstracting the water locally
and discharging within their guidelines allowed the work to be
progressed without significant delay. The area and depth of the
two main excavations resulted in construction works well below
the natural water table level, particularly at a wet time of the year.
This therefore required 24-hour water drainage and was controlled
using up to 4 (No.) diesel drainage pumps during the main elements
of the deep work. This had to be carefully monitored and tested
throughout and was under licence and discharge consent from
NIEA.
Conclusion
Dunmurry WwTW is just one example of the scale of investment
required by NI Water to provide cleaner rivers and in doing so, meet
European standards and deliver a modern water and wastewater
infrastructure. The investment is also essential to protect public
health and provide Northern Ireland with a modern service
comparable with that of water companies in the UK.
This design and build project has been undertaken by NI Water
working in partnership with Jacobs consultant services, and
the joint venture contractors Graham Construction and MWH
Treatment.
The editor & publishers thank Derek Crabbe, Project Manager with
NI Water, for providing the above article for publication.
DESIGN, MANUFACTURE, INSTALLATION AND COMMISSIONING
OF MATERIALS HANDLING EQUIPMENT.
CTM Systems Ltd are proud to have designed, manufactured and installed various shaftless screw conveyors for the new sludge dewatering
equipment at Northern Ireland Water’s Dunmurry WwTW. CTM supplied the 6 (No.) transfer conveyors which transfer the sludge cake to one of
three trailer/skip filling points within the new sludge treatment building. The conveyors are due to be commissioned in Q3/Q4 of 2013.
SUPPLIERS OF:
 Sludge cake reception bunkers
 Sludge cake storage silos
 Shafted and shaftless screw conveyors
 Fixed and radial conveyors
 Live bottom bins
 Dried sludge cooling screws
 Screenings handling conveyors
 Troughed belt conveyors
 Continuous mixers/blenders
CTM Systems Limited
Atherstone House
The Sidings
Merrylees Industrial Estate
Merrylees, Leicester LE9 9FE
Phone: 08450 775512
Fax: 08450 775513
Email: sales@ctm-systems.co.uk
Web: www.ctm-systems.co.uk

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NI_Water_Dunmurry_2012

  • 1. D unmurry Wastewater Treatment Works (WwTW) is located on the outskirts of Dunmurry Village, on the Lisburn side of Belfast City. It is located on the banks of the River Lagan, approximately 8km south of Belfast City centre. Previous upgrades were carried out in 1984 when modern inlet screening, grit plant, and storm storage were added, and in 1999, when a tertiary filtration plant and sludge dewatering plant were added to help improve the treatment and reduce the operational transport of sludges from the site. This was successfully operated for many years, but in 2009 the works failed to comply with its discharge consents and an upgrade was urgently required to meet the growing population in the area. NI Water invested £5.5 million to upgrade the Dunmurry treatment process capacity to PE 62,500 and meet the required standards. Work commenced at the site in June 2010, and was completed in June 2012. Objectives/need The old treatment works was in need of modernisation; nearly all elements of the works operation were manual or required manual intervention. The plant demanded two full time operators, with support from M&E and additional reclamation staff in order to maintain compliance. De-sludging, returning storm and general site maintenance operations were manually carried out, which resulted in significant overtime on weekends and very careful sludgemanagementtodealwiththelackofcapacity.Frequentlythe sludge export had to be carried out after hours in order to provide sufficient space for holiday periods and planned maintenance. www.WaterProjectsOnline.com Wastewater Treatment & Sewerage UK Water Projects 2012 Page 67 Dunmurry WwTW £5.5m upgrade to an outdated works in South Belfast to serve an increasing population and meet nitrogen and phosphorous consent conditions by Derek Crabbe BSc (Hons) Dunmurry WwTW – Aeration tank fine bubble membrane installation - Courtesy of NI Water This upgrade was also designed to meet new total nitrogen and total phosphorous discharge consent conditions. It will also ensure the works can meet its future full flow to treatment capacity and allow for further development in the catchments. The works required modernisation to automate the treatment process. It required modern control functionality such as historical data recording to ensure it was compliant with the permits and licensing agreements. The new control plant shall utilise SCADA Wiscon and operator controls shall be via one of three touch screen HMIs on the site.
  • 2. Wastewater Treatment & Sewerage www.WaterProjectsOnline.com Page 68 UK Water Projects 2012 This software also allows the site manager to remote dial up to the site, and provides them with full control of any plant connected to the PLC network. This provides invaluable information for the managers when alarms occur out of hours! Operations required a robust plant that would deliver consistent treatment for the lowest operating cost. The plant chosen was based around an activated sludge process, which was similar to the original plant and is familiar to the operators. It also provides a flexible treatment process which will treat the current flows and respond to the increased capacity demands for the area in the future. The future consent standards to be achieved are: Parameter 95 Percentile Upper tier limit Biochemical Oxygen Demand 10mg/l 50mg/l Suspended Solids 25mg/l 65mg/l Ammonia 2.5mg/l 10mg/l Total Phosphorous as P n/a 2mg/l (annual average) Total Nitrogen as N n/a 15mg/l (annual average) The aim of the works upgrade is to provide a treatment facility that complies with European Union legalisation, and it is designed to meet these needs for South Belfast catchments up to the year 2030. Considering the projected combined population growth in the area, the works has been designed to 62,500 PE. Solution The existing site was selected as the obvious location to construct theupgrade,asthesitebenefitedfromalltheplanningrequirements to provide a WwTW. Space on the site was at a premium, and the optimum location was chosen with the requirement to carry out a substantial excavation. While this location for the main tank was on an embankment, the location still allowed for a relatively easy connection as a parallel process and negated the need for pumping or affecting the existing plant hydraulics. The existing tanks, which were previously surface aerated, now presented the opportunity to fit fine bubble aeration, a more efficient process and more economical to operate. Additional controls were also possible and now the plant operates much more efficiently where the aeration capacity is increased to match the demand. The new aeration lane was designed in accordance with the latest research into aeration lane design. The split structure is approximately 80m long x 18m wide and 4.5m water depth. The whole structure has a capacity of approximately 5,500m3 . During the design phase, anti-floatation was identified as a particular requirement given this size of the structure and its location close to the River Lagan. Initial excavation identified a natural water table level which was 3m above the proposed finished floor. Rock tests were then carried out and rock anchoring was the proposed solution. To anchor the tank sufficiently it required 24 (No.) anchors each 14.5m in length into the rock beneath. The additional final tank construction was a 31m diameter tank, with a capacity of approximately 2,800m3 . Tank design was a traditional conical shape, but due to the existing hydraulics and requirement to maintain gravity feed and discharge as per the existing tanks, it therefore required construction with a top water level approximately 2m below the surrounding ground level. The (Left) Aerial of original plant and (right) site layout drawing. Blue: existing plant - Green: redundant plant - Orange: new plant - Both images courtesy of NI Water Tank excavation and rock anchors - Courtesy of NI Water Dunmurry WwTW – New aeration tank construction - Courtesy of NI Water
  • 3. www.WaterProjectsOnline.com Wastewater Treatment & Sewerage UK Water Projects 2012 Page 69 centre floor level was 8.3m below the surrounding ground level. The tank was also located only 80m from the River Lagan and the floor level was well below the normal river dry water level. As was the case with the aeration structure, the natural water table was only 3-4 m below the finished ground level, with a high water table and risk of floatation, the tank also required rock anchoring. This tank required 72 (No.) rock anchors, which were all 9m deep. Other new plant additions include: • Increased sludge blending capacity, 600m3 glass lined tank. • Refurbishment of the existing final tank sludge scrapers and structures. • Storm tank separation and river abatement measures. • Return activated sludge pumping station. • New power standby generator. • Inlet screening conditioning and new inlet flow control and measurement. • Final effluent recycling system, replace the potable water supply. Final effluent recycling system Final effluent shall be reused on the site in a plan to reduce the potable water consumption. Within the design the contractor has included a separate final effluent ring main on the site to feed plant requiring backwashing. This was specifically the inlet screenings, conditioning units and sludge plant. Inlet works screening is the largest consumer of water on a treatment works. Backwashing demands a high pressure of clean water to be delivered to the spray bars and allows the screen to operate efficiently. At this site, similar to many NI Water sites, the objective was to eliminate potable water consumption for the process plant, so a final effluent recirculation pumping station with automatic filtration was added to recycle final effluent and boost to approximately 6 Bar pressure to backwash the inlet screens and sludge screens as demanded. River protection and improvements NI Water in partnership with the Graham MWH JV has developed robust Environmental Management Plans to meet Northern Ireland Environmental Agency (NIEA) requirements. Deep excavations within this proximity of a main river can incur obstacles, but with assistance and agreement with NIEA, abstracting the water locally and discharging within their guidelines allowed the work to be progressed without significant delay. The area and depth of the two main excavations resulted in construction works well below the natural water table level, particularly at a wet time of the year. This therefore required 24-hour water drainage and was controlled using up to 4 (No.) diesel drainage pumps during the main elements of the deep work. This had to be carefully monitored and tested throughout and was under licence and discharge consent from NIEA. Conclusion Dunmurry WwTW is just one example of the scale of investment required by NI Water to provide cleaner rivers and in doing so, meet European standards and deliver a modern water and wastewater infrastructure. The investment is also essential to protect public health and provide Northern Ireland with a modern service comparable with that of water companies in the UK. This design and build project has been undertaken by NI Water working in partnership with Jacobs consultant services, and the joint venture contractors Graham Construction and MWH Treatment. The editor & publishers thank Derek Crabbe, Project Manager with NI Water, for providing the above article for publication. DESIGN, MANUFACTURE, INSTALLATION AND COMMISSIONING OF MATERIALS HANDLING EQUIPMENT. CTM Systems Ltd are proud to have designed, manufactured and installed various shaftless screw conveyors for the new sludge dewatering equipment at Northern Ireland Water’s Dunmurry WwTW. CTM supplied the 6 (No.) transfer conveyors which transfer the sludge cake to one of three trailer/skip filling points within the new sludge treatment building. The conveyors are due to be commissioned in Q3/Q4 of 2013. SUPPLIERS OF:  Sludge cake reception bunkers  Sludge cake storage silos  Shafted and shaftless screw conveyors  Fixed and radial conveyors  Live bottom bins  Dried sludge cooling screws  Screenings handling conveyors  Troughed belt conveyors  Continuous mixers/blenders CTM Systems Limited Atherstone House The Sidings Merrylees Industrial Estate Merrylees, Leicester LE9 9FE Phone: 08450 775512 Fax: 08450 775513 Email: sales@ctm-systems.co.uk Web: www.ctm-systems.co.uk