SlideShare a Scribd company logo
1 of 10
Download to read offline
Project Lead: Eric Mosley
Assistant: Michael Logan
December 2013
• Roller Conveyor not aligned with saw table.
• Saw table was not trammed. (square in all axies)
• Saw was down.
Due to:
• Electronic issues.
• Software issues.
• Wiring issues.
• Firmware issues.
• Mechanical issues.
BEFORE AFTER
This was resolved by levelling the saw and machining a new
improved mount plate for the roller table.
Machined a new mounting plate
that would allow the conveyor
structure to be adjusted higher, so
that the roller could be leveled with
saw table top.
New mount plate allowing roller height to be
increased where previously it could not be.
BEFORE AFTER
Resolved by rotating the machine and locking its position.
Catastrophic issues with machine across the board.
At Power up the screen would display we had a
catastrophic error. (image on the right)
My attempts to clear the errors were
successful by reprogramming the CTC registry
file. (e-stop was still an issue) But once power was
cycled, all data / program was lost.
Resulting in the same error screen at each
machine power on/restart.
The issue was caused by a bad CTC
(PLC CPU) according to Joseph Machine.
They said we would need a new CTC at the cost
of $3700.00.
The CTC was repairable but expensive and we
would be down a minimum 3-4 weeks to wait
on repairs.
Replaced old battery with secured new battery.
I decided that the
issue must be with
the CMOS battery
being dead and that
replacement of the
battery would solve the
issue of data loss on power cycles.
After removal and disassembly of
the CTC I found the battery I had
assumed was the issue.
Downloaded new Program and Corrected Registry values.
After installation of the repaired CTC
unit, I reprogrammed the registry,
cycled the power and no data loss
accrued. Problem solved.
At start up I still had an error screen for
the e-stop. I later found that the PLC
program also resides on the same non-
flash memory as the Registry. I then
verified the correct PLC program and
downloaded it to the plc controller.
Cycled power and found no software
errors.
After pushing the pin(1) out of the Molex(2)
connector I found the wire(3) was not clamped to
the pin(1) at all.
I made the obvious repair here which fixed the servo
error issue for good.
After reviewing the machines schematics, I found that
the probable cause was between the CTC and Servo
Amp. After further investigation I found the signal wire
from the CTC was in the interface jack but was not
making good contact inside the Molex plug.
Saw was experiencing random episodes of errors in regards to the servo resulting in machine down scenario.
Bad wiring causing intermittent servo errors.
After reviewing the standard registry values, I found
one value to contain the incorrect value of .100”
that turned out to be the culprit. After updating this
value the issue immediately disappeared.
“The saw has had issues for years where it would cut the
first pc in every cycle after the 1st cycle .100” short.
We had them work on it but they couldn’t ever figure it
out” (Elvin Mills) Senior Maint. Supervisor.
In the past maintenance would try tightening or
loosening the drive belt tensioner in hopes to remove
backlash or tweak things which would provide very little
help.
Operators would then fudge the parts nominal length
when inputting to the saws length value.
Between these two operations one could get the bad 1st
parts and good parts to fall with-in side of the full +/-
tolerance range. However it was extremely risky as these
tolerances were borderline, more than not.
Issue that has long plagued the saw.
What was once thought to be a mechanical issue.

More Related Content

Similar to Saw Alignment, Leveling, and Software Issues Resolved Through Troubleshooting

Ete420 robot finalproject2008
Ete420 robot finalproject2008Ete420 robot finalproject2008
Ete420 robot finalproject2008Sherlyn Victoria
 
Ete420 robot finalproject2008
Ete420 robot finalproject2008Ete420 robot finalproject2008
Ete420 robot finalproject2008Sherlyn Victoria
 
VFD Trouble Shooting with Fluke ScopeMeter
VFD Trouble Shooting with Fluke ScopeMeterVFD Trouble Shooting with Fluke ScopeMeter
VFD Trouble Shooting with Fluke ScopeMeterZhaoyi Fang
 
96000707 gas-turbine-control
96000707 gas-turbine-control96000707 gas-turbine-control
96000707 gas-turbine-controlMowaten Masry
 
GSM_BASED_VOTING_SYSTEM
GSM_BASED_VOTING_SYSTEMGSM_BASED_VOTING_SYSTEM
GSM_BASED_VOTING_SYSTEMchandan mishra
 
Fault tolearant system
Fault tolearant systemFault tolearant system
Fault tolearant systemarvinthsaran
 
Maintenance and Test Equipment Cyber Security
Maintenance and Test Equipment Cyber Security Maintenance and Test Equipment Cyber Security
Maintenance and Test Equipment Cyber Security Michael Toecker
 
Emic Effects on controlling automobile safety
Emic Effects on controlling automobile safety Emic Effects on controlling automobile safety
Emic Effects on controlling automobile safety Harshit Srivastava
 
HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31
HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31
HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31Shannon Krause
 
Robotics using EV3 Introduction
Robotics using EV3 Introduction Robotics using EV3 Introduction
Robotics using EV3 Introduction Puneet Kumar
 
14_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-16
14_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-1614_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-16
14_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-16Isham Rashik
 
ppt (6).pptx
ppt (6).pptxppt (6).pptx
ppt (6).pptxPoojaG86
 
Case Study - How Proactive Electrical Maintenance team saved a Power Transformer
Case Study - How Proactive Electrical Maintenance team saved a Power TransformerCase Study - How Proactive Electrical Maintenance team saved a Power Transformer
Case Study - How Proactive Electrical Maintenance team saved a Power TransformerSystem Protection
 
On analyzing electrical systems
On analyzing electrical systemsOn analyzing electrical systems
On analyzing electrical systemsDean White
 
Yield improvement of an eeprom for automotive applications
Yield improvement of an eeprom for automotive applicationsYield improvement of an eeprom for automotive applications
Yield improvement of an eeprom for automotive applicationsPete Sarson, PH.D
 

Similar to Saw Alignment, Leveling, and Software Issues Resolved Through Troubleshooting (20)

2011 04 Ms
2011 04 Ms2011 04 Ms
2011 04 Ms
 
Ete420 robot finalproject2008
Ete420 robot finalproject2008Ete420 robot finalproject2008
Ete420 robot finalproject2008
 
Ete420 robot finalproject2008
Ete420 robot finalproject2008Ete420 robot finalproject2008
Ete420 robot finalproject2008
 
VFD Trouble Shooting with Fluke ScopeMeter
VFD Trouble Shooting with Fluke ScopeMeterVFD Trouble Shooting with Fluke ScopeMeter
VFD Trouble Shooting with Fluke ScopeMeter
 
Final Results Memo
Final Results MemoFinal Results Memo
Final Results Memo
 
96000707 gas-turbine-control
96000707 gas-turbine-control96000707 gas-turbine-control
96000707 gas-turbine-control
 
lect18.pdf
lect18.pdflect18.pdf
lect18.pdf
 
GSM_BASED_VOTING_SYSTEM
GSM_BASED_VOTING_SYSTEMGSM_BASED_VOTING_SYSTEM
GSM_BASED_VOTING_SYSTEM
 
Fault tolearant system
Fault tolearant systemFault tolearant system
Fault tolearant system
 
Maintenance and Test Equipment Cyber Security
Maintenance and Test Equipment Cyber Security Maintenance and Test Equipment Cyber Security
Maintenance and Test Equipment Cyber Security
 
Emic Effects on controlling automobile safety
Emic Effects on controlling automobile safety Emic Effects on controlling automobile safety
Emic Effects on controlling automobile safety
 
HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31
HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31
HighLevelApplciationsForAccelerators_ShannonKrause_2009_07_31
 
Robotics using EV3 Introduction
Robotics using EV3 Introduction Robotics using EV3 Introduction
Robotics using EV3 Introduction
 
oct17
oct17oct17
oct17
 
14_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-16
14_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-1614_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-16
14_H00141747_Doula Isham_B30UC_Power System Transient Stability_Poster_2015-16
 
ppt (6).pptx
ppt (6).pptxppt (6).pptx
ppt (6).pptx
 
Case Study - How Proactive Electrical Maintenance team saved a Power Transformer
Case Study - How Proactive Electrical Maintenance team saved a Power TransformerCase Study - How Proactive Electrical Maintenance team saved a Power Transformer
Case Study - How Proactive Electrical Maintenance team saved a Power Transformer
 
mechatronics report
mechatronics reportmechatronics report
mechatronics report
 
On analyzing electrical systems
On analyzing electrical systemsOn analyzing electrical systems
On analyzing electrical systems
 
Yield improvement of an eeprom for automotive applications
Yield improvement of an eeprom for automotive applicationsYield improvement of an eeprom for automotive applications
Yield improvement of an eeprom for automotive applications
 

Saw Alignment, Leveling, and Software Issues Resolved Through Troubleshooting

  • 1. Project Lead: Eric Mosley Assistant: Michael Logan December 2013
  • 2. • Roller Conveyor not aligned with saw table. • Saw table was not trammed. (square in all axies) • Saw was down. Due to: • Electronic issues. • Software issues. • Wiring issues. • Firmware issues. • Mechanical issues.
  • 3. BEFORE AFTER This was resolved by levelling the saw and machining a new improved mount plate for the roller table.
  • 4. Machined a new mounting plate that would allow the conveyor structure to be adjusted higher, so that the roller could be leveled with saw table top. New mount plate allowing roller height to be increased where previously it could not be.
  • 5. BEFORE AFTER Resolved by rotating the machine and locking its position.
  • 6. Catastrophic issues with machine across the board. At Power up the screen would display we had a catastrophic error. (image on the right) My attempts to clear the errors were successful by reprogramming the CTC registry file. (e-stop was still an issue) But once power was cycled, all data / program was lost. Resulting in the same error screen at each machine power on/restart. The issue was caused by a bad CTC (PLC CPU) according to Joseph Machine. They said we would need a new CTC at the cost of $3700.00. The CTC was repairable but expensive and we would be down a minimum 3-4 weeks to wait on repairs.
  • 7. Replaced old battery with secured new battery. I decided that the issue must be with the CMOS battery being dead and that replacement of the battery would solve the issue of data loss on power cycles. After removal and disassembly of the CTC I found the battery I had assumed was the issue.
  • 8. Downloaded new Program and Corrected Registry values. After installation of the repaired CTC unit, I reprogrammed the registry, cycled the power and no data loss accrued. Problem solved. At start up I still had an error screen for the e-stop. I later found that the PLC program also resides on the same non- flash memory as the Registry. I then verified the correct PLC program and downloaded it to the plc controller. Cycled power and found no software errors.
  • 9. After pushing the pin(1) out of the Molex(2) connector I found the wire(3) was not clamped to the pin(1) at all. I made the obvious repair here which fixed the servo error issue for good. After reviewing the machines schematics, I found that the probable cause was between the CTC and Servo Amp. After further investigation I found the signal wire from the CTC was in the interface jack but was not making good contact inside the Molex plug. Saw was experiencing random episodes of errors in regards to the servo resulting in machine down scenario. Bad wiring causing intermittent servo errors.
  • 10. After reviewing the standard registry values, I found one value to contain the incorrect value of .100” that turned out to be the culprit. After updating this value the issue immediately disappeared. “The saw has had issues for years where it would cut the first pc in every cycle after the 1st cycle .100” short. We had them work on it but they couldn’t ever figure it out” (Elvin Mills) Senior Maint. Supervisor. In the past maintenance would try tightening or loosening the drive belt tensioner in hopes to remove backlash or tweak things which would provide very little help. Operators would then fudge the parts nominal length when inputting to the saws length value. Between these two operations one could get the bad 1st parts and good parts to fall with-in side of the full +/- tolerance range. However it was extremely risky as these tolerances were borderline, more than not. Issue that has long plagued the saw. What was once thought to be a mechanical issue.