The document discusses a well that was shut in due to low water and oil production. It was located near an oil water contact in a bottom water drive reservoir. The well was squeezed in 2006, 2007, and 2008. It was recompleted in 2010 and maintenance was performed, including a gravel pack and cleaning. When casing collapsed in one well, it was producing 150 barrels of oil per day. Another well was recompleted and initially produced 462 barrels of oil per day.