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Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 1
                     (As of 13:00 April 3rd, 2011) Major Events after the earthquake
                              Spent Fuel Pool Water Temperature - ℃                                             11th 14:46  Under operation, Automatic 
     Spent Fuel               Condition: Indicator failure                                                          shutdown by the earthquake
    Pool Cooling                                                                                                11th 15:42   Report based on the Article 10 (Total 
      System                                          Reactor Pressure A 0.394MPa*                                  loss of A/C power)
                                                      Reactor Pressure B 0.648MPa*                              11th 16:36 Occurrence of the Article 15 event 
                                                      Condition : No large fluctuation                              (Inability of water injection of the Emergency 
                                                      *converted to absolute pressure                               Core Cooling System )
                                                                                                                12 th 01:20 Occurrence of the Article 15 event 
                                                      Reactor Water Level A -1,650mm
                                                      Reactor Water Level B -1,650mm                                (Unusual rise of the pressure in PCV)
                                                      Condition: No flooding of top of active                   12th 10:17 Started to vent.
                                                                                                                12 th 15:36 Sound of explosion
                                                        fuel until the above level
                                                                                                                12th 20:20   Started to inject seawater and 
                                                      Reactor Water Temperature -                  ℃                borated water to core.
                                                      Condition: No data available                              23rd 02:33     The amount of injected water to 
                                                                                                                    the Rector Core was increased utilizing the 
                                                        Reactor Pressure Vessel (RPV)                               Feedwater Line in addition to the Fire 
                                                        Temperature:                                                Extinguish Line. (2m3/h →18m3/h)
                                                      Feedwater Nozzle Temperature                                  09:00     Switched to the Feedwater Line  
                                                                                         :252.8℃                    only.(18m3/h →11m3/h)
                                                      Temperature at the bottom head of                         24th 11:30 Lighting in the Central Control Room 
                                                        RPV                                    :116.7℃              was recovered.
                                                                                                                25th 15:37 Started fresh water injection.
                                                                                                                29th 08:32 Switched to the water injection to the 
                                                                                                                    core using the temporary motor‐driven pump.
                                                                                                                31st 12:00 ~2nd 15:26 Started to transfer  the 
                                                      PCV*3 Pressure 0.155MPa                                       stagnant water from the Condensate Storage 
                                                                                                                    Tank (CST) to the  Surge Tank of Suppression 
                                                      Condition: No large fluctuation                               Pool Water (SPT)
                                                                                                                31st 13:03~16:04 Fresh water spray by 
                                                       S/P*4 Water Temperature -                    ℃               Concrete  Pump Truck (Fresh water)
                                                       Condition: No data available                             3rd 12:02 The power supply to the temporary 
                                                       S/P*4 Pressure 0.155MPa                                      motor‐driven pump was switched from the 
           External          EDG*2       RHRS*1        Condition: No large fluctuation                              temporary power supply to the external 
            Power                                                                                                   power supply.



        *1 Residual Heat Removal System
        *2 Emergency Diesel Generator                     Current Conditions :: Fresh water is being injected to the Spent Fuel Pool
                                                          Current Conditions Fresh water is being injected to the Spent Fuel Pool
        *3 Primary Containment Vessel
        *4 Suppression Pool                               and the core
                                                          and the core
                                                                 (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)




Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 2
                 (As of 13:00 April 3rd, 2011)  Major Events after the earthquake
                                                                                                         11th 14:46  Under operation, Automatic shutdown by the 
                                                                                                                earthquake
                        Spent Fuel Pool Water Temperature  61.0 ℃                                        11th 15:42 Report based on the Article 10 (Total loss of A/C 
  Spent Fuel 
 Pool Cooling                                                                                                   power) 
                                                                                                         11th 16:36 Occurrence of the Article 15 event (Inability of water 
   System                                                                                                       injection of the Emergency Core Cooling System )
                                                   Reactor Pressure A 0.085MPa*                          13th 11:00 Started to vent.
                                                   Reactor Pressure B 0.083MPa*                              th
                                                                                                         14 13:25 Occurrence of the Article 15 event (Loss of reactor 
                                                   Condition:No large fluctuation                               cooling functions)
                                                    *converted to absolute pressure                      14th 16:34 Started to inject seawater to the Reactor Core.
                                                   Reactor Water Level A -1,500mm                        14th 22:50 Occurrence of the Article 15 event (Unusual rise of 
                                                   Condition:No flooding of top of active fuel                  the pressure in PCV)
                                                    to the above level                                   15th 00:02 Started to vent.
                                                                                                             th
                                                                                                         15 06:10 Sound of explosion
                                                   Reactor Water Temperature - ℃                         15th around 06:20 Possible damage of the suppression 
                                                   Condition:No data available
                                                                                                                chamber 
                                                   Reactor Pressure Vessel (RPV)                         20th   15:05~17:20 Approximately 40 ton seawater injection to 
                                                    Temperature:                                                the Spent Fuel Pool (SFP) via the Fuel Pool Cooling Line 
                                                   Feedwater Nozzle Temperature 150.5℃                          (FPC)
                                                   Temperature at the bottom head of RPV                 20th 15:46  Power Center received electricity.
                                                                                                             st
                                                    - ℃ (Indicator failure)                              21 18:22  White smoke generated. The smoke died down and 
                                                                                                                almost invisible at 07:11 March 22nd.
                                                                                                         22nd 16:07 Injection of around 18 tons of seawater to SFP
                                                                                                         25th 10:30~12:19 Sea water injection to SFP via FPC
                                                                                                         26th 10:10 Started to inject fresh water to the Reactor Core.
                                                   PCV*3 Pressure 0.105MPa                               26th 16:46  Lighting in the Central Control Room was recovered.
                                                                                                         27th 18:31 Switched to the water injection to the core using the 
                                                   Condition: No large fluctuation                              temporary motor‐driven pump.
        Possible damage                                                                                  29th 16:30~18:25 Switched to the temporary motor‐driven 
        of the suppression                                                                                      pump injecting fresh water to SFP. 
        chamber                                     S/P*4 Water Temperature - ℃                          29th 16:45~1st 11:50  Transferred  the water from the 
                                                    Condition: No data available                                Condensate Storage Tank (CST) to the  Surge Tank of 
                                                    S/P*4 Pressure - MPa                                        Suppression Pool Water (SPT)
                                                    Condition: Down scale (under survey)                 30th 9:25~23:50 Confirmed malfunction of the temporary 
                                                                                                                motor‐driven pump injecting fresh water to SFP(9:45). 
                                                                                                                Switched to the injection using the fire pump Truck, but 
     External                         RHRS *1                                                                   suspended as cracks were confirmed in the  hose. (12:47, 
      Power          EDG*2                                                                                      13:10) Resumed injection of fresh water(19:05)
                                                                                                          st
                                                                                                         1 14:56~17:05 Injection of fresh water from FPC to SFP 
                                                     Current Conditions:Fresh water is
                                                     Current Conditions:Fresh water is
                                                                                                                using the temporary motor‐driven pump. 
                                                     being injected to the Spent Fuel
                                                     being injected to the Spent Fuel                    2nd 17:10  Started to transfer  the water from the condenser to 
                                                     Pool and the core
                                                     Pool and the core                                          the Condensate Storage Tank (CST). 
 *1 Residual Heat Removal System                                                                         3rd 12:12 The power supply to the temporary motor‐driven 
 *2 Emergency Diesel Generator 
 *3 Primary Containment Vessel                                                                                  pump was switched from the temporary power supply to 
 *4 Suppression Pool                                                                                            the external power supply.
                                                                 (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)
Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 3
                                                Major Events after the earthquake
             (As of 13:00 April 3rd, 2011)                                                 11th 14:46 Under operation, Automatic shutdown by the earthquake
                                                                                           11th 15:42 Report based on the Article 10 (Total loss of A/C power)
                     Spent Fuel Pool Water Temperature     - ℃                             13th 05:10 Occurrence of the Article 15 event (Inability of water injection 
                     Condition:Indicator failure                                             of the Emergency Core Cooling System)
  Spent Fuel                                                                               13th 08:41 Started to vent. 
                                                                                           13th 13:12 Started to inject seawater and borated water to core.
 Pool Cooling                                                                              14th 05:20  Started to vent.
   System                                       Reactor Pressure A   0.112MPa*
                                                                                           14th 07:44  Occurrence of the Article 15 event (Unusual rise of the 
                                                                                             pressure in PCV)
                                                Reactor Pressure C 0.018MPa*               14th 11:01  Sound of explosion
                                                Condition: No large fluctuation            16th around 08:30 White smoke generated.
                                                 *converted to absolute pressure           17th 09:48~10:01 Water discharge by the helicopters of Self‐Defense 
                                                Reactor Water Level A -1,850mm               Force
                                                Reactor Water Level B -2,250mm             17th 19:05~19:15 Water spray from the ground by High pressure water‐
                                                Condition:No flooding of top of active       cannon trucks of Police
                                                                                           17th 19:35~20:09 Water spray from the ground by fire engines of Self‐
                                                fuel to the above level                      Defense Force 
                                                                                           18th before 14:00~14:38 Water spray from the ground by 6 fire engines 
                                                Reactor Water Temperature -℃                 of Self‐Defense Force
                                                Condition:No data available                18th ~14:45  Water spray from the ground by a fire engine of the US 
                                                                                             Military
                                                                                           19th 00:30 ~01:10 Water spray by Hyper Rescue Unit of Tokyo Fire 
                                                Reactor Pressure Vessel (RPV)                Department
                                                Temperature                                19th 14:10 ~ 20th 03:40 Water spray by Hyper Rescue Unit of Tokyo Fire 
                                                Feedwater Nozzle Temperature                 Department
                                                                                           20th 11:00  Pressure of PCV rose(320kPa).Afterward fell. 
                                                                   : 90.6℃(under survey)   20th 21:36 ~ 21st 03:58 Water spray by Hyper Rescue Unit of Tokyo Fire 
                                                Temperature at the bottom head of            Department
                                                                                           21st around 15:55  Grayish  smoke generated and was confirmed to be 
                                                RPV             :  114.3℃                    died down at 17:55.
                                                                                           22nd 15:10 ~16:00 Water spray by Hyper Rescue Unit of Tokyo Fire 
                                                                                             Department and Osaka City Fire Bureau.
                                                                                           22nd 22:46 Lighting in the Central Control Room was recovered.
                                                                                           23rd 11:03 ~13:20 Injection of about 35ton of  sea water to the Spent Fuel 
                                                 PCV*3 Pressure 0.1062MPa                    Pool (SFP)  via the Fuel Pool Cooling Line (FPC)
                                                 Condition: No large fluctuation           23rd around 16:20 Black  smoke generated and was confirmed to died 
                                                                                             down at around 23:30 and 24th 04:50.
                                                                                           24th 05:35~16:05  Approximately 120 ton sea water injection to SFP via 
                                                                                             FPC
                                                                                           25th 13:28~16:00 Water spray by Kawasaki City Fire Bureau supported by 
                                                 S/P*4 Water Temperature - ℃                 Tokyo Fire Department 
                                                 Condition:No data available               25th 18:02 Started fresh water injection to the core.
                                                 S/P*4 Pressure  0.1750MPa                 27th 12:34~14:36 Water spray by Concrete Pump Truck
                                                 Condition: No large fluctuation           28th 17:40~31st around 8:40 Transferring the water from the Condensate 
  External                                                                                   Storage Tank (CST) to the  Surge Tank of Suppression Pool Water (SPT)
                 EDG *2        RHRS*1                                                      28th 20:30 Switched to the water injection to the core using a temporary 
   Power                                                                                     motor‐driven pump.
                                                                                           29th 14:17~18:18  Fresh water spray by Concrete  Pump Truck
                                                                                           31st 16:30~19:33  Fresh water spray by Concrete  Pump Truck
                                                                                           2nd 09:52~12:54  Fresh water spray by Concrete  Pump Truck
                                            Current Conditions:Fresh water
                                             Current Conditions:Fresh water                3rd 12:18 The power supply to the temporary motor‐driven pump was 
*1 Residual Heat Removal System             is being injected to the Spent
                                             is being injected to the Spent                  switched from the temporary power supply to the external power supply.
*2 Emergency Diesel Generator               Fuel Pool and the core
*3 Primary Containment Vessel                Fuel Pool and the core
*4 Suppression Pool 
                                                                 (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)




     Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 4
                      (As of 13:00 April 3rd, 2011) Major events after the 
                                                                                                                earthquake
                                                                                                      In periodic inspection outage when the earthquake 
                                                           In periodic inspection                       occurred
      Spent Fuel                                                   outage                             14th 04:08 Water temperature in the Spent Fuel Pool 
     Pool Cooling                                                                                       (SFP), 84℃
       System                                                                                         15th 06:14 Confirmed the partial damage of wall in the 
                                                                                                        4th floor.
                                                                                                      15th 09:38 Fire occurred in the 3rd floor. (12:25
                                                         Spent Fuel Pool Water                          extinguished)
                                                         Temperature - ℃                              16th 05:45 Fire occurred. TEPCO couldn’t confirm any 
                                                         Condition: Indicator failure                   fire on the ground. (06:15)
                                                                                                      20th 08:21~09:40 Water spray over SFP by Self‐
                                                                                                        Defense Force
                                                                                                      20th around 18:30~19:46 Water spray over SFP by 
                                                                                                        Self‐Defense Force
                                                                                                      21st 06:37~08:41 Water spray over SFP by Self‐
                                                                                                        Defense Force
                                                                                                      21st around 15:00 Work for laying cable to Power 
                                                                                                        Center was completed.
                                                         No fuel is inside the                        22nd 10:35  Power Center received electricity.
                                                                                                      22nd 17:17~20:32 Water spray by Concrete  Pump 
                                                         reactor core                                   Truck
                                                                                                      23rd 10:00~13:02 Water spray by Concrete  Pump 
                                                                                                        Truck
                                                                                                      24th 14:36~17:30 Water spray by Concrete  Pump 
                                                                                                        Truck
                                                                                                      25th 06:05~10:20 Sea water injection to SFP via the 
                                                                                                        Fuel Pool Cooling Line (FPC)
                                                                                                      25th 19:05~22:07 Water spray by Concrete  Pump 
                                                                                                        Truck
                                                                                                      27th 16:55~19:25 Water spray by Concrete  Pump 
                                                                                                        Truck
                                                                                                      29th 11:50 Lighting in the Central Control Room was 
                                                                                                        recovered.
                                                                                                      30th 14:04~18:33 Water spray by Concrete Pump 
     External                                                                                           Truck (Fresh water)
      Power          EDG*2            RHRS*1                                                          1st 8:28~14:14 Water spray by Concrete Pump 
                                                                                                        Truck(Fresh water)


              *1 Residual Heat Removal System             Current Conditions:No fuel is in RPV*3..
                                                          Current Conditions:No fuel is in RPV*3
              *2 Emergency Diesel Generator
                                                          Fresh water is being injected to the Spent Fuel Pool.
                                                          Fresh water is being injected to the Spent Fuel Pool.
              *3 Reactor Pressure Vessel                          (Editorial committee for Nuclear Energy Handbook, Nuclear Energy
                                                                  Handbook)
Status of Fukushima Dai‐ichi Nuclear Power Stations Unit 5/6
            Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 5
                             (As of 14:00 March 18th, 2011)
                             (As of 13:00 April 3rd, 2011)
                 In periodic inspection outage


    Water Temperature in the Pool:29.7℃
    Condition: Recovery of heat removal function 
                                                                             Reactor Pressure:0.108MPa*
                                                                             Reactor Water Level:1,708mm
                                                                             Reactor Water Temperature: 51.5℃
                                                                             Condition:Pressure is under control.
                                                                             *converted to absolute pressure

        Spent Fuel 
       Pool Cooling 
         System                                                         Reactor Pressure Vessel Temperature:
                                                                         Monitoring by Reactor Water Temperature

※
                                                                        ※Heat removal was carried out alternately with the water in 
                                                                         the Reactor Core and in the Spent Fuel Pool.

                                                                                  Current Conditions:
                                                                                  Current Conditions:
                                                                                  20th 14:30 Cold shutdown
                                                                                  20th 14:30 Cold shutdown
                                                                                  21st 11:36 Receiving electricity from external power supply
                                                                                  21st 11:36 Receiving electricity from external power supply
                                                               ※                    rd
                                                                                  23 rd 17:24 Pump for Residual Heat Removal Seawater System
                                                                                  23 17:24 Pump for Residual Heat Removal Seawater System
           External                                                               (RHRS) was automatically stopped when the power supply was
                                                    RHRS*1                        (RHRS) was automatically stopped when the power supply was
            Power                                                                 switched from the temporary to the permanent.
                                                                                  switched from the temporary to the permanent.
                                                                                  24th 16:14 Repair of the RHRS pump was completed.
                                                                                  24th 16:14 Repair of the RHRS pump was completed.
                                                    *1 Residual Heat 
                                                                                  24th 16:35 Started to cooling.
                                                                                  24th 16:35 Started to cooling.
                                                    Removal System
                                                                          (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)




              Status of Fukushima Dai‐ichi Nuclear Power Stations Unit 5/6
            Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 6
                             (As of 14:00 March 18th, 2011)
                             (As of 13:00 April 3rd, 2011)
                In periodic inspection outage


                                   Water Temperature in the Pool:29.5℃
                                   Condition: Recovery of heat removal                          Current Conditions:
                                                                                                Current Conditions:
                                                                                                   th
                                   function.                                                    20 th 19:27 Cold shutdown
                                                                                                20 19:27 Cold shutdown
                                                                                                22nd 19:17  Receiving electricity from external power
                                                                                                22nd 19:17  Receiving electricity from external power
                                                                                                supply
                                                                                                supply



                                                     Spent Fuel Pool       ※
                                                     Cooling System


                                                                                         Reactor Pressure:0.106MPa*
                                                                                         Reactor Water Level:1,988mm
                                                                                         Rector Water Temperature:22.7℃
                                                                                         Condition: Pressure is under control.
                                                                                         *converted to absolute pressure


                                                                         Reactor Pressure Vessel Temperature:
                                                                          Monitoring by Reactor Water 
                                                                         Temperature
          External 
           Power                                         RHRS*1

                                                                   ※            ※Heat removal was carried out alternately with the water in 
                                                                                 the Reactor Core and in the Spent Fuel Pool.
                             *1 Residual Heat Removal System
                                                                             (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)

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En20110404 3-2

  • 1. Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 1 (As of 13:00 April 3rd, 2011) Major Events after the earthquake Spent Fuel Pool Water Temperature - ℃ 11th 14:46  Under operation, Automatic  Spent Fuel  Condition: Indicator failure shutdown by the earthquake Pool Cooling  11th 15:42   Report based on the Article 10 (Total  System Reactor Pressure A 0.394MPa* loss of A/C power) Reactor Pressure B 0.648MPa* 11th 16:36 Occurrence of the Article 15 event  Condition : No large fluctuation (Inability of water injection of the Emergency  *converted to absolute pressure Core Cooling System ) 12 th 01:20 Occurrence of the Article 15 event  Reactor Water Level A -1,650mm Reactor Water Level B -1,650mm (Unusual rise of the pressure in PCV) Condition: No flooding of top of active  12th 10:17 Started to vent. 12 th 15:36 Sound of explosion fuel until the above level 12th 20:20   Started to inject seawater and  Reactor Water Temperature - ℃ borated water to core. Condition: No data available 23rd 02:33     The amount of injected water to  the Rector Core was increased utilizing the  Reactor Pressure Vessel (RPV)  Feedwater Line in addition to the Fire  Temperature: Extinguish Line. (2m3/h →18m3/h) Feedwater Nozzle Temperature  09:00     Switched to the Feedwater Line   :252.8℃ only.(18m3/h →11m3/h) Temperature at the bottom head of  24th 11:30 Lighting in the Central Control Room  RPV                                    :116.7℃ was recovered. 25th 15:37 Started fresh water injection. 29th 08:32 Switched to the water injection to the  core using the temporary motor‐driven pump. 31st 12:00 ~2nd 15:26 Started to transfer  the  PCV*3 Pressure 0.155MPa stagnant water from the Condensate Storage  Tank (CST) to the  Surge Tank of Suppression  Condition: No large fluctuation Pool Water (SPT) 31st 13:03~16:04 Fresh water spray by  S/P*4 Water Temperature - ℃ Concrete  Pump Truck (Fresh water) Condition: No data available 3rd 12:02 The power supply to the temporary  S/P*4 Pressure 0.155MPa motor‐driven pump was switched from the  External  EDG*2 RHRS*1 Condition: No large fluctuation temporary power supply to the external  Power power supply. *1 Residual Heat Removal System *2 Emergency Diesel Generator  Current Conditions :: Fresh water is being injected to the Spent Fuel Pool Current Conditions Fresh water is being injected to the Spent Fuel Pool *3 Primary Containment Vessel *4 Suppression Pool  and the core and the core (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook) Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 2 (As of 13:00 April 3rd, 2011) Major Events after the earthquake 11th 14:46  Under operation, Automatic shutdown by the  earthquake Spent Fuel Pool Water Temperature  61.0 ℃ 11th 15:42 Report based on the Article 10 (Total loss of A/C  Spent Fuel  Pool Cooling  power)  11th 16:36 Occurrence of the Article 15 event (Inability of water  System injection of the Emergency Core Cooling System ) Reactor Pressure A 0.085MPa* 13th 11:00 Started to vent. Reactor Pressure B 0.083MPa* th 14 13:25 Occurrence of the Article 15 event (Loss of reactor  Condition:No large fluctuation  cooling functions) *converted to absolute pressure 14th 16:34 Started to inject seawater to the Reactor Core. Reactor Water Level A -1,500mm 14th 22:50 Occurrence of the Article 15 event (Unusual rise of  Condition:No flooding of top of active fuel  the pressure in PCV) to the above level 15th 00:02 Started to vent. th 15 06:10 Sound of explosion Reactor Water Temperature - ℃ 15th around 06:20 Possible damage of the suppression  Condition:No data available chamber  Reactor Pressure Vessel (RPV)  20th   15:05~17:20 Approximately 40 ton seawater injection to  Temperature: the Spent Fuel Pool (SFP) via the Fuel Pool Cooling Line  Feedwater Nozzle Temperature 150.5℃ (FPC) Temperature at the bottom head of RPV   20th 15:46  Power Center received electricity. st - ℃ (Indicator failure) 21 18:22  White smoke generated. The smoke died down and  almost invisible at 07:11 March 22nd. 22nd 16:07 Injection of around 18 tons of seawater to SFP 25th 10:30~12:19 Sea water injection to SFP via FPC 26th 10:10 Started to inject fresh water to the Reactor Core. PCV*3 Pressure 0.105MPa 26th 16:46  Lighting in the Central Control Room was recovered. 27th 18:31 Switched to the water injection to the core using the  Condition: No large fluctuation temporary motor‐driven pump. Possible damage 29th 16:30~18:25 Switched to the temporary motor‐driven  of the suppression pump injecting fresh water to SFP.  chamber S/P*4 Water Temperature - ℃ 29th 16:45~1st 11:50  Transferred  the water from the  Condition: No data available Condensate Storage Tank (CST) to the  Surge Tank of  S/P*4 Pressure - MPa Suppression Pool Water (SPT) Condition: Down scale (under survey) 30th 9:25~23:50 Confirmed malfunction of the temporary  motor‐driven pump injecting fresh water to SFP(9:45).  Switched to the injection using the fire pump Truck, but  External  RHRS *1 suspended as cracks were confirmed in the  hose. (12:47,  Power EDG*2 13:10) Resumed injection of fresh water(19:05) st 1 14:56~17:05 Injection of fresh water from FPC to SFP  Current Conditions:Fresh water is Current Conditions:Fresh water is using the temporary motor‐driven pump.  being injected to the Spent Fuel being injected to the Spent Fuel 2nd 17:10  Started to transfer  the water from the condenser to  Pool and the core Pool and the core the Condensate Storage Tank (CST).  *1 Residual Heat Removal System 3rd 12:12 The power supply to the temporary motor‐driven  *2 Emergency Diesel Generator  *3 Primary Containment Vessel pump was switched from the temporary power supply to  *4 Suppression Pool  the external power supply. (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)
  • 2. Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 3 Major Events after the earthquake (As of 13:00 April 3rd, 2011) 11th 14:46 Under operation, Automatic shutdown by the earthquake 11th 15:42 Report based on the Article 10 (Total loss of A/C power) Spent Fuel Pool Water Temperature - ℃ 13th 05:10 Occurrence of the Article 15 event (Inability of water injection  Condition:Indicator failure of the Emergency Core Cooling System) Spent Fuel  13th 08:41 Started to vent.  13th 13:12 Started to inject seawater and borated water to core. Pool Cooling  14th 05:20  Started to vent. System Reactor Pressure A   0.112MPa* 14th 07:44  Occurrence of the Article 15 event (Unusual rise of the  pressure in PCV) Reactor Pressure C 0.018MPa* 14th 11:01  Sound of explosion Condition: No large fluctuation  16th around 08:30 White smoke generated. *converted to absolute pressure 17th 09:48~10:01 Water discharge by the helicopters of Self‐Defense  Reactor Water Level A -1,850mm Force Reactor Water Level B -2,250mm 17th 19:05~19:15 Water spray from the ground by High pressure water‐ Condition:No flooding of top of active  cannon trucks of Police 17th 19:35~20:09 Water spray from the ground by fire engines of Self‐ fuel to the above level Defense Force  18th before 14:00~14:38 Water spray from the ground by 6 fire engines  Reactor Water Temperature -℃ of Self‐Defense Force Condition:No data available 18th ~14:45  Water spray from the ground by a fire engine of the US  Military 19th 00:30 ~01:10 Water spray by Hyper Rescue Unit of Tokyo Fire  Reactor Pressure Vessel (RPV)  Department Temperature 19th 14:10 ~ 20th 03:40 Water spray by Hyper Rescue Unit of Tokyo Fire  Feedwater Nozzle Temperature Department 20th 11:00  Pressure of PCV rose(320kPa).Afterward fell.  : 90.6℃(under survey) 20th 21:36 ~ 21st 03:58 Water spray by Hyper Rescue Unit of Tokyo Fire  Temperature at the bottom head of  Department 21st around 15:55  Grayish  smoke generated and was confirmed to be  RPV             :  114.3℃ died down at 17:55. 22nd 15:10 ~16:00 Water spray by Hyper Rescue Unit of Tokyo Fire  Department and Osaka City Fire Bureau. 22nd 22:46 Lighting in the Central Control Room was recovered. 23rd 11:03 ~13:20 Injection of about 35ton of  sea water to the Spent Fuel  PCV*3 Pressure 0.1062MPa Pool (SFP)  via the Fuel Pool Cooling Line (FPC) Condition: No large fluctuation 23rd around 16:20 Black  smoke generated and was confirmed to died  down at around 23:30 and 24th 04:50. 24th 05:35~16:05  Approximately 120 ton sea water injection to SFP via  FPC 25th 13:28~16:00 Water spray by Kawasaki City Fire Bureau supported by  S/P*4 Water Temperature - ℃ Tokyo Fire Department  Condition:No data available 25th 18:02 Started fresh water injection to the core. S/P*4 Pressure  0.1750MPa  27th 12:34~14:36 Water spray by Concrete Pump Truck Condition: No large fluctuation 28th 17:40~31st around 8:40 Transferring the water from the Condensate  External  Storage Tank (CST) to the  Surge Tank of Suppression Pool Water (SPT) EDG *2 RHRS*1 28th 20:30 Switched to the water injection to the core using a temporary  Power motor‐driven pump. 29th 14:17~18:18  Fresh water spray by Concrete  Pump Truck 31st 16:30~19:33  Fresh water spray by Concrete  Pump Truck 2nd 09:52~12:54  Fresh water spray by Concrete  Pump Truck Current Conditions:Fresh water Current Conditions:Fresh water 3rd 12:18 The power supply to the temporary motor‐driven pump was  *1 Residual Heat Removal System is being injected to the Spent is being injected to the Spent switched from the temporary power supply to the external power supply. *2 Emergency Diesel Generator  Fuel Pool and the core *3 Primary Containment Vessel Fuel Pool and the core *4 Suppression Pool  (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook) Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 4 (As of 13:00 April 3rd, 2011) Major events after the  earthquake In periodic inspection outage when the earthquake  In periodic inspection occurred Spent Fuel  outage 14th 04:08 Water temperature in the Spent Fuel Pool  Pool Cooling  (SFP), 84℃ System 15th 06:14 Confirmed the partial damage of wall in the  4th floor. 15th 09:38 Fire occurred in the 3rd floor. (12:25 Spent Fuel Pool Water  extinguished) Temperature - ℃ 16th 05:45 Fire occurred. TEPCO couldn’t confirm any  Condition: Indicator failure fire on the ground. (06:15) 20th 08:21~09:40 Water spray over SFP by Self‐ Defense Force 20th around 18:30~19:46 Water spray over SFP by  Self‐Defense Force 21st 06:37~08:41 Water spray over SFP by Self‐ Defense Force 21st around 15:00 Work for laying cable to Power  Center was completed. No fuel is inside the  22nd 10:35  Power Center received electricity. 22nd 17:17~20:32 Water spray by Concrete  Pump  reactor core Truck 23rd 10:00~13:02 Water spray by Concrete  Pump  Truck 24th 14:36~17:30 Water spray by Concrete  Pump  Truck 25th 06:05~10:20 Sea water injection to SFP via the  Fuel Pool Cooling Line (FPC) 25th 19:05~22:07 Water spray by Concrete  Pump  Truck 27th 16:55~19:25 Water spray by Concrete  Pump  Truck 29th 11:50 Lighting in the Central Control Room was  recovered. 30th 14:04~18:33 Water spray by Concrete Pump  External  Truck (Fresh water) Power EDG*2 RHRS*1 1st 8:28~14:14 Water spray by Concrete Pump  Truck(Fresh water) *1 Residual Heat Removal System Current Conditions:No fuel is in RPV*3.. Current Conditions:No fuel is in RPV*3 *2 Emergency Diesel Generator Fresh water is being injected to the Spent Fuel Pool. Fresh water is being injected to the Spent Fuel Pool. *3 Reactor Pressure Vessel (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)
  • 3. Status of Fukushima Dai‐ichi Nuclear Power Stations Unit 5/6 Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 5 (As of 14:00 March 18th, 2011) (As of 13:00 April 3rd, 2011) In periodic inspection outage Water Temperature in the Pool:29.7℃ Condition: Recovery of heat removal function  Reactor Pressure:0.108MPa* Reactor Water Level:1,708mm Reactor Water Temperature: 51.5℃ Condition:Pressure is under control. *converted to absolute pressure Spent Fuel  Pool Cooling  System Reactor Pressure Vessel Temperature: Monitoring by Reactor Water Temperature ※ ※Heat removal was carried out alternately with the water in  the Reactor Core and in the Spent Fuel Pool. Current Conditions: Current Conditions: 20th 14:30 Cold shutdown 20th 14:30 Cold shutdown 21st 11:36 Receiving electricity from external power supply 21st 11:36 Receiving electricity from external power supply ※ rd 23 rd 17:24 Pump for Residual Heat Removal Seawater System 23 17:24 Pump for Residual Heat Removal Seawater System External  (RHRS) was automatically stopped when the power supply was RHRS*1 (RHRS) was automatically stopped when the power supply was Power switched from the temporary to the permanent. switched from the temporary to the permanent. 24th 16:14 Repair of the RHRS pump was completed. 24th 16:14 Repair of the RHRS pump was completed. *1 Residual Heat  24th 16:35 Started to cooling. 24th 16:35 Started to cooling. Removal System (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook) Status of Fukushima Dai‐ichi Nuclear Power Stations Unit 5/6 Conditions of Fukushima Dai‐ichi Nuclear Power Station Unit 6 (As of 14:00 March 18th, 2011) (As of 13:00 April 3rd, 2011) In periodic inspection outage Water Temperature in the Pool:29.5℃ Condition: Recovery of heat removal  Current Conditions: Current Conditions: th function. 20 th 19:27 Cold shutdown 20 19:27 Cold shutdown 22nd 19:17  Receiving electricity from external power 22nd 19:17  Receiving electricity from external power supply supply Spent Fuel Pool  ※ Cooling System Reactor Pressure:0.106MPa* Reactor Water Level:1,988mm Rector Water Temperature:22.7℃ Condition: Pressure is under control. *converted to absolute pressure Reactor Pressure Vessel Temperature: Monitoring by Reactor Water  Temperature External  Power RHRS*1 ※ ※Heat removal was carried out alternately with the water in  the Reactor Core and in the Spent Fuel Pool. *1 Residual Heat Removal System (Editorial committee for Nuclear Energy Handbook, Nuclear Energy Handbook)